N288SW

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

Accident · 2001-02-25 Unresolved
Embraer EMB-120 Serious injuryoperator not yet resolved
Source: NTSB case LAX01LA105

Maintenance disclosures

J · 2012-03-16 Matched by certificate designator
ATA 7261

EXPERIENCED AN IN-FLIGHT SHUTDOWN OF THE LT ENGINE DUE TO LOW OIL PRESSURE. SHUTDOWN ENGINE & LANDED. ENGINE NEEDED 8 QUARTS OF OIL TO REFILL RESERVOIR.

Source: SDR 3MNB20121212001 · FAA SDRS
J · 2011-06-16 Matched by certificate designator
ATA 3020

RIGHT ENGINE DUCT LEAK WARNING. FOLLOWED QRH WHICH LED TO RIGHT ENGINE SHUT DOWN. (FLT 1300) REPLACED RIGHT DEICE PRESSURE REGULATOR VALVE. P/N 38E96, S/N OFF RF-1805.

Source: SDR SWIA201126579 · FAA SDRS
O · 2011-04-13 Matched by certificate designator
ATA 3350

THE 1ST OVERHEAD EMERGENCY LIGHT IS OUT. (FLT 6493) REPLACED FUSE IN OVERHEAD PANEL BY ROW 1.

Source: SDR SWIA201126022 · FAA SDRS
O · 2011-02-16 Matched by certificate designator
ATA 5210

MAIN CABIN DOOR IS DIFFICULT TO OPEN. (FLT 6527) LUBRICATED DOOR HANDLES (IN & OUT) AND ADJUSTED AFT LOCK CAM.

Source: SDR SWIA201125610 · FAA SDRS
O · 2010-12-08 Matched by certificate designator
ATA 5711

RIGHT WING INBOARD INTERNAL DRY BAY CLOSEST TO NACELLE, SPAR IS CRACKED. (C-CHECK) REPAIRED RIGHT WING AUXILIARY SPAR INBOARD OF NACELLE PER ETD AND SRM.

Source: SDR SWIA201025854 · FAA SDRS
O · 2010-12-07 Matched by certificate designator
ATA 5210

PASSENGER DOOR SKIN IS CORRODED. (C-CHECK) REPLACED PAX DOOR SKIN PER SRM.

Source: SDR SWIA201025684 · FAA SDRS
O · 2010-12-06 Matched by certificate designator
ATA 5711

LEFT WING INBOARD INTERNAL DRY BAY CLOSEST TO NACELLE HAS CRACKED SPAR CAP. (C-CHECK) REPAIRED LEFT WING AUXILIARY UPPER SPAR CAPPER ETD AND SRM.

Source: SDR SWIA201025853 · FAA SDRS
O · 2010-07-30 Matched by certificate designator
ATA 3350

FLOOR LEVEL EMERGENCY LIGHTS INOP. (FLT 6650) RELAMPED EMERGENCY LIGHT.

Source: SDR SWIA201024669 · FAA SDRS
O · 2010-07-16 Matched by certificate designator
ATA 3350

EMERGENCY LIGHTS ON THE 1ST OVERHEAD CEILING INOP. (FLT 6938) RELAMPED EMERGENCY LIGHTS.

Source: SDR SWIA201024577 · FAA SDRS
O · 2010-05-18 Matched by certificate designator
ATA 5753

RIGHT WING NACELLE FLAP CRACKED ON OUTBOARD SIDE. (C CHECK) REPAIRED PER SRM.

Source: SDR SWIA201024240 · FAA SDRS
O · 2010-05-08 Matched by certificate designator
ATA 3397

EMERGENCY OVERHEAD LIGHT AT 6A INOP. (FLT 6820) REPLACED WIRE TERMINAL.

Source: SDR SWIA201024188 · FAA SDRS
O · 2009-11-22 Matched by certificate designator
ATA 5753

NACELLE FLAP CRACKED. (C-CHECK) REPLACED FLAP PER AMM.

Source: SDR SWIA200923177 · FAA SDRS
O · 2009-07-13 Matched by certificate designator
ATA 3350

FLT 6263, CEILING EMERGENCY LIGHT INOP, ROW 7. RELAMPED.

