STERLING AVIATION, LLC

Part 135 operator · designator DBCA

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: AIRSHARE, CIRCADIAN AVIATION, STERLING AVIATION, LLC, Sterling Aviation, LLC

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

144 reports on file — showing most recent 50.

J · 2024-08-31 Matched by certificate designator
N279AH · ATA 3010

1) CREW RECEIVED AMBER WING ANTI-ICE FAIL AND AMBER WING ANTI-ICE VALVE CLOSED MESSAGES DURING OPERATION IN ICING CONDITIONS 2) CREW RETURNED TO HOME BASE 3) MTN TROUBLESHOT RH ANTI-ICE VALVE 4) MTN DEFERRED PER MEL 30-10-01 5) MTN REMOVED LH & RH WING ANTI-ICE VALVES AND REPLACED WITH UPDATED, REPAIRED UNITS 6) OPS CHECKS GOOD.

Source: SDR DBCA2024090410005 · FAA SDRS
J · 2024-08-07 Matched by certificate designator
N274AH · ATA 2400

1) CREW NOTED MOMENTARY MULTIPLE CASCADING CAS MESSAGES FOLLOWED BY CLEARING OF MAJORITY OF MESSAGES WITH FADEC1 FAIL REMAINING IN FLIGHT 2) CREW ELECTED TO RETURN TO BASE. 3) MTN COLLECTED ALMF AND F40B FILES AND SENT TO PILATUS. 4) CAS MESSAGE TRIGGERED BY MOMENTARY LOSS OF DCPU #3 WHICH TRIGGERED L FADEC FAIL FAULT. 5) MTN R&R DCPU #3 WITH INSPECTED UNIT. OPS CHECK GOOD.

Source: SDR DBCA202408070004 · FAA SDRS
J · 2024-05-25 Matched by certificate designator
N274AH · ATA 2430

ON TAKEOFF FROM IAD UMS DATABASE FAIL INDICATION RECEIVED. CREW ABORTED TAKEOFF AND RETURNED TO FBO. MTN CONTACTED PILATUS SUPPORT. SUSPECT PCU DEFECTIVE. MTN REPLACED #2 PCU WITH NEW UNIT. OPS CHECKS GOOD.

Source: SDR DBCA202405250003 · FAA SDRS
J · 2024-05-20 Matched by certificate designator
N274AH · ATA 3240

DURING DESCENT ON RETURN FLIGHT TO CLT CREW RECEIVED MAIN BRAKE FAIL CAS MESSAGE. CREW DECLARED AN EMERGENCY, USED LONGEST RUNWAY TO LAND, STOPPED ON RUNWAY AND USED TUG TO RAMP. MTN TROUBLESHOOTING FOUND THIS AS CAUSED BY AN INTERMITTENT QUANTITY SENSOR IN THE HYDRAULIC RESERVOIR. MTN REMOVED AND REPLACED RESERVOIR/SENSOR ASSY WITH SERVICEABLE UNIT. OPS CHECKS GOOD.

Source: SDR DBCA202405200002 · FAA SDRS
J · 2024-01-08 Matched by certificate designator
N279AH · ATA 7930

1) DURING DESCENT ON FLIGHT TO ELM CREW RECEIVED RH ENG HIGH OIL NOTICE. 2) CREW PERFORMED ENG INFLIGHT SHUTDOWN ON RH ENGINE. 3) CREW DECLARED AN EMERGENCY AND LANDED AT ELM. 4) MTN COMPLIED WITH FHDB AND WI DOWNLOADS. 5) MTN REMOVED AND REPLACED RH OIL PRESSURE TRANSDUCER W/ NEW. LEAK CHECK GOOD.

Source: SDR DBCA2024010800001 · FAA SDRS
B · 2022-12-31 Matched by certificate designator
N900LC · ATA 2400

SUPPLEMENTAL: 1) MTN REMOVED AND REPLACED #3 STARTER GENERATOR, FIELD WIRES, POSITIVE CABLE AND NEGATIVE CABLE. 2) OPS CHECKS GOOD.

