N2649Z

CESSNA 402C · 1980 · Valid Registration

Registered owner: HYANNIS AIR SERVICE INC, MA (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
HYANNIS AIR SERVICE INC. (HYIA)Certificate holderMatched by certificate designator
HYANNIS AIR SERVICE INC. (HYIA)Operator2022-11-18 – 2022-11-18Operator named in NTSB report

Accident & incident history

Acc · 2022-11-18 Operator named in NTSB report
CESSNA 402 None injury Part 135HYANNIS AIR SERVICE INC.
Source: NTSB case ERA23LA106
Accident · 1997-09-14 Matched by aircraft (N-number)
Cessna 402C None injuryHYANNIS AIR SERVICE INC.
Source: NTSB case ANC97LA150
Accident · 1997-09-08 Matched by aircraft (N-number)
Cessna 402C None injuryHYANNIS AIR SERVICE INC.
Source: NTSB case ANC97LA145

Maintenance disclosures

B · 2018-03-11 Matched by certificate designator
ATA 2140

PILOT REPORTED SMOKE SMELL IN COCKPIT. TURNED HEATER OFF AND SMELL STOPPED. MAINTENANCE INSPECTED AND AFTER TROUBLESHOOTING DETERMINED THE HEATER ASSEMBLY WAS TO BE REPLACED. REPLACED HEATER WITH NO FURTHER DEFECTS NOTED.

Source: SDR HYIA20180314002 · FAA SDRS
O · 2017-03-06 Matched by certificate designator
ATA 3260

PILOT REPORTED NOSE GEAR COLLAPSED ON LANDING. INITIAL INSPECTION AND TESTING INDICATES A FAULTY ACTUATOR SWITCH FALSELY INDICATED GEAR WAS DOWN AND LOCKED.

Source: SDR HYIA20170308001 · FAA SDRS
O · 2015-12-11 Matched by certificate designator
ATA 2916

DURING TROUBLESHOOTING OF PILOT DISCREPANCY OF THE MLG SLOW TO RETRACT, IT WAS DISCOVERED AN INTERNAL BAFFLE OR STAND PIPE WITHIN THE MAIN HYD RESERVOIR HAD DISLODGED AND WAS BLOCKING FLOW. R & R THE HYD RESERVOIR WITH NO FURTHER DEFECTS NOTED.

Source: SDR HYIA20151217001 · FAA SDRS
B · 2014-11-25 Matched by certificate designator
ATA 2434

BITTER FUME LIKE SMELL IN CABIN. INSPECTED ELEC WIRING & FOUND NO DEFECTS. SMELL WAS DETERMINED TO BE COMING FROM THE LT ALTERNATOR. R & R THE LT ALTERNATOR & RETURNED THE ACFT TO SERVICE WITH NO FURTHER DEFECT NOTED.

Source: SDR HYIA20141126001 · FAA SDRS
O · 2012-11-29 Matched by certificate designator
ATA 3230

AT SCHEDULED INSPECTION, NLG DRAG BRACE, PN 5142002-5 WAS FOUND TO BE CRACKED IN THE AREA OF NLG ACTUATOR ATTACH POINT. METHOD OF INSPECTION WAS DYE PENETRANT. THIS CRACK WAS FOUND TO BE BEYOND LIMIT ALLOWABLE OF MEB91-11R1. THIS UNIT HAS BEEN SCRAPPED & A REPLACEMENT DRAG BRACE HAS BEEN INSTALLED IN ACFT.

Source: SDR HYIA20140414034 · FAA SDRS
O · 2012-07-10 Matched by certificate designator
ATA 3230

AT SCHEDULED INSPECTION, NLG DRAG BRACE, PN 5142002-5, WAS FOUND TO BE CRACKED IN THE AREA OF NLG ACTUATOR ATTACH POINT. METHOD OF INSPECTION WAS DYE PENETRANT. THIS CRACK WAS FOUND TO BE BEYOND LIMIT ALLOWABLE OF MEB91-11R1. THIS UNIT HAS BEEN SCRAPPED & A REPLACEMENT DRAG BRACE HAS BEEN INSTALLED IN ACFT.

Source: SDR HYIA20140414015 · FAA SDRS
O · 2012-03-02 Matched by certificate designator
ATA 3233

NOSE GEAR COLLAPSED ON LANDING. NLG ACTUATOR WAS REMOVED AND TESTED IN A CONTROLLED ENVIRONMENT. WHEN THE ACTUATOR WAS COLD SOAKED, THE SWITCH FAILED TO ACTIVATE PROPERLY GIVING A FALSE INDICATION THAT THE GEAR WAS DOWN AND LOCKED. DUE TO THE GEAR FAILURE, BOTH ACFT PROPELLERS STRUCK THE GROUND AND CAUSED SUDDEN STOPPAGE TO THE ENGINES. THE ACFT ALSO SUFFERED STRUCTURAL DAMAGE TO THE NOSE SECTION OF THE ACFT.

Source: SDR HYIA2012030251853 · FAA SDRS
O · 2011-05-27 Matched by certificate designator
ATA 3230

AT SCHEDULED INSPECTION, NLG DRAG BRACE, OEM PN 5142002-5, WAS FOUND TO BE CRACKED IN THE AREA OF NLG ACTUATOR ATTACH POINT. METHOD OF INSPECTION WAS DYE PENETRANT. THIS CRACK WAS FOUND TO BE WITHIN ALLOWABLE LIMIT. THIS UNIT HAS BEEN REPAIRED IAW PROCEDURE OUTLINED IN MEB941-11R1 & RETURNED TO SERVICE.

Source: SDR HYIA20140415059 · FAA SDRS
O · 2011-01-28 Matched by certificate designator
ATA 3230

AT SCHEDULED INSPECTION, NLG DRAG BRACE OEM PN 5142002-5 WAS FOUND TO BE CRACKED IN THE AREA OF NLG ACTUATOR ATTACH POINT. METHOD OF INSPECTION WAS DYE PENETRANT. THIS CRACK WAS FOUND TO BE WITHIN ALLOWABLE LIMIT. THIS UNIT HAS BEEN REPAIRED IAW PROCEDURE OUTLINED IN MEB941-11R1 & RETURNED TO SERVICE.

Source: SDR HYIA20140415016 · FAA SDRS
B J · 1999-08-05 Matched by certificate designator
ATA 2910

DURING FIGHT, PILOT REPORTED SMOKE IN THE COCKPIT AND RETURNED TO AIRPORT FOR AN UNEVENTFUL LANDING. THE MAINTENANCE DEPARTMENT WAS DISPATCHED. POSSIBLE CAUSE WAS HYDRAULIC MANIFOLD SOLENOID STUCK AND CAUSED SYSTEM TO OVERHEAT CAUSING A PIN HOLE IN THE HYDRAULIC SIGHT GAUGE. THIS CAUSED THE HYDRAULIC FLUID TO ESCAPE AS A MIST.

Source: SDR 99ZZZX3400 · FAA SDRS