Source: SDR SWIA200921998 · FAA SDRS
O · 2009-06-02 Matched by certificate designator
ATA 3350

WHITE FLOOR EMERGENCY LIGHT AT ROW 11 INOP. (FLT 6129) RESECURED BULB.

Source: SDR SWIA200921759 · FAA SDRS
O · 2009-05-20 Matched by certificate designator
ATA 3350

FLT 6006 - LOWER EXIT LIGHT ROW 6A BROKEN. REPLACED LIGHT ASSEMBLY.

Source: SDR SWIA200921667 · FAA SDRS
O · 2009-05-07 Matched by certificate designator
ATA 3350

FLT 6177 - FLOOR LEVEL FORWARD EMERGENCY LIGHT INOP. RELAMPED.

Source: SDR SWIA200921597 · FAA SDRS
O · 2009-03-25 Matched by certificate designator
ATA 5713

C-CHECK, RIGHT INBOARD WING STRINGER CRACKED. REPAIRED PER SRM.

Source: SDR SWIA200921849 · FAA SDRS
B · 2008-09-07 Matched by certificate designator
ATA 2120

RIGHT BLEED OVERHEAT WARNING LIGHTS CAME ON ALONG WITH A BURNING ODOR AND VISUAL SMOKE IN THE MAIN CABIN. PERFORM OPS CHECK OF RT ENG BLEED, COULDN'T DUPLICATE AT THIS TIME.

Source: SDR SWIA200820018 · FAA SDRS
O · 2008-07-17 Matched by certificate designator
ATA 3397

WITH EMERGENCY LIGHTS IN THE ARM POSITION, LIGHTS STAY ILLUMINATED. (FLIGHT NR 5728) REPLACED RELAY K0201. OPS CHECK GOOD.

Source: SDR SWIA200819872 · FAA SDRS
O · 2008-05-04 Matched by certificate designator
ATA 5753

LEFT NACELLE FLAP IS CRACKED. REPLACED LEFT NACELLE FLAP IAW EMB MM CH 27-50-03.

Source: SDR SWIA200819581 · FAA SDRS
L · 2008-03-15 Matched by certificate designator
ATA 3397

FLT 5561 - RED EMERGENCY LIGHTS ARE NOT WORKING. REPAIRED WIRING AT ENVIRONMENTAL SPLICE. OPS CHECK GOOD.

Source: SDR SWIA200819359 · FAA SDRS
O · 2007-11-15 Matched by certificate designator
ATA 5753

RIGHT INBOARD FLAP TRACK IS CRACKED. REPLACED FLAP TRACK WITH A SERVICEABLE UNIT IAW 57-53-02.

Source: SDR SWIA200718879 · FAA SDRS
O · 2007-09-07 Matched by certificate designator
ATA 3350

FLT 5720 - EXIT ROW EMERGENCY LIGHT ASSEMBLY IS BROKEN. REPLACED EXIT SIGN ASSEMBLY, P/N 10-1301-15.

Source: SDR SWIA200718659 · FAA SDRS
L · 2007-01-17 Matched by certificate designator
ATA 3350

EMERGENCY FLOOR LIGHT AT ROW 11A IS NOT WORKING. REPLACE LIGHT BULB ON FLOOR EMERGENCY LIGHT AT SEAT 11A. OPERATIONAL CHECKS GOOD.

Source: SDR SWIA200717682 · FAA SDRS
N · 2006-04-02 Matched by certificate designator
ATA 2611

SMOKE DET IN LAVATORY SOUNDS INTERMITTENTLY. REPLACED DETECTOR AND BATTERY. OPERATIONAL CHECK GOOD.

Source: SDR SWIA200616510 · FAA SDRS
O · 2006-04-01 Matched by certificate designator
ATA 3350

FLOOR LEVEL EXIT SIGN AT 6C IS MISSING. INSTALLED SERVICEABLE EMER EXIT PANEL AT SEAT 6C. OPERATIONAL CHECK GOOD.

Source: SDR SWIA200616509 · FAA SDRS
F · 2006-01-19 Matched by certificate designator
ATA 2216

WHILE IN A DESCENT, AC PITCHED UP AND STARTED CLIMBING. BOTH FLIGHT DIRECTORS PITCHED UP AND DESC BUTTON WOULD NOT STAY ILLUM. REPLACED ELEVATOR AUTOPILOT SERVO IAW MM 22-10-05. OPERATIONAL CHECK GOOD.