Source: SDR DBCA202212310011 · FAA SDRS
J · 2022-12-31 Matched by certificate designator
N900LC · ATA 2435

NR 3 ENGINE STARTER FAILED AFTER ENGINE START. CREW SHUT DOWN ENGINE PRIOR TO PARKING BRAKE RELEASE. CONTACTED MTN, TROUBLESHOOTING IN PROGRESS. OPEN

Source: SDR DBCA202301031011 · FAA SDRS
R Y · 2022-12-20 Matched by certificate designator
N301ML · ATA 7313

PRIOR TO POWER APPLICATION ON TAKEOFF THE NR 2 ENGINE ROLLED BACK. CREW EXITED THE RUNWAY AND RETURNED TO RAMP. MTN REMOVED AND INSPECTED ENGINE. FOUND FUEL NOZZLES UNSERVICEABLE.

Source: SDR DBCA202212200010 · FAA SDRS
S · 2022-12-07 Matched by certificate designator
N301ML · ATA 3460

DURING TAKE-OFF ROLL PILOT'S PFD WENT BLANK. CREW EXECUTED A LOW SPEED ABORT AND RETURNED TO BED.MTN REMOVED AND REPLACED PILOT'S PFD WITH OVH UNIT. OPS CHECKED GOOD.

Source: SDR DBCA202212070009 · FAA SDRS
J · 2022-11-07 Matched by certificate designator
N317ML · ATA 5230

1) AFTER DEPARTURE FROM TYS CREW NOTED LOSS OF PRESSURIZATION WHILE CLIMBING THROUGH 8000'. 2) CREW RETURNED TO TYS 3) MTN FOUND BROKEN CABLE IN BAGGAGE DOOR PRESSURE FLAP SYSTEM 4) MTN REMOVED AND REPLACED CABLE WITH NEW 5) PRESSURIZATION AND OPS CHECKS GOOD.

Source: SDR DBCA202211070008 · FAA SDRS
B · 2022-11-06 Matched by certificate designator
N279AH · ATA 2140

1) CREW NOTED SMOKE IN COCKPIT/CABIN AFTER TAKE OFF. 2) CREW DECLARED AN EMERGENCY AND RETURNED TO SAT. 3) MTN FOUND RH FWD CABIN ELECTRIC HEATER/FAN PCB BURNED. 4) MTN REPLACED RH FWD CABIN ELECTRIC HEATER ASSY WITH NEW.

Source: SDR DBCA2022AA060007 · FAA SDRS
J M · 2022-07-13 Matched by certificate designator
N279AH · ATA 7200

MANUFACTURER INDICATES A FAILED BRAZE WELD ON THE #1 LPT NOZZLE GUIDE VANE WHICH ALLOWED THE NOZZLE TO FLEX AND CONTACT THE #1 LPT DISK. THIS DAMAGED THE DISK SENDING DEBRIS THROUGH THE REST OF THE TURBINE SECTION CAUSING DAMAGE THROUGHOUT. ENGINEERING IS INVESTIGATING IF THE FAILED WELD WAS THE ROOT CAUSE OR THE RESULT OF SOME OTHER FAILURE, POSSIBLY VIBRATION FROM A BEARING. AFTER REPAIR OF ENGINE NOTED FAILED PART WAS A NOZZLE/HEATSHIELD ASSY.

Source: SDR DBCA202207130006 · FAA SDRS
J · 2022-06-10 Matched by certificate designator
N210CM · ATA 3260

ON APPROACH CREW NOTED BRAKE FAILURE WITH ANTI-SKID INOP ANNUNCIATOR. CREW STOPPED THE AIRCRAFT WITH EMERGENCY BRAKE LEVER. PERFORMED ROTARY TEST OF ANTISKID SYSTEM, NO FAULTS NOTED. MAINTENANCE PERFORMED OHM READINGS OF LT AND RT WHEEL TRANDUCERS AND NOTED LT WHEEL TRANSDUCER READINGS ERRATIC AND SPIKING. MELD TRANSDUCER AND RETURNED TO HOME BASE. MTN REPLACED LT MAIN WHEEL SPEED TRANSDUCER WITH SERVICEABLE UNIT.

Source: SDR DBCA202206100005 · FAA SDRS
J · 2022-05-12 Matched by certificate designator
N279AH · ATA 3230

1) ON APPROACH WITH GEAR DOWN CREW NOTED "GEAR" ON MFD AND LH GEAR ANNUN FLICKER TO WHITE UNSAFE POSITION FOR A SECOND. IN THE FLARE AFTER RETARDING POWER HEARD AN AUDIBLE GEAR WARNING 2) MTN CHECKS SHOWED NO DEFECTS ON GROUND. 3) MTN PERFORMED CHECKS ON DOWN AND LOCK MICROSWITCHES FOR RIGGING. FOUND LH MLG SWITCH OUT OF RIG. ADJUSTED SWITCH. 4) COMPLIED WITH GEAR SWINGS WITH NO DEFECTS NOTED.

