OSF AVIATION LLC

Part 135 operator · designator O84A

Data confidence: Records are linked by certificate number, aircraft registration, or a name match that a reviewer has confirmed. Each record below shows how it was linked.

Also recorded as: OSF AVIATION LLC

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

Acc · 2017-10-12 Operator named in NTSB report
EUROCOPTER DEUTSCHLAND GMBH MBB BK 117 (N140SF) None injury Part 91

Operated by OSF AVIATION LLC. (per NTSB report)

Source: NTSB case GAA18CA012
Inc · 2009-07-01 Operator named in NTSB report
BELL 230 (N880SF) None injury Part 135

Operated by OSF AVIATION LLC (per NTSB report)

Source: NTSB case CEN09IA618

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

51 reports on file — showing most recent 50.

E · 2026-06-22 Matched by certificate designator
N240SF · ATA 2121

UNUSUAL NOISE FROM THE PASSENGER BLOWER MOTOR.

Source: SDR 2026FA0000545 · FAA SDRS
B · 2026-06-09 Matched by certificate designator
N240SF · ATA 2121

DURING TAKEOFF IT WAS NOTED AN UNUSUAL NOISE WAS HEARD IN THE CABIN OVERHEAD FOLLOWED BY AN ODOR. ABORTED TAKEOFF AND SHUT DOWN AIRCRAFT.

Source: SDR 2026FA0000509 · FAA SDRS
J · 2026-05-10 Matched by certificate designator
N440SF · ATA 2436

NR 1 GENERATOR DISCONNECT ON THE CAD. RESET ATTEMPTED AND STILL DISCONNECTED. PATIENT FLIGHT ABORTED DUE TO MEL RESTRICTION OF DAY VFR ONLY.

Source: SDR 2026FA0000365 · FAA SDRS
J · 2026-05-10 Matched by certificate designator
N440SF · ATA 2436

NR 1 GENERATOR DISCONNECT ON THE CAD. RESET ATTEMPTED AND STILL DISCONNECTED. PATIENT FLIGHT ABORTED DUE TO MEL RESTRICTION OF DAY VFR ONLY.

Source: SDR 2026FA0000366 · FAA SDRS
J · 2026-05-10 Matched by certificate designator
N440SF · ATA 2436

NR 1 GENERATOR DISCONNECT ON THE CAD. RESET ATTEMPTED AND STILL DISCONNECTED. PATIENT FLIGHT ABORTED DUE TO MEL RESTRICTION OF DAY VFR ONLY.

Source: SDR 2026FA0000367 · FAA SDRS
J · 2026-05-10 Matched by certificate designator
N440SF · ATA 2436

NR 1 GENERATOR DISCONNECT DISPLAYED ON THE CAD. RESET GENERATOR TO NO AVIAL. DUE TO MEL RESTRICTIONS OF DAY VFR ONLY FLIGHT WAS ABORTED.

Source: SDR 2026FA0000368 · FAA SDRS
J · 2026-05-10 Matched by certificate designator
N440SF · ATA 2436

#1 GENERATOR DISCONNECT LIGHT DISPLAYED ON CAD. CONFIRMED LOSS OF GENERATOR. RESET ATTEMPTS FAILED. ABORTED FLIGHT AS MEL ONLY ALLOWED DAY VFR AND COULD NOT COMPLETE THE PATIENT TRANSFER BEFORE SUNSET.

Source: SDR 2026FA0000400 · FAA SDRS
N · 2025-11-26 Matched by certificate designator
N340SF · ATA 2297

YAW ACTUATOR LIGHT ILLUMINATED ON AUTO PILOT TEST. INSPECTED, CLEANED, AND RESEATED THE YAW SEMA CANNON PLUG PROBLEM WENT AWAY.

Source: SDR 2025FA0000787 · FAA SDRS
M · 2025-11-10 Matched by certificate designator
N340SF · ATA 7720

DURING START UP PILOT REPORTED POSSIBLE OVER TEMP OF ENGINE. AFTER FURTHER INSPECTION FOUND A BAD TEMP PROBE.

