N31171

FAIRCHILD SA227-AC · 1985 · Valid Registration

Registered owner: CBG LLC, OR (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
KEY LIME AIR CORPORATION (KY7A)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2025-09-17 Matched by certificate designator
ATA 3240

LEFT BRAKE SPONGEY, WILL GO ALL THE WAY TO THE FLOOR. BLED & SERVICED BRAKE SYSTEM IAW SA277 MM CH 32-41-00. RTS CHECKS COMPLETED

Source: SDR KY7A2025093000038 · FAA SDRS
K J · 2025-01-15 Matched by certificate designator
ATA 2910

R & R ENGINE HYDRAULIC PRESSURE LINE. IAW SA227A MM 29-00-00 OPS CHECK GOOD.

Source: SDR KY72025F00000 · FAA SDRS
O · 2024-01-30 Matched by certificate designator
ATA 2161

LEFT THROTTLE NOT RESPONSIVE. R &R LH POWER CABLE IAW FAIRCHILD SA227 MM CHAPTER 76-10-00. OPS GOOD.

Source: SDR KY7A2024040800038 · FAA SDRS
O · 2023-12-19 Matched by certificate designator
ATA 7722

E1 DOESN'T MAKE TORQUE ON GROUND OR IN FLIGHT. REMOVED & REPLACED EGT COMPENSATOR AND PREFORMED ENGINE RIGGING CHECK PER SA227 MM CH 71-00-30.

Source: SDR KY7A20230120038 · FAA SDRS
O · 2022-08-29 Matched by certificate designator
ATA 3230

PILOT REPORTED THAT HE HAD CYCLE THE GEAR HANDLE MULTIPLE TIMES BEFORE GEAR WOULD ACTUATE

Source: SDR 2022FA0000484 · FAA SDRS
O · 2021-05-01 Matched by certificate designator
ATA 3230

CREW REPORTED LANDING GEAR WOULD NOT EXTEND AND SWITCHED ESS BUS TRANSFER AND STILL WOULDN'T WORK, GEAR RETRACTED AFTER ATTEMPTING QUITE A FEW TIMES. MX INSPECTED THE LANDING GEAR AND MADE SURE ALL HANDLES WERE STOWED, LUBED GEAR COMPLETED RETRACT CHECKS. LANDING GEAR OPS CHECKED GOOD.

Source: SDR KY7A20210501001 · FAA SDRS
K · 2021-04-05 Matched by certificate designator
ATA 2910

HYDRAULIC LEAK IN NOSE GEAR IN FLIGHT. MX REMOVED AND REPLACED NLG STEERING LINE WITH A NEW NLG STEERING LINE. MX DID GROUND RUNS AND OPERATIONAL CHECKS WERE GOOD.

Source: SDR KY7A20210405001 · FAA SDRS
R · 2019-12-02 Matched by certificate designator
ATA 7497

PILOT REPORTED PARTIAL POWER LOSS IN FLIGHT, PILOT ACTIVATED CONTINUOUS IGNITION WHICH RESTORED POWER. AUTO IGNITION DID NOT OPERATE PROPERLY. MX PERFORMED NTS GROUND CHECK IAW TPE331 MM CHAPTER 72-00-00 TROUBLE-SHOT SYSTEM AUTO IGNITION SWITCH NOT EXTINGUISHING DUE TO BROKEN WIRE, REAPPLIED WIRE POST. OPERATIONAL CHECK GOOD AND NTS CHECK GOOD.

Source: SDR KY7A201912052001 · FAA SDRS
J · 2015-06-22 Matched by certificate designator
ATA 3260

FLIGHT CREW REPORTED LG WOULD NOT RETRACT AFTER TAKEOFF. FOUND DEFECTIVE UPLOCK SWITCH & REPLACED.

Source: SDR KY7A20150622001 · FAA SDRS
X J · 2010-11-05 Matched by certificate designator
ATA 7310

ON APPROACH FOR LANDING, THE RT ENGINE FLAMED OUT. AFTER INSP, A FUEL LINE PN 894568-1 BETWEEN THE FCU AND THE FUEL FLOW TRANSDUCER WAS FOUND CRACKED AT THE ATTACHMENT TO THE FUEL CONTROL. THIS IS THE SECOND FAILURE OF THIS LINE IN OUR FLEET. THE FUEL FLOW TRANSDUCER IS SUPPORTED ONLY BY THE FUEL LINES IN AND OUT AND IT IS BELIEVED THIS LEADS TO FATIGUE OF THE LINE. A SUPPORT BRACKET FOR THE TRANSDUCER WOULD BE BENEFICIAL.

Source: SDR KY7AR4480 · FAA SDRS
J K · 1996-07-30 Matched by certificate designator
ATA 7261

AIRCRAFT WAS ON APPROACH WHEN RIGHT ENGINE OIL LIGHT CAME ON. PILOT CHECKED PRESSURE AND FOUND OIL PSI WAS LOW AND SHUT ENGINE DOWN WITH STOP AND FEATHER. LANDED WITH NO FURTHER PROBLEM. DRIVE GEAR ON THE TURBINE SCAVENGE PUMP SEARED APPROX 3 TEETH, CAUSING TURBINE BEARING TO CAVITY AND TO FILL WITH OIL AND LEAK INTO EXHAUST. THE TEETH ON THE SHAFT DRIVING PUMP WAS ALSO DAMAGED AND REQUIRED REPLACEMENT. SCAVENGE PUMP AND DRIVE SHAFT WAS REPLACED. (M)

Source: SDR HKGA0012 · FAA SDRS