Source: SDR DBCA202205120003 · FAA SDRS
F · 2022-05-12 Matched by certificate designator
N747RX · ATA 2750

ON APPROACH TO RIL CREW NOTED FLAPS WOULD NOT DEPLOY. CREW DELCARED AN EMERGENCY AND DIVERTED TO GJT. MAINTENANCE ADJUSTED RIGGING ON LEFT INBOARD FLAP, OPS CHECK GOOD.

Source: SDR DBCA202205120004 · FAA SDRS
O · 2022-04-13 Matched by certificate designator
N196AH · ATA 3230

1) UPON ARRIVAL IN HDC CREW NOTED A BRAKE FAILURE. STERLING MAINTENANCE CONTROL CONTACTED MAINTENANCE IN HDC. MAINTENANCE REMOVED AND REPLACED BRAKE PUMP WITH REPAIRED UNIT.

Source: SDR DBCA202204130002 · FAA SDRS
K · 2022-01-05 Matched by certificate designator
N279AH · ATA 2810

1) IN FLIGHT CREW NOTED 200 LB IMBALANCE, OBSERVED FUEL LEAKING FROM LH WINGTIP AREA 2)CREW DIVERTED TO BHM 3)LANDING WAS UNEVENTFUL 4) STERLING MTN WITH PILATUS TECH SUPPORT DETERMINED THE ISSUE WAS CAUSED BY EXCESSIVE PRESSURE DURING FUELING CAUSING FUEL TO BE FORCED INTO THE CLIMB VENT LINE. ONCE AIRBORNE DIFFERENTIAL PRESSURE CAUSED THIS FUEL TO BE SIPHONED OUT UNTIL FUEL LEVEL DROPPED BELOW LEVEL OF VENT OUTLET DURING DESCENT. 5)LEAK CHECK OF SYSTEM REVEALED NO CURRENT LEAKS 6)AIRCRAFT RELEASED TO CLT

Source: SDR DBCA20220105001 · FAA SDRS
J · 2021-11-12 Matched by certificate designator
N265CM · ATA 2420

1) DURING TAKEOFF ROLL CREW RECEIVED MASTER WARNING. 2) CREW ABORTED TAKEOFF, RETURNED TO RAMP. 3) MAINTENANCE TROUBLESHOT TO #2 INVERTER 4) MAINTENANCE REMOVED AND REPLACED #2 INVERTER 5) OPS CHECKS GOOD.

Source: SDR DBCA202111120004 · FAA SDRS
J · 2021-08-26 Matched by certificate designator
N265CM · ATA 3421

ON TAXI OUT CREW NOTED AIRCRAFT ATTITUDE MISCOMPARE. AIRCRAFT RETURNED TO BLOCK. MAINTENANCE DETERMINED #2 VERTICAL GYRO HAD FAILED. #2 VERTICAL GYRO REPLACED WITH OVH UNIT. OPERATIONAL TEST OF #2 VERTICAL GYRO GOOD.

Source: SDR DBCA202108260003 · FAA SDRS
J · 2021-07-07 Matched by certificate designator
N210CM · ATA 2910

AFTER TAKE-OFF LANDING GEAR WOULD NOT RETRACT. CREW DECLARED AN EMERGENCY AND RETURNED TO CHS. MAINTENANCE TROUBLESHOT TO DEFECTIVE HYDRAULIC PRESSURE REGULATING VALVE. PRESSURE REGULATING VALVE WAS REPLACED WITH AN OVERHAULED UNIT. PERFORMED MULTIPLE EXTENSION/RETRACTION CYCLE TESTS. OPS CHECKS GOOD.

Source: SDR DBCA2021071270002 · FAA SDRS
O · 2021-04-09 Matched by certificate designator
N339SM · ATA 7800

DURING PILOTS PRE-FLIGHT INSPECTION A PORTION OF THE MIXER CASE ASSEMBLY WAS OBSERVED IN THE FAN AIR BYPASS DUCT OF THE RIGHT HAND ENGINE. FURTHER INVESTIGATION DISCOVERED MULTIPLE CRACKS AND MISSING SECTIONS OF THE ASSEMBLY. THE LEFT HAND ENGINE MIXER CASE ASSEMBLY WAS OBSERVED TO HAVE CRACKING AND MISSING SECTIONS AS WELL.