Source: SDR SWIA200616149 · FAA SDRS
J · 2005-09-11 Matched by certificate designator
ATA 3418

STALL WARNING SYSTEM 2 INOP. REPLACED STALL WARNING TEST PANEL. OPERATIONAL CHECK GOOD.

Source: SDR SWIA200515525 · FAA SDRS
L · 2005-07-15 Matched by certificate designator
ATA 3350

LAST EMERGENCY LIGHT IN BACK OF CABIN IS OUT. INSTALLED BULB INTO SOCKET OF EMERGENCY LIGHT IN THE BACK OF THE CABIN. OPS CHECKS GOOD.

Source: SDR SWIA200515312 · FAA SDRS
O · 2005-06-19 Matched by certificate designator
ATA 3350

ROW 10 FLOOR LEVEL EXIT ROW WHITE LIGHT OUT. REPLACED BULBS AT ROW 10 EMERGENCY LIGHTS. OPERATIONAL CHECK GOOD.

Source: SDR SWIA200515218 · FAA SDRS
J · 2005-03-23 Matched by certificate designator
ATA 2216

WHEN CAPTAIN'S STALL WARNING SYSTEM IS TESTED THE SHAKER DOES NOT ACTIVATE. REPLACED NR 1 STICK SHAKER SERVO. OPERATIONAL CHECK GOOD.

Source: SDR SWIA200514756 · FAA SDRS
O · 2005-01-26 Matched by certificate designator
ATA 3397

EMERGENCY LIGHTS BETWEEN ROW 2 & 5 INOPERATIVE. REPLACED BLOWN FUSE AND REPAIRED WIRES. OPERATIONAL CHECK GOOD.

Source: SDR SWIA200514507 · FAA SDRS
O · 2004-12-18 Matched by certificate designator
ATA 3350

EMERGENCY EXIT SIGN IN SEAT 6A BROKEN. REPAIRED EMERGENCY EXIT SIGN AT 6A. OPERATIONAL CHECK GOOD.

Source: SDR SWIA200414302 · FAA SDRS
J · 2004-09-16 Matched by certificate designator
ATA 3418

RIGHT STALL SHAKER INOPERATIVE. INSTALLED SERVICEABLE SERVO STICK SHAKER ON NR 2 SIDE. OPERATIONAL CHECK GOOD. P/N C-81802-2, S/N ON 408, S/N OFF 298.

Source: SDR SWIA200413830 · FAA SDRS
J · 2004-07-13 Matched by certificate designator
ATA 5230

LEVELING AT 22,000 CABIN PRESSURIZATION DUMPED. REPLACED CARGO DOOR SEAL AT 3 LOWER SEAL RETAINERS IAW EMB MM 52-30-01. LEAK CHECK GOOD.

Source: SDR SWIA200413572 · FAA SDRS
F · 2004-07-04 Matched by certificate designator
ATA 2215

RIGHT RUDDER PEDAL RUBBING AND GRINDING AND CATCHING ON SOMETHING DURING FLIGHT CONTROL CHECK. REMOVED AND REPLACED RUDDER AUTOPILOT SERVO AND SERVO CLUTCH IAW MM 22-10-05 AND 27-00-03. OPERATIONAL CHECK GOOD. P/N 622-5734-004, S/N OFF 7268.

Source: SDR SWIA200413535 · FAA SDRS
O · 2004-06-09 Matched by certificate designator
ATA 5411

RIGHT OUTBOARD NACELLE INTERNAL FRAME CRACKED. DISCOVERED AT C-CHECK INSPECTION. INSTALLED DOUBLER AT AFFECTED AREA IAW 120 SRM 51-10-02 P2 SEC 2B.

Source: SDR SWIA200413399 · FAA SDRS
O · 2004-05-15 Matched by certificate designator
ATA 5411

LEFT OUTBOARD NACELLE INTERNAL FRAME CRACKED. DISCOVERED AT C-CHECK INSPECTION. APPLIED DOUBLER TO LEFT OUTBOARD NACELLE FRAME IAW SRM 120 51-10-02 PG 2 SEC 2B.