Source: SDR 2025FA0000752 · FAA SDRS
N · 2025-10-19 Matched by certificate designator
N240SF · ATA 6597

PILOT REPORTED TR CHIP CT ON WARNING UNIT DURING STARTUP. FLIGHT WAS THEN ABORTED. MX FOUND A CHAFED WIRE ON THE TAIL SECTION THAT CAUSED CONTINUITY TEST TO FAIL. WIRE WAS REPAIRED AND AIRCRAFT WENT BACK IN SERVICE.

Source: SDR 2025FA0000726 · FAA SDRS
M · 2025-10-01 Matched by certificate designator
N140SF · ATA 7700

DURING START UP THE PILOT NOTED A HIGH RISE IN TEMP WHICH EXCEEDED ALLOWABLE TEMP FOR START. IMMEDIATELY SHUT THE ENGINE DOWN. CONTACTED MX. PER THE MX MANUAL NO TEMPS WERE EXCEEDED PER THE MX MANUAL ONLY THE "ALLOWABLE" LIMIT FOR PILOT START. FURTHER TROUBLESHOOTING FOUND A FAULTY TEMP PROBE WHICH WOULD HAVE CAUSED A HIGHER THAN NORMAL TEMP DURING THE START. CHANGED THE TEMP PROBE AND ENGINE STARTED NORMAL.

Source: SDR 2025FA0000682 · FAA SDRS
J · 2025-09-12 Matched by certificate designator
N240SF · ATA 6710

VARTOMS SYSTEM KICKED INTO MANUAL MODE AS ENGINES COULDN'T HOLD TORQUE MATCHING AT THE SPECIFIC POWER SETTING. SYSTEM WAS TROUBLESHOT AND FOUND TO BE WITHIN ALL PARAMETERS. NO DEFECTS NOTED DURING TEST FLIGHTS.

Source: SDR 2025FA0000647 · FAA SDRS
W J · 2025-05-24 Matched by certificate designator
N140SF · ATA 7320

ENGINE WOULD NOT START. THE ENGINE WAS FLOODED WITH FUEL

Source: SDR 2025FA0000382 · FAA SDRS
O · 2025-05-02 Matched by certificate designator
N140SF · ATA 8097

PATIENT ONBOARD FOR DEPARTURE #2 ENGINE WOULD NOT START. FOUND A BAD TERMINAL BOARD AND BUS TIE RELAY.

Source: SDR 2025FA0000341 · FAA SDRS
R · 2025-01-31 Matched by certificate designator
N340SF · ATA 7601

DURING DECENT THE VARTOMS SYSTEM DISENGAGED. CAUSING THE NUMBER 1 ENGINE TORQUE TO DECREASE. THE PILOT WAS UNABLE TO GET THE TORQUES MATCHED MANUALLY. ABORTED THE LANDING AND PROCEEDED TO AN AIRPORT TO PERFORM A PRECAUTIONARY LANDING. AFTER EXTENSIVE TROUBLESHOOTING AND CONTACT WITH TECH SUPPORT, WE COULD NOT DUPLICATE THE ISSUE OR FIND ANY FAULTS WITH THE SYSTEM.

Source: SDR 2025FA0000075 · FAA SDRS
O · 2025-01-23 Matched by certificate designator
N140SF · ATA 3320

LOSS OF ALL MED CREW LIGHTING AND POWER RECEPTACLES

Source: SDR 2025FA0000051 · FAA SDRS
J · 2025-01-14 Matched by certificate designator
N140SF · ATA 2210

ON APPROACH PILOT OBSERVED CAUTION ON THE CAD FOR AP1 ACTUATOR WITH A P ON THE PFD. THIS WAS DURING EXTREME COLD TEMPERATURES. COULD NOT DUPLICATE.

Source: SDR 2025FA0000082 · FAA SDRS
J · 2025-01-05 Matched by certificate designator
N240SF · ATA 7600

ON APPROACH THE VARTOMS SYSTEM DISENGAGED AND TORQUE MATCHING HAD TO BE PERFORMED MANUALLY

Source: SDR 2025FA0000013 · FAA SDRS
R · 2025-01-03 Matched by certificate designator
N140SF · ATA 6710

COLLECTIVE FRICTION WAS TOO LIGHT ALLOWING COLLECTIVE TO FALL WHEN HANDS OFF CONTROLS. FOUND THE COLLECTIVE FRICTION KNOB FULLY LOOSENED AND NOT TIGHTENED TO INPUT COLLECTIVE FRICTION ON THE COLLECTIVE ALLOWING THE CONSTANT POWER TO BE MAINTAINED.