Source: SDR PAIR41221339 · FAA SDRS
O · 2021-02-04 Matched by certificate designator
N265CM · ATA 7510

AFTER TAKE-OFF CREW NOTED RT ENGINE ANTI-ICE FAIL INDICATION. CREW RETURNED TO HOME BASE. MX TROUBLESHOT. REPLACED RT ENGINE INLET ANTI-ICE SOLENOID VALVE WITH REPAIRED UNIT. OPS CHECKED GOOD

Source: SDR DBCA202102040001 · FAA SDRS
R · 2020-08-17 Matched by certificate designator
N210CM · ATA 7322

AFTER STARTING BOTH ENGINES CREW NOTED 5% SPLIT IN N2 INDICATIONS. CREW ADVANCED POWER ON BOTH ENGINES TO BEGIN TAXIING OUT OF PARKING, ONLY RT ENGINE WOULD ADVANCE IN POWER. CREW SHUT DOWN BOTH ENGINES AND CONTACTED MX. MX TROUBLESHOT AND NOTED NR 1 FUEL CONTROL REQUIRES REPLACEMENT. REMOVED AND REPLACED WITH OVH UNIT. OPS CHECKS GOOD.

Source: SDR DBCA202008170002 · FAA SDRS
O · 2019-12-13 Matched by certificate designator
N265CM · ATA 2360

1) AFTER DEPARTING CLT CREW REPORTED BOTH #1 COMM AND #2 COMM HAVE HEAVY STATIC DURING CLIMBOUT AND INTERMITTENT AT LEVEL FLIGHT. MODERATE PRECIP THROUGHOUT THE FLIGHT. 2) CREW RETURNED TO HOME BASE. LANDING WAS UNEVENTFUL. 3) TECHNICIANS TESTED ALL STATIC WICKS AND FOUND SEVERAL IN NEED OF REPLACEMENT DUE TO EROSION OR FAILURE DURING TESTING. 4) REMOVED AND REPLACED ALL WICKS AT THE LH & RH AILERON, WING TIP AND ELEVATOR WITH NEW. REMOVED AND REPLACED 3 ON RUDDER WITH NEW. TESTED WITH NO FURTHER DEFECTS.

Source: SDR DBCA2019121730006 · FAA SDRS
J · 2019-11-13 Matched by certificate designator
N339SM · ATA 2710

1) AFTER DEPARTING DTS HAD A RIGHT ROLL TRIM FAIL MESSAGE AND LEFT ROLL TRIM INTERMITTENT. 2) CREW DIVERTED TO TPA 3) CONSTANT AVIATION TROUBLESHOT AND FOUND RH SIDE FROZEN AT NEUTRAL. 4) REMOVED RH ROLL TRIM ACTUATOR AND REPLACED WITH OVH UNIT. OPS CHECKS GOOD.

Source: SDR DBCA201911153005 · FAA SDRS
J · 2019-10-07 Matched by certificate designator
N256WB · ATA 3251

ON STARTUP CREW RECEIVED NWS FAIL CAS MESSAGE. CREW SHUT DOWN AND RESTARTED - MESSAGE REMAINED. CREW RETURNED TO GATE. TROUBLESHOT AND FOUND NWS RVDT INOP. REMOVED AND REPLACED NWS RVDT WITH REPAIRED UNIT. OPS CHECKS GOOD.

Source: SDR DBCA201910107004 · FAA SDRS
J · 2019-04-28 Matched by certificate designator
N210CM · ATA 3297