Source: SDR SWIA200413402 · FAA SDRS
O · 2004-05-15 Matched by certificate designator
ATA 5411

LEFT INBOARD NACELLE INTERNAL FRAME CRACKED. DISCOVERED AT C-CHECK INSPECTION. INSTALLED DOUBLER AT AFFECTED AREA IAW EMB120 SRM 51-10-02 PG 2 SEC 2B.

Source: SDR SWIA200413403 · FAA SDRS
O · 2004-05-15 Matched by certificate designator
ATA 5411

RIGHT INBOARD NACELLE INTERNAL FRAME CRACKED. DISCOVERED AT C-CHECK INSPECTION. APPLIED DOUBLER TO RIGHT INBOARD NACELLE FRAME IAW SRM 120 51-10-02 PG 2 SEC 2B.

Source: SDR SWIA200413401 · FAA SDRS
O · 2004-05-15 Matched by certificate designator
ATA 5420

RIGHT HYDRAULIC RESERVOIR LOWER SUPPORT CHANNEL CRACKED. DISCOVERED AT C-CHECK. REPLACED RIGHT HYDRAULIC RESERVOIR LOW SUPPORT CHANNEL IAW SRM 120 51-10-02 PG 3 SEC 3A.

Source: SDR SWIA200413404 · FAA SDRS
O · 2004-05-15 Matched by certificate designator
ATA 5411

RIGHT ENGINE FRAME NR 1 IS CRACKED ON OUTBOARD SIDE. DISCOVERED AT C-CHECK. INSTALLED NEW RIGHT ENGINE FRAME NR 1 IAW SB 120-54-0036 AND RII CARD RII54-301.

Source: SDR SWIA200413405 · FAA SDRS
F · 2003-11-09 Matched by certificate designator
ATA 2210

CA'S AP DOES NOT HOLD ALTITUDE. REMOVED AND REPLACED NR 1 APC-65B. OPS CHECK GOOD IAW MM 22-11-00. P/N: 622-8317-402, S/N OFF: 4147.

Source: SDR SWIA200312602 · FAA SDRS
J · 2003-10-31 Matched by certificate designator
ATA 2750

AFTER LANDING, BOTH NACELLE FLAPS WERE SLOW TO RETRACT, CAUSING DISAGREEMENT. NACELLE FLAPS EVENTUALLY RETRACTED ON THEIR OWN. REMOVED AND REPLACED LT NACELLE FLAP ACTUATOR WITH SERVICEABLE UNIT IAW MM 27-50-00. OPS CHECKS GOOD. PN: 343100-1001, SN ON: 0228, SN OFF: 0175

Source: SDR SWIA200312571 · FAA SDRS
F · 2003-10-06 Matched by certificate designator
ATA 2210

CAPTAIN'S AUTOPILOT AND TRIM FAIL. REPLACED CAPTAIN'S AUTO PILOT COMPUTER. OPS CHECK GOOD.

Source: SDR SWIA200312496 · FAA SDRS
L · 2003-09-25 Matched by certificate designator
ATA 3418

NR 2 STALL SHAKER INOPERATIVE. REPLACED NR 2 STALL SHAKER. SYSTEM TESTS NORMALLY IAW MM 27-34-00.

Source: SDR SWIA200312459 · FAA SDRS
F · 2003-09-14 Matched by certificate designator
ATA 2211

ALTITUDE HOLD ON CAPT SIDE WILL DRIFT 150' DOWN. REPLACED AUTO PILOT COMPUTER APC-65B. OPS CHECK GOOD IAW MM 22-10-00.

Source: SDR SWIA200312406 · FAA SDRS
B · 2003-06-14 Matched by certificate designator
ATA 2121

SMOKE IN CABIN AND ASSOCIATED RIGHT PACK FAIL. REPLACED RIGHT PACK GROUND COOLING FAN. OPS CHECKED NORMAL.

