N265CM

CESSNA 560 · 1999 · Valid Registration

Registered owner: CHARLOTTE-MECKLENBURG HOSPITAL AUTHORITY, NC (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
STERLING AVIATION, LLC (DBCA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2021-11-12 Matched by certificate designator
ATA 2420

1) DURING TAKEOFF ROLL CREW RECEIVED MASTER WARNING. 2) CREW ABORTED TAKEOFF, RETURNED TO RAMP. 3) MAINTENANCE TROUBLESHOT TO #2 INVERTER 4) MAINTENANCE REMOVED AND REPLACED #2 INVERTER 5) OPS CHECKS GOOD.

Source: SDR DBCA202111120004 · FAA SDRS
J · 2021-08-26 Matched by certificate designator
ATA 3421

ON TAXI OUT CREW NOTED AIRCRAFT ATTITUDE MISCOMPARE. AIRCRAFT RETURNED TO BLOCK. MAINTENANCE DETERMINED #2 VERTICAL GYRO HAD FAILED. #2 VERTICAL GYRO REPLACED WITH OVH UNIT. OPERATIONAL TEST OF #2 VERTICAL GYRO GOOD.

Source: SDR DBCA202108260003 · FAA SDRS
O · 2021-02-04 Matched by certificate designator
ATA 7510

AFTER TAKE-OFF CREW NOTED RT ENGINE ANTI-ICE FAIL INDICATION. CREW RETURNED TO HOME BASE. MX TROUBLESHOT. REPLACED RT ENGINE INLET ANTI-ICE SOLENOID VALVE WITH REPAIRED UNIT. OPS CHECKED GOOD

Source: SDR DBCA202102040001 · FAA SDRS
O · 2019-12-13 Matched by certificate designator
ATA 2360

1) AFTER DEPARTING CLT CREW REPORTED BOTH #1 COMM AND #2 COMM HAVE HEAVY STATIC DURING CLIMBOUT AND INTERMITTENT AT LEVEL FLIGHT. MODERATE PRECIP THROUGHOUT THE FLIGHT. 2) CREW RETURNED TO HOME BASE. LANDING WAS UNEVENTFUL. 3) TECHNICIANS TESTED ALL STATIC WICKS AND FOUND SEVERAL IN NEED OF REPLACEMENT DUE TO EROSION OR FAILURE DURING TESTING. 4) REMOVED AND REPLACED ALL WICKS AT THE LH & RH AILERON, WING TIP AND ELEVATOR WITH NEW. REMOVED AND REPLACED 3 ON RUDDER WITH NEW. TESTED WITH NO FURTHER DEFECTS.

Source: SDR DBCA2019121730006 · FAA SDRS
O · 2018-02-02 Matched by certificate designator
ATA 3231

DURING INSPECTION, NOTED THE NOSE GEAR DOORS WAS SAGGING. FURTHER INSPECTION FOUND TORQUE TUBE WELD ASSY BROKEN AT THE WELD. REPLACED TORQUE TUBE WITH NEW.

Source: SDR DBCA2018020200001 · FAA SDRS
J · 2017-11-04 Matched by certificate designator
ATA 2130

DURING TAKEOFF ROLL, CREW NOTED UNCOMMANDED HOT AIR COMING INTO CABIN AND FLUCTUATIONS IN CABIN PRESSURIZATION RATE. RETURNED TO BASE, LANDING WAS UNEVENTFUL. TROUBLESHOT AND FOUND EMERGENCY PRESSURE VALVE INTERMITTENT. REPLACED THE VALVE WITH AN OVERHAULED UNIT. OPS CHECKED GOOD.

Source: SDR DBCA2017110400004 · FAA SDRS
B · 2017-11-02 Matched by certificate designator
ATA 2120

AFTER TAKEOFF, CREW NOTED UNCOMMANDED HOT AIR COMING INTO CABIN AND FLUCTUATIONS IN CABIN PRESSURIZATION RATE. RETURNED TO BASE, LANDING WAS UNEVENTFUL. COULD NOT DUPLICATE. AIRCRAFT RETURNED TO SERVICE. NO DISCREPANCIES ON RETURN FLIGHT.

Source: SDR DBCA201711060001 · FAA SDRS