1) ON APPROACH WITH LANDING GEAR SELECTED DOWN THE 3 DOWN AND LOCKED INDICATOR LIGHTS DIDN'T ILLUMINATE 2) CREW ABORTED APPROACH TO ASSESS SITUATION 3)CREW FOUND 2 AMP LANDING GEAR WARNING CB TRIPPED. CREW ATTEMPTED ONE TIME RESET FOR CHECKLIST AND DOWN AND LOCKED LIGHTS ILLUMINATED FOR SEVERAL SECONDS BEFORE CB TRIPPED AGAIN. 4)CREW PERFORMED FLY BY OF TOWER, TOWER AND ANOTHER AIRCRAFT WAITING TO DEPART VISUALLY OBSERVED LANDING GEAR APPEARED DOWN AND LOCKED 5) CREW DECLARED AN EMERGENCY AND PROCEEDED WITH LANDING. LANDING WAS UNEVENTFUL. 6) STERLING AVIATION MAINTENANCE CONTROL CONTACTED TO TROUBLESHOOT. 7) PERFORMED 10 PLUS LANDING GEAR RETRACTION, EXTENSION CYCLES WITH NORMAL OPERATION, CB DIDN'T TRIP. INSPECTED UPLOCK AND DOWNLOCK SWITCHES AND ALL ASSOCIATED WIRING. NO DEFECTS NOTED. COMPLETED UPLOCK AND DOWNLOCK SWITCH PARALLELING CIRCUIT TESTS. NO DEFECTS NOTED. 8) TECHNICIANS ARE CONTINUING TROUBLESHOOTING EFFORTS. SUPPLEMENTAL: TECHNICIANS TROUBLESHOT AND FOUND LEFT MAIN LANDING GEAR WIRE HARNESS CHAFING ON HYDRAULIC LINE. REPAIRED WIRING. OPS CHECKED GOOD.

Source: SDR DBCA201904280003 · FAA SDRS
J · 2019-03-30 Matched by certificate designator
N793CG · ATA 7910

CREW RECEIVED "CHECK OIL" AND "OIL PRESS 3" CAS MESSAGE IN FLIGHT. CREW SHUTDOWN #3 ENGINE, DECLARED EMERGENCY AND DIVERTED. FOUND OIL COOLER SUPPLY LINE CRACKED, NON-MAGNETIC MATERIAL IN INLET AND MAGNETIC DEBRIS IN TRANSFER GEARBOX. REPLACED OIL COOLER SUPPLY LINE WITH NEW P/N 3061253-5.

Source: SDR DBCA2019040130002 · FAA SDRS
O · 2019-03-11 Matched by certificate designator
N210CM · ATA 2150

1)ON CLIMBOUT CREW NOTED CABIN PRESSURIZATION NOT HOLDING CORRECT CABIN ALTITUDE. 2)CREW RETURNED TO HOME BASE. 3)MAINTENANCE TROUBLESHOT AND FOUND THE AIR CYCLE MACHINE DUCT COUPLER COMING LOOSE. 4) RESECURED DUCT COUPLER, OPS CHECK GOOD.

Source: SDR DBCA201903110001 · FAA SDRS
J · 2018-10-14 Matched by certificate designator
N793CG · ATA 7321

1) DURING CLIMB PILOT NOTED NR 1 DEEC CAS MESSAGE. 2) PILOT RETURNED TO HOMEBASE. 3) MAINTENANCE INSPECTED AND REPLACED NR 1 FUEL CONTROL 4) AIRCRAFT RETURNED TO SERVICE.

Source: SDR DBCA2018101800006 · FAA SDRS
O · 2018-08-31 Matched by certificate designator
N92ND · ATA 2150

DURING LIVE LEG PILOT NOTED AIR CONDITIONING WASN'T WORKING. LANDING IN CZBM WAS UNEVENTFUL. TECHNICIANS TROUBLESHOT TO BAD CURRENT LIMITER AND VCCS MOTOR. REMOVED AND REPLACED MOTOR. OPERATIONS CHECKS GOOD. AIRCRAFT RETURNED TO SERVICE.

Source: SDR DBCA2018090400054 · FAA SDRS
O · 2018-07-11 Matched by certificate designator
N339SM · ATA 7810

ON POST FLIGHT AFTER FIRST LEG OF TRIP CREW NOTED A SECTION OF RIGHT ENGINE EXHAUST FLUME DAMAGED. CONTACTED OFFSITE MAINTENANCE FOR SUPPORT. CONTACTED ENGINE MANUFACTURER FOR REPAIR SCHEME. DRESSED OUT DAMAGE IN ACCORDANCE WITH SERVICE LETTER SL44-72-481.

