N331FX

EMBRAER-EMPRESA BRASILEIRA DE EMB-505 · 2011 · Valid Registration

Registered owner: FLEXJET LLC, OH (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
FLEXJET, LLC (J7SA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2025-12-26 Matched by certificate designator
ATA 2750

ON START UP, FLAP FAIL CAS ILLUMINATED AND FLAP INDICATOR ON MFD SHOWED YELLOW. CYCLED FLAPS AND MESSAGE REMAINED. REPLACED FCE 1 IAW EMB 505 AMM 27-03-01. RIGGING/OPS CHECK GOOD.

Source: SDR J7SA2026010600468 · FAA SDRS
J · 2025-12-22 Matched by certificate designator
ATA 2750

DURING CRUISE, CREW RECEIVED SWPS FAULT, FLAPS FAIL, PTRIM BKP FAIL AND SPOILER FAULT. AIRCRAFT LANDED WITHOUT INCIDENT. REPLACED FCE 1 IAW EMB 505 AMM 27-03-01. FCE 1 RIGGING / OPS CHECK GOOD AND NO CAS MESSAGE ILLUMINATED.

Source: SDR J7SA2026010600466 · FAA SDRS
J · 2024-06-08 Matched by certificate designator
ATA 2760

CREW RECEIVED GROUND SPOILER FAIL ON LANDING. REPLACED # 2 FCE IAW PH300 AMM 27-03-01.

Source: SDR J7SA2024070100405 · FAA SDRS
J · 2024-05-19 Matched by certificate designator
ATA 2760

CREW RECEIVED GROUND SPOILER FAULT, SPOILER FAIL, AND PRIMARY TRIM FAIL (PTRIM NML FAIL). REPLACED FAILED # 2 FCE. PERFORMED SPOILER ELECTRONIC RIGGING. OPS CHECK GOOD. ALL WORK COMPLETED IAW PHENOM 300 AMM 27-03-01.

Source: SDR J7SA2024060300402 · FAA SDRS
B · 2019-08-08 Matched by certificate designator
ATA 2497

ELECTRICAL BURN SMELL. FOUND BURNT WIRE HARNESS (W311) AT LH PDU CONNECTING TO THE GPU POWER RECEPTACLE. REMOVED AND REPLACED THE LPDU EXTERNAL POWER RECEPTACLE, AND HARNESS W311 REF PHENOM 300 AMM 24-65-01 AND 24-41-00 PERFORMED OPS CHECKS OPS CHECKED GOOD. AMM 24-61-00

Source: SDR DJFA201908238001 · FAA SDRS
M J · 2006-05-21 Matched by certificate designator
ATA 7200

LEFT ENGINE ITT WENT INTO THE RED. ENGINE ICON POSTED ABOVE THE ITT GAUGE. THE PILOT OBSERVED THE LEFT ITT WAS ABOVE 900. DURING TAKEOFF ROLL THE LEFT ENGINE ITT WENT INTO THE RED. THE ENGINE ICON POSTED ABOVE THE ITT GAUGE. THE PILOT OBSERVED THE LEFT ITT WAS ABOVE 900. ELECTED TO PULL BACK POWER AND ABORT TAKEOFF. MDC ENGINE EXCEED OBSERVED LEFT ENGINE WENT TO 909 FOR 4.1 SECONDS. AIRCRAFT IS BEING TROUBLESHOT BY MAINTENANCE. WILL FILE ADDITIONAL DATA AS IS DISCOVERED.

Source: SDR 6045491052106 · FAA SDRS