N2611

BELL HELICOPTER TEXTRON 206L-1 · 1980 · Valid Registration

Registered owner: JBI SOUTH LEASING LLC, NH (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
JOE BRIGHAM INC (FTYA)Operator2025-07-23 – 2025-07-23Operator named in NTSB report

Accident & incident history

Acc · 2025-07-23 Operator named in NTSB report
BELL HELICOPTER TEXTRON 206L-1 Fatal injury Part 137JOE BRIGHAM INC Not yet finalized — may be revised.
Source: NTSB case CEN25FA281
Accident · 1988-06-27 Unresolved
Bell 206L-1 None injuryoperator not yet resolved
Source: NTSB case FTW88DRD10

Maintenance disclosures

X J · 2016-06-06 Matched by certificate designator
ATA 7322

IN THE COURSE OF A PRACTICE AUTOROTATION, THE ENGINE FLAMED OUT WHEN THE THROTTLE WAS ROLLED TO THE IDLE DETENT POSITION.

Source: SDR YTRA2016060715801 · FAA SDRS
O · 2012-03-22 Unresolved
ATA 7323

GOVERNOR ALLOWS ENGINE TO OVERSPEED. FAILED SHOP TEST. DIASSEMBLED AND FOUND UNIT IMPROPERLY ASSEMBLED. SPOOL BUSHING ANTI-ROTATION TANG WAS ENGAGED IN LEVER SLOT.

Source: SDR 3HCR03222012 · FAA SDRS
E J Y · 2011-02-22 Matched by certificate designator
ATA 7200

IN CRUISE FLIGHT THE PILOT REPORTED HIGH FREQUENCY VIBRATION AND WHINING NOISE FROM THE ENGINE COMPARTMENT. THIS WAS FOLLOWED BY AN ENGINE CHIP LIGHT INDICATION AND NOISE AT WHICH POINT THE ENGINE LOST POWER AND PROCEDED TO SHUT DOWN.

Source: SDR YTRA1105401 · FAA SDRS
O · 2010-01-06 Matched by certificate designator
ATA 5302

CRACKED AFT UPPER LT LONGERON AT TAILBOOM ATTACH POINT.

Source: SDR YTRA1000702 · FAA SDRS
J · 2005-01-14 Matched by certificate designator
ATA 6340

JUST AFTER TAKEOFF, THE LOW ROTOR CAUTION LIGHT ILLUMINATED. 2 OR 3 SECONDS LATER, THE LOW ROTOR RPM HORN SOUNDED. ROTOR TACH INDICATIONS WERE NORMAL, PILOT RETURNED TO BASE. UPON LANDING, THE MECHANIC REMOVED AND REPLACED BOTH THE LOW ROTOR RPM AND ENGINE OUT SENSORS DUE TO CORROSION AND AC WAS OPS CHECKED AND RETURNED TO SERVICE. (K)

Source: SDR ALG2005F00016 · FAA SDRS
N · 2005-01-14 Matched by certificate designator
ATA 6340

JUST AFTER TAKEOFF, THE LOW ROTOR CAUTION LIGHT ILLUMINATED. 2 OR 3 SECONDS LATER THE LOW ROTOR RPM HORN SOUNDED. ROTOR TACH INDICATIONS WERE NORMAL, PILOT RETURNED TO BASE. UPON LANDING, THE MECHANIC REMOVED AND REPLACED BOTH THE LOW ROTOR RPM AND ENGINE. OUT SENSORS DUE TO CORROSION AND AC WAS OPS CHECKED AND RETURNED TO SERVICE. (K)

Source: SDR ALG2005F00015 · FAA SDRS
R J · 2004-05-20 Matched by certificate designator
ATA 7532

WHILE TAKING OFF, HEARD POP AND AIRCRAFT YAWED, SYMPTOMS OF A COMPRESSOR STALL. LANDED STRAIGHT AHEAD AND HAD TOWER CALL AIRLOG OPS. MAINTENANCE REMOVED BLEED VALVE AND INSTALLED SERVICEABLE BLEED VALVE (PN 23073353)(SN FF44236). ALL WORK DONE IAW 206L-1MM AND RR MM.

Source: SDR ALG2004F00026 · FAA SDRS
R J · 2004-05-20 Matched by certificate designator
ATA 7532

WHILE TAKING OFF IN HMA HEARD POP AND AIRCRAFT YAWED, SYMPTOMS OF A COMPRESSOR STALL. LANDED STRAIGHT AHEAD AND HAD TOWER CALL OPS. MAINTENANCE REMOVED BLEED VALVE AND INSTALLED SERVICEABLE BLEED VALVE PN 23073353 SN FF44236. ALL WORK IAW 206L1MM.

Source: SDR ALG2004F00025 · FAA SDRS
O · 2004-03-21 Matched by certificate designator
ATA 6210

FOUND MAIN ROTOR TRAILING EDGE EXTRUSION EXFOLIATED APPROXIMATELY 2.5.