Source: SDR DBCA2018071300004 · FAA SDRS
O · 2018-06-22 Matched by certificate designator
N210CM · ATA 3423

DURING DEPARTURE TAXI, CREW NOTICED THE COPILOT PFD BUTTON STUCK IN TEST MODE. CREW RETURNED TO BLOCKS. MAINTENANCE CLEANED THE SELECTOR SWITCH. OPS CHECKED GOOD.

Source: SDR DBCA2018062920003 · FAA SDRS
F J · 2018-06-04 Matched by certificate designator
N504W · ATA 2720

CREW CALLED SAYING THEY HAVE A COMPUTER ISSUE WITH RUDDER DEFLECTION NOTIFICATION ON GROUND DURING PREFLIGHT INSPECTION. DETERMINED THE POSITION TRANSMITTER FLEXIBLE COUPLER WAS UNSERVICEABLE. REPLACED THE FLEXIBLE COUPLER WITH NEW. OPS CHECKED GOOD.

Source: SDR DBCA2018060640002 · FAA SDRS
O · 2018-02-02 Matched by certificate designator
N265CM · ATA 3231

DURING INSPECTION, NOTED THE NOSE GEAR DOORS WAS SAGGING. FURTHER INSPECTION FOUND TORQUE TUBE WELD ASSY BROKEN AT THE WELD. REPLACED TORQUE TUBE WITH NEW.

Source: SDR DBCA2018020200001 · FAA SDRS
J · 2017-11-04 Matched by certificate designator
N265CM · ATA 2130

DURING TAKEOFF ROLL, CREW NOTED UNCOMMANDED HOT AIR COMING INTO CABIN AND FLUCTUATIONS IN CABIN PRESSURIZATION RATE. RETURNED TO BASE, LANDING WAS UNEVENTFUL. TROUBLESHOT AND FOUND EMERGENCY PRESSURE VALVE INTERMITTENT. REPLACED THE VALVE WITH AN OVERHAULED UNIT. OPS CHECKED GOOD.

Source: SDR DBCA2017110400004 · FAA SDRS
B · 2017-11-02 Matched by certificate designator
N265CM · ATA 2120

AFTER TAKEOFF, CREW NOTED UNCOMMANDED HOT AIR COMING INTO CABIN AND FLUCTUATIONS IN CABIN PRESSURIZATION RATE. RETURNED TO BASE, LANDING WAS UNEVENTFUL. COULD NOT DUPLICATE. AIRCRAFT RETURNED TO SERVICE. NO DISCREPANCIES ON RETURN FLIGHT.

Source: SDR DBCA201711060001 · FAA SDRS
O · 2017-09-12 Matched by certificate designator
N420KM · ATA 2312

PRIOR TO DEPARTURE, PILOT NOTED ONE RADIO NOT WORKING. REMOVED AND REPLACED THE NR 1 VHF COM MODULE. OPS CHECKED GOOD.

Source: SDR DBCA2017091200002 · FAA SDRS
J · 2017-06-23 Matched by certificate designator
N250CM · ATA 2710

NO TAKEOFF CAS MESSAGE - ROLL SYSTEM CAS IN NO TAKEOFF PAGE NOTED WHILE TAXIING. CREW RETURNED TO HOME BASE. REMOVED AND REPLACED AILERON RATIO ACTUATOR PROXIMITY SWITCH. OPERATIONS CHECKED GOOD.

Source: SDR DBCA2017062300001 · FAA SDRS
N · 2016-11-26 Matched by certificate designator
N209CM · ATA 3610

5 MINUTES AFTER TAKEOFF RIGHT SIDE BLEED AIR ANNUNCIATOR CAME ON DURING FLIGHT. CREW RETURNED TO DEPARTURE. LANDING WAS UNEVENTFUL. TROUBLESHOT AND FOUND BLEED AIR PRESSURE SWITCH FAILED. REPLACED THE SWITCH, OPS CHECKED GOOD.

Source: SDR DBCA2016112600007 · FAA SDRS
J · 2016-11-19 Matched by certificate designator
N363NH · ATA 2612

10 MINUTES INTO FLIGHT, THE LEFT ENGINE LOWER SQUIB LIGHT ILLUMINATED. CREW RETURNED TO DEPARTURE. LANDING WAS UNEVENTFUL. MAINTENANCE FOUND LEFT AFT FIRE LOOP HAD FAILED AND REPLACED THE FIRE LOOP. OPS CHECKED GOOD.