Source: SDR 2025FA0000014 · FAA SDRS
E · 2023-12-18 Matched by certificate designator
N240SF · ATA 6230

VIBRATION FELT IN A HOOVER. FOUND ROD END BEARING WORN ON MAIN ROTOR PITCH LINK.

Source: SDR 2023FA0000839 · FAA SDRS
G · 2023-11-25 Matched by certificate designator
N240SF · ATA 3497

PILOT PFD AND ND WENT BLANK WITH AHRS INDICATION. CLEANED CONNECTOR PLUG GOING INTO MODE SELECT PANEL COULD NOT DUPLICATE THE ISSUE.

Source: SDR 2023FA0000814 · FAA SDRS
N · 2023-11-07 Matched by certificate designator
N240SF · ATA 6240

MAST MOMENT WAS EXCEEDED IN A HOVER. LANDED THE AIRCRAFT WITH NO ISSUES. AFTER TROUBLESHOOTING FOUND THE STRAIN GAUGE IN THE MAST HAD DEBONDED CAUSING A FALSE INDICATION IN THE COCKPIT.

Source: SDR 2023FA0000766 · FAA SDRS
J · 2023-10-31 Matched by certificate designator
N340SF · ATA 7540

#2 ENGINE CHIP LIGHT AFTER START. BURNT CHIP AND IT CAME BACK. SHUTDOWN AND CALLED MX

Source: SDR 2023FA0000699 · FAA SDRS
J · 2023-08-11 Matched by certificate designator
N340SF · ATA 7200

DURING CRUISE #1 ENGINE WARNING. AFTER 2 ATTEMPTS TO BURN THE LIGHT REMAINED ON. POWER WAS REDUCED AND PLANNING FOR A PRECAUTIONARY LANDING BEGAN. THE ENGINE WAS THEN SHUT DOWN AND A RUN-ON LANDING WAS PERFORMED WITH NO FURTHER INCIDENT. AFTER INSPECTION THE ENGINE WAS DETERMINED UNAIRWORTHY AND WAS REMOVED AND REPLACED.

Source: SDR 2023FA0000418 · FAA SDRS
J · 2023-07-21 Matched by certificate designator
N440SF · ATA 7200

DURING CRUISE FLIGHT THE #1 ENGINE CHIP LIGHT ILLUMINATED. AFTER 2 ATTEMPTS TO BURN THE LIGHT REMAINED ON. THE ENGINE POWER WAS REDUCED AND PLANNING FOR PRECAUTIONARY LANDING BEGAN. THE ENGINE WAS THEN SHUT DOWN AND A RUN-ON LANDING WAS PERFORMED WITH NO FURTHER INCIDENTS. THE CHIP PLUG WAS INSPECTED REF MM AND TECH SUPPORT. PLUGS CLEANED AND GROUND RUNS WERE PERFORMED, THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 2023FA0000417 · FAA SDRS
M · 2023-07-16 Matched by certificate designator
N340SF · ATA 7720

ENGINE OVER TEMP ON START. T4 CIRCUIT BOARD TT UNKNOWN

Source: SDR 2023FA0000378 · FAA SDRS
J · 2023-04-26 Matched by certificate designator
N140SF · ATA 7330

FUEL PRESSURE SENSOR FAILED

Source: SDR 2023FA0000244 · FAA SDRS
N · 2023-03-21 Matched by certificate designator
N140SF · ATA 6230

FALSE MAST MOMENT INDICATION

Source: SDR 2023FA0000162 · FAA SDRS
G · 2022-12-27 Matched by certificate designator
N140SF · ATA 7700

TRIPLE TACH WOULDN'T PASS SELF TEST ON START UP

Source: SDR 2022FA0000775 · FAA SDRS
J · 2022-10-28 Matched by certificate designator
N340SF · ATA 6540

1&2 NP AND ROTOR RPM INDICATOR (TRIPLE TAC) WAS INOP DURING THE START SEQUENCE.