Source: SDR SWIA200312109 · FAA SDRS
K J · 2002-12-15 Matched by certificate designator
ATA 2752

ON TAXI OUT, AFTER SELECTING FLAPS 15 DEGREES, THE HYDRAULIC QUANTITY ON THE BLUE SIDE WENT TO ZERO WITH ASSOCIATED LIGHTS. REMOVED AND REPLACED LEFT NACELLE FLAP ACTUATOR IAW RII 27-307 AND 27-50-08. LEAK CHECKS GOOD. NO LEAKS NOTED AT THIS TIME.

Source: SDR SWIA200211577 · FAA SDRS
B · 2002-10-10 Matched by certificate designator
ATA 2121

RIGHT GROUND COOLING FAN STOPS INTERMITTENTLY AND CAUSES SMOKE IN CABIN. REPLACED RIGHT GROUND COOLING FAN. OPS CHECK GOOD.

Source: SDR SWIA200211329 · FAA SDRS
B J · 2002-09-20 Matched by certificate designator
ATA 2150

F/A SMELLED SMOKE IN CABIN AFTER PAX DEPLANED IN MFR. CABIN HAD FILLED WITH SMOKE. LAV SMOKE DETECTOR ACTIVATED. CALLED FIRE DEPT. INVESTIGATED CABIN FOR SMOKE. RAN APU ON BOTH PACKS AT SEPARATE TIMES. INSPECTED EXTERIOR OF PACK UNITS. OIL NOTED ON RT PACK. RAN RT ENGINE WITH RT PACK. DETERMINED POSSIBLE CAUSE TO BE OIL IN RT BLEED & RT PACK. INSPECTED RT ENGINE BLEED DUCT AFT OF FIRE SEAL FOR OIL ON INSIDE. NONE NOTED. RAN RT PACK WITH RT ENGINE BLEED FOR 15-20 MINUTES. NO SMOKE NOTED. DID NOTICE RT PACK MODE SELECT IN MANUAL, SWITCHED TO AUTO. OPS CHECKED GOOD, NO DISCREPANCIES NOTED.

Source: SDR SWIA200211241 · FAA SDRS
K B · 2002-09-09 Matched by certificate designator
ATA 7261

RIGHT ENGINE SMOKES ON SHUTDOWN. FOUND ENGINE BLOWING OIL OUT FROM FRONT COMPRESSOR. REMOVED AND REPLACED RT ENGINE AS REQUIRED IAW 71-00-00. OPS CHECK GOOD. PACKS NO LONGER SMOKING.

Source: SDR SWIA200211211 · FAA SDRS
F J · 2002-08-30 Matched by certificate designator
ATA 2211

CAPTAINS AUTOPILOT DOES NOT CAPTURE GS WITH APPR MODE. CAPTAIN'S AUTOPILOT FAILED WITH AILERON SERVO FAILURE. REPLACED PUSHED OUT PIN 44 ON J3 OF PILOT'S AUTOPILOT COMPUTER RACK. CAPTAIN`S AUTOPILOT OPS CHECK GOOD IAW MM 22-10-00. TESTED AILERON SERVO WITH BOTH CAPT'S AND F/O'S AUTOPILOT. COULD NOT DUPLICATE DISCREPANCY. BOTH AUTOPILOTS AND AILERON SERVO OPS CHECKS GOOD IAW MM 22-10-00.

Source: SDR SWIA200211197 · FAA SDRS
L · 2002-03-01 Matched by certificate designator
ATA 3350

EXIT SIGN ON FIRST OFFICER'S SIDE BULKHEAD DOES NOT ILLUMINATE WHEN EMERGENCY LIGHTS ARE TESTED. FOUND LOOSE CONNECTION. SECURED CONNECTION. OPS CHECK GOOD.

Source: SDR SWIA200210696 · FAA SDRS
J · 2002-01-04 Matched by certificate designator
ATA 3425

AFTER DEPARTURE, BOTH THE EHSI AND THE NAVIGATION SCREENS WENT BLANK ON THE FIRST OFFICER'S SIDE. REMOVED AND REPLACED CTL32 (NR 2). OPS CHECKS GOOD ON GROUND.

Source: SDR SWIA200210517 · FAA SDRS
J · 2001-05-08 Matched by certificate designator
ATA 3425

FIRST OFFICERS HDG FLAG AND NR 1 RMI FLAG ON IN CRUISE. RETURNED TO THE FIELD. RE-ORIENTATED BOTH NR 1 AND 2 AHRS SYSTEMS IAW 34-00-00. GROUND OPS CHECK GOOD AT THIS TIME.