Source: SDR DBCA201611190006 · FAA SDRS
K · 2016-08-02 Matched by certificate designator
N99BC · ATA 2820

THE AIRCRAFT ARRIVED FOR UNRELATED MAINTENANCE WHEN IT WAS NOTED THAT A LARGE AMOUNT OF FUEL WAS EMANATING FROM THE BELLY AREA BETWEEN THE WHEEL WELLS. ACCESS WAS GAINED TO THE AREA BETWEEN THE WHEEL WELLS CONTAINING THE MAIN FUEL SHUTOFF VALVES. WITH BOOST PUMPS ON, FUEL WAS OBSERVED TO COME FROM THE LEFT SHUTOFF VALVE. IT WAS INITIALLY THOUGHT THE O-RING BETWEEN THE MATING SURFACES OF THE ADAPTER AND SHUTOFF VALVE HAD FAILED. UPON DISASSEMBLY FOR REPLACEMENT OF THE SUSPECTED O-RING, IT WAS FOUND THAT THE ADAPTER, MADE FROM PLASTIC, FROM THE SHUTOFF VALVE TO THE HARD FLUID LINE TO THE ENGINE HAD A CRACK APPROXIMATELY 90 DEGREES OF CIRCUMFERENCE BETWEEN THE VALVE MATING FLANGE AND PIPE FLANGE. NEW REPLACEMENTS WERE ORDERED AND INSTALLED FOR BOTH LEFT AND RIGHT SHUTOFF VALVES. THE REAR EQUIPMENT COMPARTMENT WAS CLEANED AND DRIED OF A LARGE AMOUNT OF FUEL. THE REPLACEMENTS ARE ALSO CONSTRUCTED FROM PLASTIC. IT IS THE OPINION OF THE SUBMITTER THAT A PART THIS CRITICAL IN NATURE BE CONSTRUCTED FROM A MORE SUBSTANTIAL MATERIAL TO PREVENT UNCONTROLLED LOSS OF FUEL WHILE FILLING A COMPARTMENT CONTAINING ELECTRICAL MOTORS AND EQUIPMENT WITH FUEL.

Source: SDR 2016FA0000386 · FAA SDRS
J · 2016-07-10 Matched by certificate designator
N793KK · ATA 3420

WHILE ENROUTE, CREW NOTED MAU1 FAIL. CREW DIVERTED, CONTACTED MAINTENANCE FOR SUPPORT, REPLACED NR1 DUAL NIC PROCESSOR. OPS CHECK GOOD.

Source: SDR DBCA2016071000005 · FAA SDRS
J · 2016-07-10 Matched by certificate designator
N314CM · ATA 2430

RIGHT GENERATOR SPIKED TO 450 AMPS. CREW RAN CHECKLIST, SWITCHED TO OFF, AMPS DECREASED TO 25 ON RT AND 185 ON LT. AFTER SHUTDOWN WITH ONLY BATTERY ON, RT AMPS INDICATED 120+. RETURNED TO DEPARTURE FOR MAINTENANCE. REPLACED THE CURRENT SENSOR. OPS CHECKED GOOD.

Source: SDR DBCA2016071400004 · FAA SDRS
K J · 2016-06-02 Matched by certificate designator
N363NH · ATA 2910

ON APPROACH, CREW EXPERIENCED HYDRAULIC QTY LOW LIGHT FOLLOWED BY HYDRAULIC PRESSURE AND BOTH HYDRAULIC PUMP LIGHTS INTERMITTENTLY ON LANDING. CREW ALSO NOTED INTERMITTENT BRAKING AND NOSE STEERING DIFFICULTIES. MAINTENANCE SUSPECTS SPEED BRAKE LINE IS LEAKING, CONTINUING TO TROUBLESHOOT. MAINTENANCE VERIFIED RT SPEED BRAKE HYDRAULIC PRESSURE LINE HAD FAILED. REPLACED FAILED LINE AND BLEED HYDRAULIC SYSTEMS. OPS AND LEAK CHECK GOOD.

Source: SDR DBCA2016060200003 · FAA SDRS
N · 2016-05-14 Matched by certificate designator
N333PC · ATA 3150

ON TAXI OUT WHILE COMPLYING WITH RUDDER BIAS CHECK WITH THE ENGS AT POWER, CREW RECEIVED MASTER WARNING HORN. CREW RETURNED THROTTLES TO IDLE, NO CHANGE. CREW PULLED BREAKER & MASTER WARNING HORN STOPPED. CREW RETURNED FOR MX. MX POWERED ACFT NORMALLY & FOUND MASTER WARNING HORN DID NOT SOUND. ALL SYSTEMS OPERATING NORMALLY. ACFT RETURNED TO SERVICE.