Source: SDR 2022FA0000655 · FAA SDRS
J · 2022-10-28 Matched by certificate designator
N140SF · ATA 6520

RECEIVE T\R CHIP WARNING. ON SHORT FINAL TO LANDING SO NO TIME TO BURN. FOUND A SMALL SLIVER ON THE 90 DEGREE G\B. FOLLOWED MANUFACTURES RECOMMENDED PROCEDURES. NO FURTHER ISSUES

Source: SDR 2022FA0000660 · FAA SDRS
N · 2022-10-17 Matched by certificate designator
N140SF · ATA 7797

FLIGHT # 03766 - RIGHT AFTER LIFT OFF FROM GBG BASE APRON, ANALOG TRIPLE TACH GAVE ERRATIC INDICATIONS SHOWING #1 NEEDLE DROPPING TO 80-83 RANGE AND BOUNCING BACK UP TO MATCH ROTOR AND NUMBER 2. SIMULTANEOUSLY, VARTOMS DROPPED TO MANUAL MODE AND NG1 SPLIT TO HIGH SIDE, GIVING APPEARANCE OF TRYING TO DRAG THE NG2 UP. TURNED THE AIRCRAFT BACK TO THE APRON AND LANDED PROMPTLY WITHOUT FURTHER INCIDENT.

Source: SDR 2022FA0000654 · FAA SDRS
K J · 2021-06-11 Matched by certificate designator
N240SF · ATA 7261

IN CRUISE FLIGHT #1 ENGINE OIL PRESSURE LIGHT CAME ON ENGINE OIL TEMP STARTED TO RISE FOLLOWED BY DEC4REASING ENGINE TORQUE INDICATION. PILOT SHUTDOWN #1 ENGINE AND PERFORMED A RUNNING LANDING AT KYVS. INVESTIGATION SHOWED LOSS OF OIL IN ENGINE RESERVOIR AND AND BURNT OI AT THE POWER TURBINE WHEEL AT THE BACK OF THE ENGINE. ENGINE WAS REPLACED AND THE SUSPECT ENGINE WILL BE SENT TO THE MANUFACTURER FOR FURTHER INVESTIGATION.

Source: SDR 2021FA0000171 · FAA SDRS
J · 2020-08-24 Matched by certificate designator
N340SF · ATA 3150

DURING FLIGHT, ACTUATOR CAUTION APPEARED ON CAD. PILOT DECIDED TO LAND AT BMI AIRPORT INSTEAD OF HIS DESTINATION AT HOSPITAL. COULD NOT DUPLICATE FAULT AFTER A POWER CYCLE.

Source: SDR 2020FA0000385 · FAA SDRS
N · 2020-07-17 Matched by certificate designator
N440SF · ATA 6340

AIRCRAFT WAS PULLED INTO A HOVER AND THE LOW ROTOR WARNING SOUNDED AND THE ROTOR RPM READ ZERO. AIRCRAFT LANDED AND FLIGHT WAS CANCELLED.

Source: SDR 2020F00343 · FAA SDRS
J · 2018-12-03 Matched by certificate designator
N240SF · ATA 6340

M/R GEARBOX CHIP LIGHT ILLUMINATED DURING HOVER. MECHANIC INSPECTED CHIP PLUGS AND FOUND NORMAL FUZZ PER MM. CLEANED CHIP PLUGS AND PERFORMED 10 MINUTE HOVER CHECK AND FOUND NO DEBRIS ON CHIP PLUGS. RETURNED AIRCRAFT TO SERVICE.

Source: SDR O84A2018F00155 · FAA SDRS
J · 2018-11-18 Matched by certificate designator
N440SF · ATA 2822

DURING CRUISE FLIGHT F PUMP AFT WARNING APPEARED ON THE CAD. ABORTED FLIGHT AND RETURNED TO BASE AT KPIA.

