N2143J

RAYTHEON AIRCRAFT COMPANY 58 · 1998 · Valid Registration

Registered owner: TVPX AIRCRAFT SOLUTIONS INC TRUSTEE, UT (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
QUEST DIAGNOSTICS INC (Q5QA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2023-02-15 Matched by certificate designator
ATA 5312

DURING AN INSPECTION OF THE TAIL SECTION OF N2143J, THE AFT-MOST FUSELAGE BULKHEAD ASSEMBLY, FS 272.0, WAS NOTED CRACKED AT THE LEFT LOWER AND RIGHT LOWER RADII.

Source: SDR Q5QA20230215001 · FAA SDRS
R · 2021-03-05 Matched by certificate designator
ATA 7414

PILOT NOTED ON RUN-UP THAT THE #2 ENGINE LH MAGNETO WAS MISFIRING. THE MAGNETO WAS REPLACED WITH NO FURTHER INCIDENT. TROUBLESHOOTING DISCLOSED THE MAGNETO POINT GAP HAD APPARENTLY SHIFTED AND THE INTERNAL MAGNETO TIMING WAS SUBSTANTIALLY OUT OF LIMITS. IN ADDITION, IT WAS DISCOVERED THAT AN INCORRECT P/N MAGNETO WAS INSTALLED. ALTHOUGH THE FORM 8130-3 LISTED A P/N 10-500556-1 MAGNETO (THE CORRECT P/N FOR THIS AIRCRAFT), S/N D20GA041, THE MAGNETO DATA PLATE SHOWS A P/N 10-500556-101 MAGNETO, SAME S/N, WHICH IS A PRESSURIZED MAGNETO AND NOT APPLICABLE TO THIS AIRCRAFT/ENGINE. THE CONTINENTAL MOTORS MAGNETO WAS PURCHASED NEW FROM BOEING.

Source: SDR Q5QA2021030501 · FAA SDRS
O · 2016-11-08 Matched by certificate designator
ATA 5320

WHILE PERFORMING A ROUTINE INSPECTION, CRACKS WERE NOTED ON A LATERAL CHANNEL IN THE TAIL SECTION OF THE FUSELAGE. CRACKS WERE APPEARING ON THE UPPER LT AND RT CORNERS AT THE CUTOUT RELIEFS.

Source: SDR Q5QA20161108003 · FAA SDRS
O · 2015-09-09 Matched by certificate designator
ATA 3233

100 HOURS AGO, NOTED THA THE INBD GEAR DOOR ACTUATOR ROD BOLTS AT THE GEAR ACTUATOR CROSSARM HAD BECOME LOOSE. WE HAD REPLACED THE 130909B84 BOLT, 58-8100151, BUSHING AND THE AN960-416 WASHERS WITH NEW PARTS. WE MARKED THE HEAD OF THE BOLT TO THE ABLE TO TELL AT A GLACE IF THE BOLT IS ROTATING, WHICH PREVIOUSLY CAUSED THE COTTER PIN TO BREAK AND THE BOLT TO BECOME LOOSE ON 2 OF OUR ACFT. ON THIS INSPECTION, WE CHECKED AND NOTED THAT THE BOLT ON THE RIGHT SIDE HAD BECOME LOOSE AND AFTER LOOKING INTO IT FOUND THAT THE BUSHING HAD IDENTED ITSELF INTO THE WASHERS THAT HOLD THE PUSHROD IN PLACE, CAUSING IT TO BECOME LOOSE. IT IS OUR OPINION THAT THE BUSHING SIDEWALLS ARE TOO THIN AND UNDER THE SIDELOAD THAT IT SEES AT ALL TIMES, THE BUSING IS ABLE TO SLIDE INTO THE SPACE BETWEEN THE BOLT AND WASHERS. THIS CAN AND HAS, LEAD TO THE ARM BECOMING PINCHED AND ROTATING THE BOLT, WHICH BREAKS THE COTTER PIN AND ALLOWS THE NUT TO COME OFF. IF NOT NOTICED BY THE PILOT, THIS COULD LEAD TO THE INBOARD DOOR PUSHROD BECOMING DISENGAGED AND THE INBD DOOR COULD INTERFERE WITH THE LANDING GEAR, RESULTING IN A PARTIAL OR FULL GEAR UP LANDING. A THICKER WALLED BUSHING WOULD FIX THE PROBLEM, AND HAVE SPOKEN TO MFG ABOUT IT, BUT THEY WOULD NOT OFFER US ANLY ENGINEERING ASSISTANCE.

Source: SDR Q5Q2015F00002 · FAA SDRS