Source: SDR DBCA2016051400002 · FAA SDRS
N · 2016-03-06 Matched by certificate designator
N101FC · ATA 2697

AFTER TAKEOFF, THE CREW RECEIVED AN APU FIRE WARNING. CREW DISCHARGED APU FIRE BOTTLE & RETURNED. FIRE WARNING DIDN'T CANCEL WHEN FIRE BOTTLE WAS DISCHARGED, SO CREW DECLARED AN EMER & EVACUATED ACFT ON THE RUNWAY. INSPECTION REVEALED NO EVIDENCE OF FIRE IN APU AREA. ACFT REPOSITIONED FOR INVESTIGATION OF FALSE FIRE WARNING. FOUND WIRE SHORTED AT APU LOWER FWD OVERTEMP SWITCH. REPAIRED WIRE. OPERATIONS CHECKED GOOD.

Source: SDR DBCA2016030600001 · FAA SDRS
E · 2015-12-28 Matched by certificate designator
N301ML · ATA 7230

ENROUTE CREW NOTED A VIBRATION FROM LT ENG. CREW DIVERTED & LANDING WAS UNEVENTFUL. CONTACTED MFG FOR SUPPORT. MFG COMPLETED VIBRATION SURVEY & DETERMINED LT ENG FAN REQUIRED BALANCING. REMOVED FAN BLADES, LUBED DOVETAILS & REINSTALLED. BALANCED FAN. OPERATIONS CHECKED GOOD.

Source: SDR DBCA201512280008 · FAA SDRS
N · 2015-07-07 Matched by certificate designator
N69VH · ATA 3260

ON APPROACH, THE CREW DID NOT HAVE A LT MAIN DOWN & LOCK INDICATION. DECLARED AN EMER, LANDING WAS UNEVENTFUL. FOUND INDICATOR LAMP HAD FAILED. REPLACED BULB, OPERATIONS CHECKED GOOD.

Source: SDR DBCA201507070007 · FAA SDRS
O · 2015-06-12 Matched by certificate designator
N504WV · ATA 5210

ON DEPARTURE, CREW NOTED LOUD SQUEAL FROM CABIN DOOR AREA. CREW RETURNED & LANDING WAS UNEVENTFUL. INSPECTED AREA & FOUND DOOR SEAL FAILED. DOOR SEAL WAS REPLACED. FUNCTIONAL CHECKED GOOD.

Source: SDR DBCA201506120006 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N196AHPILATUS AIRCRAFT LTD PC-242020Valid RegistrationMatched by certificate designator
N210CMCESSNA 5601996Valid RegistrationMatched by certificate designator
N255VGTEXTRON AVIATION INC 680A2016Valid RegistrationMatched by certificate designator
N265CMCESSNA 5601999Valid RegistrationMatched by certificate designator
N279AHPILATUS AIRCRAFT LTD PC-242021Valid RegistrationMatched by certificate designator
N301MLHAWKER BEECHCRAFT CORP HAWKER 900XP2008Valid RegistrationMatched by certificate designator
N317MLDASSAULT FALCON 900 EX2005Valid RegistrationMatched by certificate designator
N339SMMatched by certificate designator
N716SCESSNA 5601998Valid RegistrationMatched by certificate designator
N717JJBOMBARDIER INC BD-100-1A102007Valid RegistrationMatched by certificate designator
N728QLCESSNA 7502008Valid RegistrationMatched by certificate designator
N747RXMatched by certificate designator
N751MTRAYTHEON AIRCRAFT COMPANY HAWKER 850XP2005Valid RegistrationMatched by certificate designator
N782BJMatched by certificate designator
N847RCGULFSTREAM AEROSPACE GIV-X (G450)2011Valid RegistrationMatched by certificate designator
N900LCDASSAULT AVIATION MYSTERE FALCON 9002000Valid RegistrationMatched by certificate designator
N900WTRAYTHEON AIRCRAFT COMPANY HAWKER 850XP2006Valid RegistrationMatched by certificate designator
N950MJMatched by certificate designator
N955PMMatched by certificate designator