Source: SDR O84A2018111900091 · FAA SDRS
B · 2017-12-15 Matched by certificate designator
N340SF · ATA 3397

ENROUTE TO HOSPITAL, THERE WAS A BRIGHT FLASH IN COCKPIT AND A BURNED ELECTRICAL ODOR. AIRCRAFT TURNED BACK TO BASE AND CONTACTED FLIGHT COM. AFTER A FEW MOMENTS THE SMELL CEASED SO THEY CONTINUED BACK TO BASE. BOUT I MINUTE FROM LANDING ANOTHER FLASH APPEARED IN THE COCKPIT FROM THE OVERHEAD CIRCUIT BREAKER PANEL AND THEY LANDED AT THE AIRPORT AND CONTACTED MAINTENANCE. MAINTENANCE FOUND THE WIRING FOR THE CIRCUIT PANEL BACKLIGHTING WAS PINCHED BETWEEN THE PANEL AND THE AIRFRAME CAUSED BY WORK BEING DONE IN THAT AREA EARLIER THAT DAY. THE WIRING WAS REPAIRED AND REROUTED TO PREVENT THIS FROM HAPPENING AGAIN. THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 2018F00054 · FAA SDRS
N · 2017-06-13 Matched by certificate designator
N140SF · ATA 7603

DURING STARTUP, THE NR 1 ENGINE TWIST GRIP LIGHT REMAINED ILLUMINATED. THE AIRCRAFT WAS SHUTDOWN AND MAINTENANCE WAS NOTIFIED. FOUND THE SWITCH WAS STICKING AND OUT OF ADJUSTMENT. THE SWITCH WAS CLEANED AND ADJUSTED AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 2017FA0000252 · FAA SDRS
N · 2015-07-28 Matched by certificate designator
N240SF · ATA 6540

TAIL ROTOR GEARBOX CHIP LIGHT OCCURRED OVER AIRPORT, MADE PRECAUTIONARY LANDING. FINISHED PATIENT TRANSPORT BY GND AMBULANCE.

Source: SDR 2015F00091 · FAA SDRS
J · 2015-02-05 Matched by certificate designator
N440SF · ATA 2497

ON FINAL APPROACH, NR 1 GEN DISCONNECT APPEARED ON CAD. AFTER SEVERAL ATTEMPTS TO RESET GENERATOR, IT REMAINED OFFLINE. THE ACFT LANDED AND MAINTENACE WAS CONTACTED. A MECHANIC WENT TO ACFT AND DEFERRED THE DISCREPANCY AND THE ACFT WAS FLOWN TO THE MAIN MAINTENACE FACILITY. THE NEXT DAY A BROKEN WIRE WAS DISCOVERED AT THE NR 1 GENERATOR.

Source: SDR O84A2015F00029 · FAA SDRS
J · 2014-11-23 Matched by certificate designator
N140SF · ATA 2210

AS AIRCRAFT WAS PICKED UP INTO A HOVER CAD WARNING ACTUATOR APPEARED WITH THE ASSOCIATED Y ON THE PILOTS PRIMARY FLIGHT DISPLAY. AIRCRAFT WAS LANDED, SYSTEM WAS RESET AND PICKED UP INTO A HOVER WITH THE SAME RESULT. AIRCRAFT LANDED, FLIGHT DISCONTINUED AND MAINTENANCE WAS CALLED.

Source: SDR O84A2015F00008 · FAA SDRS
B · 2014-10-14 Matched by certificate designator
N140SF · ATA 2120

ON LEVEL OFF AND INTO CRUISE FLIGHT, MED CREW DETECTED A STRONG FUEL ODOR IN CABIN. ODOR THEN SPREAD TO COCKPIT. FLIGHT ABORTED AND RETURNED TO PAD. ACFT INSPECTED FOR FUEL LEAKS NONE FOUND. TOOK TWO ATTEMPTS TO START NR 2 ENGINE AND ODOR IS BELIEVED TO BE EXCESS FUEL FROM THE ABORTED FIRST START.

Source: SDR O84A2014101400161 · FAA SDRS
J · 2014-09-22 Matched by certificate designator
N140SF · ATA 6520

DURING APPROACH, TAIL ROTOR CHIP LIGHT ILLUMINATED, ATTEMPT TO BURN THE CHIP WAS UNSUCCESSFUL AND A LANDING WAS MADE. DUE TO METAL IN THE TAIL ROTOR GEARBOX THE UNIT WAS REPLACED.

