N346FX

EMBRAER S A EMB-505 · 2012 · Valid Registration

Registered owner: FLEXJET LLC, OH (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
FLEXJET, LLC (J7SA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

B · 2026-04-08 Matched by certificate designator
ATA 3100

DIVERTED TO KMRY DUE TO AN ELECTRICAL BURNING SMELL IN THE CABIN. DURING CRUISE, THE PIC NOTED A RED X APPEAR OVER COM2 WHICH THEN EXTINGUISHED AND REAPPEARED MULTIPLE TIMES SHORTLY THEREAFTER. THE CREW OBSERVED SMOKE EMANATING FROM THE GLARESHIELD PROMPTING THEM TO DON THEIR OXYGEN MASKS. AN EMERGENCY WAS DECLARED AND THE AIRCRAFT LANDED WITHOUT INCIDENT. REPLACED GIA 2 IAW EMB 505 AMM 31-41-05. ALL FOLLOW-ON CHECKS PASSED.

Source: SDR J7SA2026041300478 · FAA SDRS
J · 2024-06-08 Matched by certificate designator
ATA 2750

DIVERTED DUE TO FLAP FAIL CAS DURING APPROACH WITH GEAR DOWN AT 1500FT AGL. CREW PERFORMED GO AROUND, RAN QRH, AND LANDED WITHOUT INCIDENT AT KAUS. REPLACED THE FCE 1 IAW EMB 505 AMM 27-03-01. RIG AND OPS CHECKS GOOD.

Source: SDR J7SA2024070300408 · FAA SDRS
J · 2024-06-06 Matched by certificate designator
ATA 2760

CREW RECEIVED FLAP FAIL, SWPS FAULT, PTRIM BKP FAIL, AND SPOILER FAULT ON POWER UP AND PERFORMED TWO UNSUCCESSFUL RESETS. REPLACED # 1 FCE IAW PH300 AMM 27-03-01. RIGGED AND OPS TESTED WITH NO DEFECTS FOUND.

Source: SDR J7SA2024070100406 · FAA SDRS
J · 2023-08-06 Matched by certificate designator
ATA 2700

ON DESCENT, SWPS FAIL AND PTRIM BKP FAIL CAS ILLUMINATED. CREW RAN QRH, DETERMINED THIS WAS A TRUE FLAP FAILURE, DECLARED EMERGENCY WITH ATC, NOTIFIED PAX, AND LANDED WITHOUT INCIDENT AT KRAP. TROUBLESHOT ISSUE TO FCE # 1. REPLACED FCE #1 IAW EMB P300 AMM 27-50-00 AND 27-03-01. PERFORMED RIGGING AND OPS CHECKS WITH NO DEFECTS NOTED.

Source: SDR J7SA2023081000369 · FAA SDRS
J O · 2022-01-18 Matched by certificate designator
ATA 3600

AIR TURN BACK DUE TO BLEED 1 OFF AND BLEED 1 FAIL CAS. RAN QRH, TURNED BLEED 1 SWITCH OFF FOR 60 SECONDS. DURING 60 SECOND PERIOD, BLEED 2 OFF AND BLEED 2 FAIL CAS ILLUMINATED. PERFORMED EMERGENCY DESCENT; DECLARED EMERGENCY; MANUAL PAX MASK DEPLOYMENT. CABIN ALTITUDE SEEN AT 19,000'. AT 20,000’ RE-PERFORMED QRH AND ALL BLEED FAULTS CLEARED. AIRCRAFT LANDED SAFELY AT KNEW. REPLACED RH PRECOOLER DUE TO BROKEN INTERNAL FIN. COMPLETED SL505-36-0003 REV 2. OPS AND LEAK CHECK GOOD IAW PH 300 AMM 36-11-05/400 AND SL505-36-0003 REV 2.

Source: SDR J7SA2022012600308 · FAA SDRS
F · 2021-11-14 Matched by certificate designator
ATA 2131

DIVERTED DUE TO CABIN ALTITUDE PRESSURIZATION INCREASING AT A RATE OF 800FT PER MINUTE. THE CREW IMMEDIATELY INSTRUCTED ATC THEY NEEDED TO DESCEND. THE PRESSURIZATION RATE WAS NOT DECREASING DURING DESCENT, CAUSING THE CREW TO DECLARE AN EMERGENCY. THE CABIN ALTITUDE WENT ABOVE 10,000FT AND THE AIRCRAFT WENT INTO EMERGENCY DESCENT. ONCE THEY DESCENDED TO 15,000FT THE CABIN RATE BEGAN DECREASING TO THE PROPER PRESSURIZATION. AIRCRAFT LANDED WITHOUT INCIDENT AT KJAX. REPLACED PRESSURE RELIEF VALVE WITH A NEW GASKET IAW PHENOM 300 AMM 21-31-04/400. OPS, PRESSURIZATION, AND LEAK CHECK GOOD. P/N 103918-2; S/N 13918-00622.

Source: SDR 2021FA0000327 · FAA SDRS
J · 2021-10-24 Matched by certificate designator
ATA 2720

VENTRAL RUDDER FAIL CAS ON SHORT FINAL IN HEAVY CROSS WIND CONDITIONS. DURING POST FLIGHT, FOUND VENTRAL RUDDER FULLY DEFLECTED AND FROZE TO THE LEFT. PERFORMED VISUAL INSPECTION OF AIRCRAFT, NO DAMAGE NOTED. TROUBLESHOT IAW FIM 22-11-00. PERFORMED VENTRAL RUDDER SERVICE OPERATIONAL CHECK THREE TIMES AS DIRECTED BY FIM IAW AMM 27-26-01. NO FAULTS FOUND. INSPECTED VENTRAL RUDDER SURFACE DRIVE MECHANISM, LINKAGE CABLES, AND STOPS—NO DEFECTS NOTED. VENTRAL RUDDER SURFACE OPS CHECK GOOD IAW AMM 27-26-01. PERFORMED CMC DOWNLOAD FOR FURTHER REVIEW.

Source: SDR J7SA2021102600299 · FAA SDRS
J · 2017-12-26 Matched by certificate designator
ATA 3240

BRAKES FAILED CAS MESSAGE ON LANDING. MAIN BRAKES DID NOT WORK. BOTH MAIN TIRES HAD FLAT SPOTTED. R & R THE BRAKE CONTROL UNIT AND BOTH MAIN WHEEL AND TIRE ASSYS. OPS CHECKED GOOD.

Source: SDR DJFA20171226001 · FAA SDRS
G J S · 2014-09-28 Matched by certificate designator
ATA 2740

PITCH TRIM NORMAL FAIL CAS (MSG) COMES ON IN FLIGHT. REMOVED PITCH TRIM ACTUATOR P/N 467500-1003 S/N 0038 AND INSTALLED REPAIRED ACTUATOR P/N 467500-1003 S/N 0047. OPS CHECKED GOOD.

Source: SDR DJFA20140928001 · FAA SDRS
J · 2014-06-23 Matched by certificate designator
ATA 2740

PTRIM BKP FAIL CAS MESSAGE. REMOVED AND REPLACED THE PITCH TRIM ACTUATOR WITH REPAIRED UNIT. REMOVED SN 0047 AND INSTALLED SN 0038.

Source: SDR DJFA201042600001 · FAA SDRS