Source: SDR SWIA972558 · FAA SDRS
F · 2001-04-21 Matched by certificate designator
ATA 2710

ON DOWNWIND THE AILERONS FROZE FOR 12 SECONDS, WE WERE UNABLE TO MOVE YOKE. ON BASE TURN THE AILERONS FROZE FOR 5 SECONDS AND ON FINAL THE AILERONS FROZE FROM APPROX 200 FT AGL UNTIL 20 SECONDS AFTER ROLLOUT. AUTOPILOT WAS CONFIRMED DISCONNECTED BY BOTH PILOTS. WHEN AILERONS WERE FROZEN THE YOKE WAS NEUTRAL AND UNMOVEABLE BY BOTH PILOTS. REMOVED UPPER AND LOWER ACCESS PANELS TO LEFT AND RIGHT AILERONS. INSPECTED YOKE CHAIN DRIVE. NO DEFECTS NOTED. FOUND PANEL MISSING 2 SCREWS ON LT AILERON JUST FWD OF THE TRIM TAB. LEADING EDGE WAS BENT FORWARD AND IMPEDING TRAVEL ON LEFT AILERON BELLCRANK. RE-SECURED PANEL. SCREW HOLES ARE NOT ELONGATED. CLOSED ALL PANELS. CONTROL DISCONNECT LIGHTS OUT ON MAP.

Source: SDR SWIA972529 · FAA SDRS
F · 2001-02-25 Matched by certificate designator
ATA 2731

ELEVATOR TRIM FROZE IN FLIGHT AND BROKE LOOSE SUDDENLY, CAUSING VIOLENT PITCH DOWN. REMOVED AND REPLACED RIGHT AND LEFT ELEVATOR TRIM TAB LINEAR ACTUATORS IAW EMB 120 MM 27-32-02 AND 27-00-01. LEFT TRIM ACTUATOR S/N OFF: 735, S/N ON: UNKNOWN. RIGHT TRIM ACTUATOR S/N OFF: 736, S/N ON: 426.

Source: SDR SWIA972399 · FAA SDRS
B J · 2001-01-04 Matched by certificate designator
ATA 2163

NOTICED HOT AIRCRAFT BEFORE TAKEOFF. AFTER TAKEOFF FA SMELLED SMOKE AND SMOKE DETECTOR IN LAV WENT OFF. RETURNED TO LAX. INSTALLED NEW LEFT PAC DUCT TEMP SENSOR. CHECKS GOOD.

Source: SDR SWIA972245 · FAA SDRS
J · 2000-09-01 Matched by certificate designator
ATA 3020

RIGHT ENGINE DUCT LEAK LIGHT ILLUMINATED ONE MINUTE AFTER TAKEOFF. RIGHT ENGINE WAS SHUT DOWN PER QRH PROCEDURE. RETURNED TO PSP AIRPORT. REPLACED RIGHT DEICE LINE PRESSURE REGULATOR VALVE. RAN RIGHT ENGINE FOR SEVERAL MINUTES AT TAKEOFF SETTINGS. OPS CHECKS GOOD. P/N ON: 38E96-6A, S/N: RF-2273, S/N OFF: B-2266.

Source: SDR SWIA971954 · FAA SDRS
J · 2000-08-20 Matched by certificate designator
ATA 5230

AIRCRAFT LOST PRESSURIZATION AT 17,000 FEET. SLOW LOSS OF PRESSURIZATION, DESCENDED PER QRH. RETURNED TO LAX. INSPECTED AND FOUND SMALL SECTION OF CARGO DOOR SEAL LOOSE FROM RETAINER. REINSTALLED AND SECURED CARGO DOOR SEAL. PRESSURIZED AIRCRAFT TO 5+ PSID. NO LEAKS NOTED. PRESSURIZATION OPS CHECKS GOOD.

Source: SDR SWIA971944 · FAA SDRS
N · 1999-11-26 Matched by certificate designator
ATA 5297

PASSENGER DOOR LIGHT CAME ON AFTER TAKEOFF. RETURNED TO SEA. REPAIRED BROKEN WIRE AT DOOR HINGE, OPS CHECK GOOD IAW 52.