Source: SDR O84A201409260159 · FAA SDRS
R J · 2014-08-24 Matched by certificate designator
N440SF · ATA 7200

BRIEFLY BEFORE ENTERING CRUISE FLIGHT, BOTH ENGINE CAD DISPLAYS SHOWED ENG PA DIS. ALSO ROTOR RPM DROPPED TO THE POINT OF WP LIGHT AND HORN. PILOT LOWERD POWER AND ATTEMPTED TO BEEP UP RPM. LOWERING POWER BROUGHT UP ROTOR RPM. AFTER CONSULTING CHECKLIST FOR WARNINGS, PILOT DECIDED TO ATTEMPT RUNWAY LANDING IN CASE THERE WAS NOT ENOUGH POWER TP HOVER. AT 5 FEET THERE THERE WAS SUFFICIENT POWER AND ROTOR RPM TO HOVER SO PILOT OPTED TO HOVER OVER TO HANGAR TO LAND. ACFT WAS TAKEN OUT OF SERVICE AND MAINTENANCE CONTACTED.

Source: SDR O84A2014082700149 · FAA SDRS
O · 2011-08-08 Matched by certificate designator
N830SF · ATA 7200

NR 1 ENGINE WAS LOW. TROUBLESHOT AND FOUND NR 1 OVERSPEED VALVE BYPASSING AIR. PART HAD BEEN INSTALLED FOR 115.4 HRS SINCE O/H.

Source: SDR O842011F00000 · FAA SDRS
O · 2010-07-28 Matched by certificate designator
N880SF · ATA 2435

GENERATOR WOULD NOT GO ON-LINE AFTER ENGINE START FOR RETURN FLIGHT BACK TO HOME BASE FROM HELIPAD AFTER PATIENT DROP-OFF.

Source: SDR O842010F00000 · FAA SDRS
O · 2009-11-18 Matched by certificate designator
N870SF · ATA 7321

COMPONENT HAS A HISTORY OF CAUSING ENG TO MOMENTARILY DECELERATE AS THROTTLE IS ADVANCED PAST THE IDLE STOP TO FLIGHT. DECELERATION CAN BE OVERCOME BY CONTINUING TO ADVANCE THROTTLE THROUGH THE DECELERATION. ONCE THROUGH DECELERATION A MAXIMUM OF ONLY 90 PERCENT OF MAIN ROTOR RPM COULD BE ACHIEVED. ALL ENGINE INDICATING INSTRUMENTS ARE WITH IN LIMITS AT FULL OPEN THROTTLE AS WELL AS AT IDLE ABOVE AND BELOW IDLE STOP.

Source: SDR 2009FA0000961 · FAA SDRS
K · 2009-10-22 Matched by certificate designator
N880SF · ATA 2913

2 BOLTS HOLDING THE BACK PUMP COVER ON, SHEARED AND ALLOWED ALL OF THE FLUID IN THE SYSTEM TO BE PUMPED OVERBOARD CAUSING A LOSS OF THE NR 1 HYD SYS. (K)

Source: SDR O842009F00000 · FAA SDRS
O · 2007-04-26 Matched by certificate designator
N880SF · ATA 6510

FWD TAIL ROTOR HANGER BEARING FAILED. SAFETY STRAP WAS THE ONLY THING HOLDING DRIVESHAFT IN PLACE. PILOT AND CREW NOTICED A MOMENTARY KNOCKING NOISE AFTER NR 1 ENGINE AT IDLE ONLY. CONTACTED BELL PRODUCT SUPPORT AND REPLACED HANGER BEARING ASSY. AFTER INSPECTION.

Source: SDR O84A115223 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N140SFEUROCOPTER DEUTSCHLAND GMBH MBB-BK 117 C-22010Valid RegistrationMatched by certificate designator
N140SFEUROCOPTER DEUTSCHLAND GMBH MBB-BK 117 C-22010Valid RegistrationOperator named in NTSB report
N240SFEUROCOPTER DEUTSCHLAND GMBH MBB-BK 117 C-22010Valid RegistrationMatched by certificate designator
N340SFEUROCOPTER DEUTSCHLAND GMBH MBB-BK 117 C-22010Valid RegistrationMatched by certificate designator
N440SFEUROCOPTER DEUTSCHLAND GMBH MBB-BK 117 C-22011Valid RegistrationMatched by certificate designator
N880SFBELL 230Valid RegistrationOperator named in NTSB report