Source: SDR ALGA093984 · FAA SDRS
J · 1999-06-22 Unresolved
ATA 7310

DURING CRUISE FLIGHT FROM OFFSHORE, PILOT NOTICED N2 DROPPING. LANDING WAS MADE - NO DAMAGE TO AIRCRAFT. DURING TROUBLESHOOTING, FOUND PC LINE FROM ACCUMULATOR TO FUEL CONTROL CRACKED AT FLARE ON POWER CONTROL SIDE CAUSING ENGINE TO SPOOL DOWN. REPLACED LINE AND TEST FLEW AIRCRAFT. OPS CHECK GOOD. TROUBLESHOOTING DID SHOW .9 VIB IN ENG AREA - FOUND AFT ADAPTER ON DRIVESHAFT FROM ENGINE TO OIL COOLER BLOWER WORN. REPLACED ADAPTER AND VIB LEVEL DROPPED TO .02. CHECK OF ADAPTER SHOWS PER MANUAL, IS STILL WITHIN LIMITS. SUBMITTER STATED THEY ARE INSPECTING FLEET FOR QUESTIONABLE LINES AND ADAPTERS.

Source: SDR 99ZZZX2651 · FAA SDRS
O · 1999-02-25 Unresolved
ATA 6320

UPON TEAR-DOWN OF TRANSMISSION FOR INSPECTION, FOUND SCREEN ASSY FULL ON PLASTIC OR NYLON PIECES. INSPECTED PLANETARY ASSY FOUND 3 EACH GEAR ASSYS WITH NO RETAINERS REMAINING, ONE EACH RETAINER WAS IN PLACE. ONCE REMOVED, IT FELL APART. UPGRADE RETAINERS TO NEW P/N 214-040-515-001.

Source: SDR 99ZZZX1247 · FAA SDRS
W · 1998-06-09 Unresolved
ATA 6720

INSTALLED OVERHAULED T/R HUB AND BLADES ON AIRCRAFT. NOTICED AFTER RIGGING T/R HORNS, P/N 206-011-809-107, THEY WERE CONTACTING T/R HUB, P/N 206-011-810-139. REMOVED AND REPLACED ASSY. INSPECTION OF REMOVED UNITS AND OF UNITS IN STOCK SHOWED THAT MACHINING OF HUBS AND HORNS IS NOT CONSISTANT. SUGGEST TRAIL AND ERROR METHOD OF MATCHING UP HORNS TO HUBS OR CHANGE TO USING 206-011-809-109 HORNS.

Source: SDR 98ZZZX2541 · FAA SDRS
O · 1997-11-12 Unresolved
ATA 6230

EXCESSIVE PLAY AT TWO PLACES. SEE BELL MM L-3 FIG 62-21. ON TEAR-DOWN, FOUND BEARINGS AND SPACERS WORN BEYOND LIMITS. TOTAL TIME OF PARTS LESS THAN 1,000 HOURS/1 YEAR SINCE REPLACEMENT.

Source: SDR 98ZZZX298 · FAA SDRS
O · 1997-10-02 Unresolved
ATA 6230

THIS IS NR 6 AND NR 7 DUPLEX BEARING CHANGE FOR BRINELLING ON RACES PARTICULARLY THE LOWER INNER RACE. ALL HAVE BEEN CHANGED WITH LESS THAN 100-HOUR TT SINCE NEW.

Source: SDR 97ZZZX4972 · FAA SDRS
O · 1996-10-07 Unresolved
ATA 6410

T/R BLADES REMOVED DUE TO FEATHERING BEARINGS WORN AND EXCESSIVE AXIAL MOVEMENT OF THE BLADES. INSPECTED BLADE FEATHERING BEARINGS PER BELL 206L MM, CH 65-30-00, PG 65-49 PARA 65-62 ITEM 6 AXIAL LOOSENESS EXCEEDED .190 INCHES AT BLADE TIP. BEARINGS REPLACED. TOTAL TIME OF OLD BEARINGS 537.7.

Source: SDR 96ZZZX6182 · FAA SDRS
O · 1996-10-07 Unresolved
ATA 6410

T/R BLADES REMOVED DUE TO FEATHERING BEARINGS WORN AND EXCESSIVE AXIAL MOVEMENT OF THE BLADES. INSPECTED BLADE FEATHERING BEARINGS PER BELL 206L MM, CH 65-30-00, PG 65-49 PARA 65-62 ITEM 6 AXIAL LOOSENESS EXCEEDED .190 INCHES AT BLADE TIP. BEARINGS REPLACED. TOTAL TIME OF OLD BEARINGS 537.7.

Source: SDR 96ZZZX6183 · FAA SDRS
O · 1996-04-25 Unresolved
ATA 3340

ON DAILY AIRWORTHY INSPECTION, FOUND STROBE LIGHT BULB BURNED OUT. HAD REPLACED BULB LAST WEEK. CAUSE OF PROBLEM UNKNOWN AT THIS TIME.

Source: SDR 96ZZZX2605 · FAA SDRS
O · 1995-12-08 Unresolved
ATA 6410

DURING ROUTINE MAINTENANCE, FOUND TAIL ROTOR BLADE INBOARD BEARING CRACKED ON BLADE, SN 452, AND SMALL INDICATION ON INBOARD BEARING, SN 446.

Source: SDR 96ZZZX1417 · FAA SDRS
O · 1995-12-08 Unresolved
ATA 6410

DURING ROUTINE MAINTENANCE, FOUND TAIL ROTOR BLADE INBOARD BEARING CRACKED ON BLADE, SN 452, AND SMALL INDICATION ON INBOARD BEARING, SN 446.

Source: SDR 96ZZZX1416 · FAA SDRS