Source: SDR SWIA971612 · FAA SDRS
J · 1999-05-08 Matched by certificate designator
ATA 2131

CABIN ALTITUDE CLIMBS IN AUTO, OK IN MANUAL. RETURNED TO SFO. REPLACED AUTO CONTROLLER. OPS CHECKS GOOD.

Source: SDR SWIA971483 · FAA SDRS
B · 1999-03-03 Matched by certificate designator
ATA 2150

DIVERTED TO BUR WHEN THE LEFT PACK FAILED AND FILLED CABIN WITH SMOKE. OPERATIONAL CHECKED LEFT PACK, LEFT ENGINE HIGH STAGE BLEED SWITCHING SYSTEM, RAM AIR SYSTEM AND PACK FAIL SWITCH WIRING. NO DISCREPANCIES NOTED ANY WHERE. ALL SYSTEMS OPERATE NORMALLY.

Source: SDR SWIA971437 · FAA SDRS
N · 1997-11-18 Matched by certificate designator
ATA 3620

RIGHT DUCT LEAK LIGHT CAME ON AFTER TAKEOFF DURING CLIMB-OUT. WENT THROUGH PROCEDURE BUT THE LIGHT WOULD NOT EXTINGUISH UNTIL ENGINE SHUTDOWN. RETURNED TO SLC. INSPECTED ENTIRE RIGHT SIDE BLEED ON DUCT SYSTEM AND FOUND NO DISCREPANCIES. RAN AIRCRAFT ON GROUND FOR 1/2 HR AND COULD NOT DUPLICATE.

Source: SDR SWIA971032 · FAA SDRS
O · 1997-10-28 Matched by certificate designator
ATA 5320

CORRODED BUTT STRAP JUST FORWARD OF AFT CENTER BUTT STRAP. REMOVED CENTER BUTT STRAP SECOND FROM AFT OF PLANE AND REPLACED WITH A NEW BUTT STRAP IAW SRM 51-40-02.

Source: SDR SWIA971023 · FAA SDRS
O · 1997-10-28 Matched by certificate designator
ATA 5320

AFT CENTER BUTT STRAP CORRODED. REMOVED AFT CENTER BUTT STRAP AND REPLACED WITH A NEW BUTT STRAP IAW SRM 51-40-02.

Source: SDR SWIA971022 · FAA SDRS
O · 1997-10-28 Matched by certificate designator
ATA 5320

CORRODED CENTER OMEGA BEAM AFT CABIN ADJACENT TO LAVATORY. REMOVED CENTER OMEGA BEAM AFT CABIN ADJACENT TO LAVATORY AND REPLACED WITH A NEW OMEGA BEAM IAW SRM 51-40-02.

Source: SDR SWIA971026 · FAA SDRS
O · 1997-10-28 Matched by certificate designator
ATA 5320

RIGHT CENTER FLOOR BOARD CROSS BEAM TOP PLATE CORRODED, ADJACENT TO LAVATORY. REMOVED AND REPLACED RIGHT CENTER FLOOR BOARD CROSS BEAM TOP T-SECTION ADJACENT TO LAVATORY IAW SRM 51-40-02.

Source: SDR SWIA971025 · FAA SDRS
O · 1997-10-28 Matched by certificate designator
ATA 5320

RT AFT BUTT STRAP CORRODED. REMOVED AND REPLACED RT AFT BUTT STRAP WITH A NEW BUTT STRAP IAW MM SRM 51-40-02.

Source: SDR SWIA971024 · FAA SDRS
K J · 1996-07-28 Matched by certificate designator
ATA 2910

IN-FLIGHT FAILURE OF THE BLUE HYDRAULIC SYSTEM WITH LOSS OF FLUID. FOUND NR 6 HYDRAULIC LINE CHAFING ON ENGINE OIL COOLER AIR INLET. REPLACED NR 6 LINE AND RIGHT ENGINE DRIVEN HYDRAULIC PUMP. RAN RIGHT ENGINE, OPS CHECK AND LEAK CHECK GOOD.

Source: SDR SWIA95753 · FAA SDRS