N285TW

DASSAULT/SUD FAN JET FALCON SER E · Valid Registration

Registered owner: SIERRA AMERICAN CORPORATION, DE (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AMERISTAR JET CHARTER, INC. (HAEA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2023-11-08 Matched by certificate designator
ATA 3100

ON DECENT IN TO ELP THE LANDING GEAR WAS EXTENDED, THE RH M/L/G DOWN AND LOCKED GREEN LIGHT DID NOT ILLUMINATE. THE ALTERNATE LANDING GEAR EXTENSION SYSTEM WAS USED WITH THE GREEN LIGHT STILL WAS NOT ILLUMINATED. THE CREW DECLARED AN EMERGENCY AND FLEW BY THE TOWER FOR A VISUAL CHECK OF THE GEAR, ATC REPORTED ALL THREE LANDING GEAR WERE DOWN. A NORMAL LANDING WAS COMPLETED.

Source: SDR 2023FA0000749 · FAA SDRS
X · 2023-09-11 Matched by certificate designator
ATA 7200

AIRCRAFT DEPARTED LYH-SHV, AT CRUISE ALTITUDE OF FL280 THE LEFT ENGINE EXPERENCED A LOSS OF POWER/FLAMEOUT, THE CREW DECENDED TO FL240 AND PERFORMED A SUCCESSFUL AIR START. AFTER LANDING IN SHV THE ENGINE WAS INSPECTED BY AMERISTAR MAINT AND THEY FOUND FOD DAMAGE TO THE 1ST STAGE COMPRESSOR BLADES AND THE FAN BLADES.

Source: SDR HAEA202309120274 · FAA SDRS
J · 2019-03-05 Matched by certificate designator
ATA 3230

ON APPROACH IN TO KYIP THE LANDING GEAR WAS SELECTED DOWN WITH ONLY 3 RED LIGHTS ILLUMINATED, PILOT REPORTED IT DID NOT SOUND LIKE THE GEAR HAD EXTENDED AND CONTACTED TOWER TO DO A FLYBY AND WAS TOLD THEY DID NOT SEE THE GEAR EXTENDED. LANDING GEAR EMER EXTENSION PROCEDURE 'A' WAS PERFORMED PER THE AFM WITH THE GEAR EXTENDED AND ALL INDICATIONS NORMAL. AIRCRAFT LANDED WITHOUT INCIDENT.

Source: SDR HAEA20190305002 · FAA SDRS
J · 2010-10-27 Matched by certificate designator
ATA 2750

TOOK OFF FROM RUNWAY 30, TAKEOFF NORMAL AT 400 FT, V2 + 20 SELECTED FLAPS ZERO. FLAPS STAYED AT 15 DEGREES. CLIMBED TO 4000 FT MSL. ATTEMPTED TO IDENTIFY PROBLEM AND FOUND FLAPS WOULD NOT EXTEND PAST 15 DEGREES. CONTACT TOWER AND ASKED FOR LONGEST RUNWAY. TOWER DECLARED EMERGENCY UNREQUESTED BY FLT CREW. LANDED WITHOUT INCIDENT. MAINTENANCE DISCOVERED INTERMITTENT FAILURE OF THE FLAP DRIVE MOTOR. FLAP DRIVE MOTOR/GEAR REDUCTION UNIT REPLACED IAW MM 27. OPERATIONS CHECK GOOD. AIRCRAFT RETURNED TO SERVICE.

Source: SDR HAEA201000217 · FAA SDRS
J · 2009-01-30 Matched by certificate designator
ATA 3260

CLIMBOUT GTR GEAR UNSAFE LIGHT UPON GEAR RETRACTION. CREW PERFORMED PROCEDURES PER MANUAL. LANDING UNEVENTFUL IN GTR. AIRCRAFT MOVED TO ADS UNDER FAA SPECIAL FLIGHT PERMIT FOR REPAIR. MAINTENANCE FOUND FAULTY SWITCH IN NOSE GEAR UP LOCK. REPLACED FAULTY SWITCH IN UP LOCK ASSY. NO FURTHER ACTION REQUIRED.

Source: SDR HAEA200900207 · FAA SDRS
O · 2007-07-17 Matched by certificate designator
ATA 5341

DURING TANK AND PLANK INSPECTION THE LT AND RT WING TO FUSELAGE ATTACH FITTINGS WERE DISCOVERED TO HAVE MINOR CORROSION ON THE LOWER OB SURFACE. THE WINGS WERE DEMATED TO INSURE THAT CORROSION HAD NOT MIGRATED TO BETWEEN THE WING TO FUSELAGE ATTACH FITTINGS. CORROSION WAS EVALUATED BY ENGINEERING AND AN ENGINEERING INSTRUCTION WAS ISSUED. CORROSION WAS WORKED IAW THE ENGINEERING INSTRUCTION. NO FURTHER ACTION REQUIRED. [CLOSED]

Source: SDR HAEA002002007 · FAA SDRS
W · 2005-12-09 Matched by certificate designator
ATA 5230

DEPARTED RWY, CLIMBING TO 9500 FT CARGO DOOR OPENED. CREW DECLARED AN EMERGENCY & RETURNED, LANDING NORMAL. INSPECTION FOUND CARGO DOOR SUSTAINED DAMAGED DURING EVENT ABOVE. ACFT FERRIED TO MX FOR REPAIRS. MX REPAIRED DAMAGE TO DOOR CAP & SURROUNDING SKIN IAW DER INSTRUCTIONS. OPS/RIGGING CHECK OF DOOR LOCK MECHANISHM REVEALED NO DESCREPANCIES. FOUND CHANNEL CRACKED & REPAIRED. AFTER REPAIR PERFORMED GROUND PRESSURIZATION CHK & FOUND SAT. A REVIEW OF EVENTS PRIOR TO DOOR OPENING REVEALED CHANNEL CRACK COULD HAVE BEEN PRE-EXISTING ALLOWING DOOR TO FLEX UNDER CABIN PRESSURE ENOUGH TO DISENGAGE FROM FORWARD LOCK & DISENGAGE ALL LOCKS. ACFT RTS. [CLOSED]

Source: SDR HAEA200500186 · FAA SDRS
N · 2004-08-04 Matched by certificate designator
ATA 3260

AIRCRAFT DIVERTED. PILOTS REPORTED THAT THE GEAR WOULD RETRACT BUT THE GEAR DOORS WOULD NOT CLOSE. MAINTENANCE FOUND RT GEAR UPLOCK SWITCH BAD. REPLACED SWITCH, OPS CHECK GOOD. <CLOSED>.

