N279AH

PILATUS AIRCRAFT LTD PC-24 · 2021 · Valid Registration

Registered owner: CHARLOTTE-MECKLENBURG HOSPITAL AUTHORITY DBA, NC (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
STERLING AVIATION, LLC (DBCA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2024-08-31 Matched by certificate designator
ATA 3010

1) CREW RECEIVED AMBER WING ANTI-ICE FAIL AND AMBER WING ANTI-ICE VALVE CLOSED MESSAGES DURING OPERATION IN ICING CONDITIONS 2) CREW RETURNED TO HOME BASE 3) MTN TROUBLESHOT RH ANTI-ICE VALVE 4) MTN DEFERRED PER MEL 30-10-01 5) MTN REMOVED LH & RH WING ANTI-ICE VALVES AND REPLACED WITH UPDATED, REPAIRED UNITS 6) OPS CHECKS GOOD.

Source: SDR DBCA2024090410005 · FAA SDRS
J · 2024-01-08 Matched by certificate designator
ATA 7930

1) DURING DESCENT ON FLIGHT TO ELM CREW RECEIVED RH ENG HIGH OIL NOTICE. 2) CREW PERFORMED ENG INFLIGHT SHUTDOWN ON RH ENGINE. 3) CREW DECLARED AN EMERGENCY AND LANDED AT ELM. 4) MTN COMPLIED WITH FHDB AND WI DOWNLOADS. 5) MTN REMOVED AND REPLACED RH OIL PRESSURE TRANSDUCER W/ NEW. LEAK CHECK GOOD.

Source: SDR DBCA2024010800001 · FAA SDRS
B · 2022-11-06 Matched by certificate designator
ATA 2140

1) CREW NOTED SMOKE IN COCKPIT/CABIN AFTER TAKE OFF. 2) CREW DECLARED AN EMERGENCY AND RETURNED TO SAT. 3) MTN FOUND RH FWD CABIN ELECTRIC HEATER/FAN PCB BURNED. 4) MTN REPLACED RH FWD CABIN ELECTRIC HEATER ASSY WITH NEW.

Source: SDR DBCA2022AA060007 · FAA SDRS
J M · 2022-07-13 Matched by certificate designator
ATA 7200

MANUFACTURER INDICATES A FAILED BRAZE WELD ON THE #1 LPT NOZZLE GUIDE VANE WHICH ALLOWED THE NOZZLE TO FLEX AND CONTACT THE #1 LPT DISK. THIS DAMAGED THE DISK SENDING DEBRIS THROUGH THE REST OF THE TURBINE SECTION CAUSING DAMAGE THROUGHOUT. ENGINEERING IS INVESTIGATING IF THE FAILED WELD WAS THE ROOT CAUSE OR THE RESULT OF SOME OTHER FAILURE, POSSIBLY VIBRATION FROM A BEARING. AFTER REPAIR OF ENGINE NOTED FAILED PART WAS A NOZZLE/HEATSHIELD ASSY.

Source: SDR DBCA202207130006 · FAA SDRS
J · 2022-05-12 Matched by certificate designator
ATA 3230

1) ON APPROACH WITH GEAR DOWN CREW NOTED "GEAR" ON MFD AND LH GEAR ANNUN FLICKER TO WHITE UNSAFE POSITION FOR A SECOND. IN THE FLARE AFTER RETARDING POWER HEARD AN AUDIBLE GEAR WARNING 2) MTN CHECKS SHOWED NO DEFECTS ON GROUND. 3) MTN PERFORMED CHECKS ON DOWN AND LOCK MICROSWITCHES FOR RIGGING. FOUND LH MLG SWITCH OUT OF RIG. ADJUSTED SWITCH. 4) COMPLIED WITH GEAR SWINGS WITH NO DEFECTS NOTED.

Source: SDR DBCA202205120003 · FAA SDRS
K · 2022-01-05 Matched by certificate designator
ATA 2810

1) IN FLIGHT CREW NOTED 200 LB IMBALANCE, OBSERVED FUEL LEAKING FROM LH WINGTIP AREA 2)CREW DIVERTED TO BHM 3)LANDING WAS UNEVENTFUL 4) STERLING MTN WITH PILATUS TECH SUPPORT DETERMINED THE ISSUE WAS CAUSED BY EXCESSIVE PRESSURE DURING FUELING CAUSING FUEL TO BE FORCED INTO THE CLIMB VENT LINE. ONCE AIRBORNE DIFFERENTIAL PRESSURE CAUSED THIS FUEL TO BE SIPHONED OUT UNTIL FUEL LEVEL DROPPED BELOW LEVEL OF VENT OUTLET DURING DESCENT. 5)LEAK CHECK OF SYSTEM REVEALED NO CURRENT LEAKS 6)AIRCRAFT RELEASED TO CLT

Source: SDR DBCA20220105001 · FAA SDRS