N340SF

EUROCOPTER DEUTSCHLAND GMBH MBB-BK 117 C-2 · 2010 · Valid Registration

Registered owner: OSF AVIATION LLC, IL (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
OSF AVIATION LLC (O84A)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

N · 2025-11-26 Matched by certificate designator
ATA 2297

YAW ACTUATOR LIGHT ILLUMINATED ON AUTO PILOT TEST. INSPECTED, CLEANED, AND RESEATED THE YAW SEMA CANNON PLUG PROBLEM WENT AWAY.

Source: SDR 2025FA0000787 · FAA SDRS
M · 2025-11-10 Matched by certificate designator
ATA 7720

DURING START UP PILOT REPORTED POSSIBLE OVER TEMP OF ENGINE. AFTER FURTHER INSPECTION FOUND A BAD TEMP PROBE.

Source: SDR 2025FA0000752 · FAA SDRS
R · 2025-01-31 Matched by certificate designator
ATA 7601

DURING DECENT THE VARTOMS SYSTEM DISENGAGED. CAUSING THE NUMBER 1 ENGINE TORQUE TO DECREASE. THE PILOT WAS UNABLE TO GET THE TORQUES MATCHED MANUALLY. ABORTED THE LANDING AND PROCEEDED TO AN AIRPORT TO PERFORM A PRECAUTIONARY LANDING. AFTER EXTENSIVE TROUBLESHOOTING AND CONTACT WITH TECH SUPPORT, WE COULD NOT DUPLICATE THE ISSUE OR FIND ANY FAULTS WITH THE SYSTEM.

Source: SDR 2025FA0000075 · FAA SDRS
J · 2023-10-31 Matched by certificate designator
ATA 7540

#2 ENGINE CHIP LIGHT AFTER START. BURNT CHIP AND IT CAME BACK. SHUTDOWN AND CALLED MX

Source: SDR 2023FA0000699 · FAA SDRS
J · 2023-08-11 Matched by certificate designator
ATA 7200

DURING CRUISE #1 ENGINE WARNING. AFTER 2 ATTEMPTS TO BURN THE LIGHT REMAINED ON. POWER WAS REDUCED AND PLANNING FOR A PRECAUTIONARY LANDING BEGAN. THE ENGINE WAS THEN SHUT DOWN AND A RUN-ON LANDING WAS PERFORMED WITH NO FURTHER INCIDENT. AFTER INSPECTION THE ENGINE WAS DETERMINED UNAIRWORTHY AND WAS REMOVED AND REPLACED.

Source: SDR 2023FA0000418 · FAA SDRS
M · 2023-07-16 Matched by certificate designator
ATA 7720

ENGINE OVER TEMP ON START. T4 CIRCUIT BOARD TT UNKNOWN

Source: SDR 2023FA0000378 · FAA SDRS
J · 2022-10-28 Matched by certificate designator
ATA 6540

1&2 NP AND ROTOR RPM INDICATOR (TRIPLE TAC) WAS INOP DURING THE START SEQUENCE.

Source: SDR 2022FA0000655 · FAA SDRS
J · 2020-08-24 Matched by certificate designator
ATA 3150

DURING FLIGHT, ACTUATOR CAUTION APPEARED ON CAD. PILOT DECIDED TO LAND AT BMI AIRPORT INSTEAD OF HIS DESTINATION AT HOSPITAL. COULD NOT DUPLICATE FAULT AFTER A POWER CYCLE.

Source: SDR 2020FA0000385 · FAA SDRS
B · 2017-12-15 Matched by certificate designator
ATA 3397

ENROUTE TO HOSPITAL, THERE WAS A BRIGHT FLASH IN COCKPIT AND A BURNED ELECTRICAL ODOR. AIRCRAFT TURNED BACK TO BASE AND CONTACTED FLIGHT COM. AFTER A FEW MOMENTS THE SMELL CEASED SO THEY CONTINUED BACK TO BASE. BOUT I MINUTE FROM LANDING ANOTHER FLASH APPEARED IN THE COCKPIT FROM THE OVERHEAD CIRCUIT BREAKER PANEL AND THEY LANDED AT THE AIRPORT AND CONTACTED MAINTENANCE. MAINTENANCE FOUND THE WIRING FOR THE CIRCUIT PANEL BACKLIGHTING WAS PINCHED BETWEEN THE PANEL AND THE AIRFRAME CAUSED BY WORK BEING DONE IN THAT AREA EARLIER THAT DAY. THE WIRING WAS REPAIRED AND REROUTED TO PREVENT THIS FROM HAPPENING AGAIN. THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 2018F00054 · FAA SDRS
J · 1996-11-02 Unresolved
ATA 2913

HYDRAULIC SYSTEM WARNING ON CWP SYSTEM PRESSURE INDICATED ZERO AND LANDING GEAR INDICATED UNSAFE. REPLACED THE HYDRAULIC SYSTEM PUMP.

Source: SDR COMA9630156 · FAA SDRS
O · 1996-09-30 Unresolved
ATA 3230

NOSE GEAR ASSIST SPRING BROKEN. REPLACED NOSE UPLOCK HOOK RETRACT SPRING.

Source: SDR COMA9630148 · FAA SDRS
O · 1996-04-02 Unresolved
ATA 6111

LEFT PROPELLER, BLADE EROSION GUARDS, ARE CRACKED AND DEBONDING. REPLACED PROPELLER.

Source: SDR COMA9630094 · FAA SDRS
O · 1996-03-18 Unresolved
ATA 6114

RT PROPELLER RPM DROPPED TO 1340 DURING LANDING. REPLACED THE PROPELLER PISTON DOME O-RING.