Source: SDR HAEA200400161 · FAA SDRS
J · 2004-07-03 Matched by certificate designator
ATA 2130

AIRCRAFT DEPARTED ADS CLIMBING THROUGH 10,000 FT CABIN DID NOT PRESSURIZE. ALL SWITCHES CHECKED NORMAL. AIRCRAFT RETURNED TO ADS FOR MAINTENANCE. LANDING NORMAL.

Source: SDR HAEA153 · FAA SDRS
J · 2004-06-15 Matched by certificate designator
ATA 7261

ON DESCENT INTO CHS, AIRCRAFT LOST OIL PRESSURE IN NR 1 ENGINE. CREW INITIATED ENGINE SHUTDOWN PROCEDURES. DECLARED EMERGENCY, LANDED AT CHS UNEVENTFUL.

Source: SDR HAEA00147 · FAA SDRS
N · 2004-05-07 Matched by certificate designator
ATA 5270

PILOT REPORTED MAIN CARGO DOOR LIGHT CAME ON AND CABIN PRESS DUMPED, RETURNED TO DEPARTURE AIRPORT FOR MAINTENANCE. MAINTENANCE ADJUSTED SWITCH AND OPS CHECKED AIRCRAFT AND SYSTEM, RETURNED AIRCRAFT TO SERVICE. (CLOSED)

Source: SDR 00138 · FAA SDRS
J · 2003-09-22 Matched by certificate designator
ATA 5210

PILOT REPORTED SEMI- RAPID DECOMPRESSION AT FL290 SIMULTANEOUSLY WITH DOOR LIGHT, AFTER RAPID DESCENT WAS INITIATED TO 10,000FT, AFTER APPROX 7 OR 8 MINUTES THE CABIN BEGAN PRESSURIZING. AIRCRAFT WAS DIVERTED TO ADS FOR MAINTENANCE. WILL UPDATE REPORT AFTER MAINTENANCE. RIGGED DOOR LATCH AND SWITCHES ON CARGO DOOR IAW AVDOOR MANUAL.

Source: SDR HAEA00114 · FAA SDRS
J · 2003-09-09 Matched by certificate designator
ATA 2130

PILOT REPORTED CABIN ALTITUDE INDICATING HIGH, CYCLED PRESSURIZATION VALVES, RETURNED TO DEPARTURE AIRPORT FOR MAINTENANCE, REPAIRED BROKEN PRESSURIZATION LINE IAW / FALCON MM. RETURN AIRCRAFT TO SERVICE.

Source: SDR 00110 · FAA SDRS
B · 2003-03-26 Matched by certificate designator
ATA 3310

PILOT REPORTED DURING CLIMB AT FL290 ELECTRICAL SMOKE IN COCKPIT REQUESTED RETURN TO DEPARTURE AIRPORT ADS, ISOLATED NR 1 ELECTRICAL SYSTEM AND SMOKE DECREASED, REMAINDER OF FLIGHT UNEVENTFUL. WILL UPDATE THIS REPORT AFTER MAINTENANCE. REMOVED AND REPLACED FAILURE WARNING PANEL. OPS CHECK GOOD.

Source: SDR 00086 · FAA SDRS
N · 2003-02-05 Matched by certificate designator
ATA 7930

PILOT REPORTED OIL TEMP INDICATION ON LT ENGINE HIGHER THAN NORMAL, PILOT RETURNED TO DEPARTURE AIRPORT. MAINTENANCE REMOVED AND CLEANED OIL TEMP CONNECTOR PLUG RESEATED AND OPS CHECKED NORMAL.

Source: SDR 00077 · FAA SDRS
B · 2003-02-02 Matched by certificate designator
ATA 7500

PILOT REPORTED ODOR OF BURNING WIRES , RETURN TO DEPARTURE AIRPORT. MAINTENANCE FOUND LOOSE BLEED AIR LINE BEHIND CO-PILOT RADIO RACK, GROUND RUN CHECK GOOD.

Source: SDR 00076 · FAA SDRS
P · 2002-10-28 Matched by certificate designator
ATA 3422

AIRCRAFT DEPARTED AND PILOT DIRECTIONAL GYRO STOPPED MOVING, AIRCRAFT DIVERTED FOR MAINTENANCE, REMOVED AND REPLACED LEFT DIRECTIONAL GYRO, AIRCRAFT RETURN TO SERVICE.

Source: SDR 00056 · FAA SDRS
O · 2002-06-28 Matched by certificate designator
ATA 3260

AIRCRAFT CLIMBING OUT OF LIT EN ROUTE TO DET AIRCRAFT STARTED TO DEPRESSURIZE, LEVELED OFF STILL WOULD NOT HOLD CABIN. DIVERTED TO MEM. REMOVED AND REPLACED RT SQUAT SWITCH AND ALTITUDE CONTROLLER, GROUND CK GOOD. RETURNED AIRCRAFT TO SERVICE.

Source: SDR 00032 · FAA SDRS