Source: SDR COMA9630070 · FAA SDRS
N · 1996-02-27 Unresolved
ATA 2613

RT TAIL PIPE HOT WARNING ILLUMINATED DURING TAKEOFF. DRIED MOISTURE ON THE TAIL PIPE HEAT SENSORS. ACFT RETURNED TO SERVICE.

Source: SDR COMA9630047 · FAA SDRS
Y · 1996-01-23 Unresolved
ATA 7320

LEFT ENGINE SHUT DOWN IN-FLIGHT. TORQUE WAS ERRATIC FOR 3 SECONDS AND THEN SHUT DOWN BY ITSELF. PROBLEM COULD NOT BE DUPLICATED. ENGINE WAS INSPECTED AND NO DEFECTS NOTED. THE ELECTRONIC CONTROL UNIT WAS REPLACED AS A PRECAUTIONARY MEASURE. PART TOTAL CYCLES, 15,108.

Source: SDR COMA9630023 · FAA SDRS
N · 1996-01-02 Unresolved
ATA 2613

RIGHT ENGINE TAIL PIPE HOT WARNING SHORTLY AFTER TAKEOFF. COULD NOT DUPLICATE DISCREPANCY. GROUND RUNS WERE NORMAL AND ACFT RETURNED TO SERVICE.

Source: SDR COMA9630004 · FAA SDRS
O · 1996-01-02 Unresolved
ATA 7603

WHEN THE RIGHT ENGINE POWER LEVER WAS ADVANCED DURING CRUISE, THE ENGINE SURGED TO 95 PERCENT. REPLACED BINDING RT ENGINE POWER LEVER CABLE.

Source: SDR COMA9630003 · FAA SDRS
O · 1995-12-18 Unresolved
ATA 7722

RT ENGINE ITT INDICATION IS ERRATIC. REPLACED THE ITT THERMOCOUPLE HARNESS ASSY.

Source: SDR COMA9531214 · FAA SDRS
B · 1995-12-04 Unresolved
ATA 3425

DURING ENGINE START PILOT'S EFIS TUBES WENT BLANK AND SMOKE WAS NOTICED FROM GLARESHIELD AREA. REPLACED THE PILOT'S EAD2-EFD-86.

Source: SDR COMA9531198 · FAA SDRS
O · 1995-10-28 Unresolved
ATA 2435

THE LEFT ENGINE WOULD NOT ROTATE DURING START CYCLE. REPLACED THE LEFT ENGINE STARTER/GENERATOR.

Source: SDR COMA9531181 · FAA SDRS
P · 1995-08-14 Unresolved
ATA 3260

NOSE LANDING GEAR DOWN AND LOCKED INDICATOR IS INOP. REPLACED THE LANDING GEAR CONTROL HANDLE ASSY.

Source: SDR COM31136 · FAA SDRS
N · 1995-05-25 Unresolved
ATA 7712

WITH CTOT ENGAGED, THE RT ENGINE TORQUE ADVANCED TO 120 PERCENT. PLACED CTOT SYSTEM ON DEFERRED MAINTENANCE LIST AND AIRCRAFT CONTINUED SERVICE.

Source: SDR COM31091 · FAA SDRS
O · 1995-05-10 Unresolved
ATA 3250

NOSE WHEELS TURNED 180 DEGREES TO THE LEFT. REPOSITIONED NOSE WHEELS, INSPECTED SYSTEM AND FOUND TO BE SERVICEABLE. AIRCRAFT CONTINUED SERVICE.

Source: SDR COM31076 · FAA SDRS
O · 1995-04-06 Unresolved
ATA 3246

MECHANIC REMOVED WHEEL ASSEMBLY FROM A/C DUE TO TIRE WORN TO LIMITS. DURING INSPECTION, FOUND INNER RACE HAD SPUN. SUBASSEMBLY HAS BEEN REMOVED FROM SERVICE AND SENT TO ABS FOR BUSHING REPAIR.

Source: SDR COM31056 · FAA SDRS
O · 1995-04-03 Unresolved
ATA 7603

WHEN RT POWER LEVER IS ADVANCED ABOVE FLIGHT IDLE, ENGINE OVERSPEEDS. ADJUSTED POWER LEVER CONTROLS AIRFRAME RIGGING TO M/N SPECS. SYSTEM OPERATES NORMAL.

Source: SDR COM31054 · FAA SDRS
O · 1995-03-13 Unresolved
ATA 3246

MECHANIC REMOVED WHEEL ASSY FROM A/C DUE TO TIRE WORN TO LIMITS. DURING VISUAL INSPECTION FOUND INNER RACE HAD SPUN. SUBASSY HAS BEEN REMOVED FROM SERVICE AND SENT TO ABS FOR REPAIR.

Source: SDR COM31044 · FAA SDRS
O · 1995-03-13 Unresolved
ATA 3246

MECHANIC REMOVED WHEEL ASSY FROM A/C DUE TO TIRE WORN TO LIMITS. DURING VISUAL INSPECTION FOUND INNER RACE HAD SPUN. SUBASSY HAS BEEN SENT TO ABS FOR REPAIR.

Source: SDR COM31045 · FAA SDRS
O · 1995-02-06 Unresolved
ATA 2720

RUDDER LIMITER WARNING ACTIVATED. REPLACED DEFECTIVE WIRING CONNECTOR ON RUDDER LIMITER OVERRIDE ACTUATOR.

Source: SDR COM31029 · FAA SDRS
M Y · 1995-01-13 Unresolved
ATA 7200

RT ENGINE FAILED DURING CLIMB. REPLACED THE ENGINE ASSY.

Source: SDR COM31007 · FAA SDRS