N37408

BOEING 737-924 · 2001 · Valid Registration

Registered owner: UNITED AIRLINES INC, IL (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
UNITED AIRLINES INCOperator2016-08-17 – 2016-08-17Operator named in NTSB report
UNITED AIRLINES, INC. (CALA)Operator2016-08-17 – 2016-08-17Operator named in NTSB report

Accident & incident history

Acc · 2016-08-17 Operator named in NTSB report
BOEING 737 924 Serious injury Part 121UNITED AIRLINES, INC.
Source: NTSB case DCA16CA214

Maintenance disclosures

N · 2026-06-24 Matched by certificate designator
ATA 2611

FLIGHT ATTENDANT CALL LIGHT ILLUMINATED RANDOMLY 3 TIMES THEN FWD LAV SMOKE DETECTOR ALARM SOUNDED FOR APPROXIMATELY 2 SECONDS IMMEDIATELY AFTER. NO EVIDENCE OF SMOKE/FIRE/FUMES PRESENT. PERFORMED LAV SMOKE TEST. SYSTEM OPERATES NORMAL REF AMM 26-14-00

Source: SDR CALA2026062517323 · FAA SDRS
O · 2026-05-13 Matched by certificate designator
ATA 3350

EMERGENCY EXIT LIGHTS DO NOT COME ON FROM ROW 22 TO ROW 26. REMOVED AND REPLACED BATTERY FOR EMERGENCY EXIT LIGHTS FOR ROWS 22 THRU 26 AS REQUIRED, REFERENCE AMM 33-51-06. OPS CHECK GOOD.

Source: SDR CALA2026051416230 · FAA SDRS
J · 2026-03-22 Matched by certificate designator
ATA 2160

ON DEPARTURE CABIN TEMP WENT TO 40C. AT FL250 WOULD NOT COOL BE LOW 35C PERFORMED PACK TEMPERATURE CONTROL - BITE PROCEDURE REF FIM 21-62 TASK 801 ON BOTH CONTROLLERS 1 & 2. OPS CHECKS PASSED, NO FAULTS FOUND ON BOTH CONTROLLERS 1 & 2.

Source: SDR CALA2026032414816 · FAA SDRS
O · 2026-01-30 Matched by certificate designator
ATA 3350

PASSENGER EMERGENCY SIGN AT 20CBA INOPERATIVE. R & R PASSENGER EMERGENCY SIGN AT 20CBA IAW AMM 33-51-00. OPS CHECKED GOOD.

Source: SDR CALA2026020113461 · FAA SDRS
L · 2025-08-06 Matched by certificate designator
ATA 3397

ASILE PATHWAY LIGHT INOP ON 14 ABC. RELAMPED NO HELP. ALL OTHER EEL LIGHTS WORK AND IS NOT AT AN OVERWING EXIT. FOUND NO VOLTAGE AT SEAT MOUNTED FLOOR LIGHT. DISCONNECTED CONNECTOR AT SEAT AT FLOOR TRACK. HAS POWER. RECONNECTED AND OPS CHECKS GOOD IAW AMM 33-51-11-960-802.

Source: SDR CALA2025080707444 · FAA SDRS
O · 2025-08-03 Matched by certificate designator
ATA 5100

STRONG ODOR OF FUEL THROUGHOUT AIRPLANE AFTER PARKING W/ APU SHUTDOWN. PORTABLE CONDITIONED GROUND AIR CART CAUSING ODOR. SHUTDOWN UNIT. STARTED APU AND RAN PACKS. ODOR CLEARED

Source: SDR CALA2025080507290 · FAA SDRS
F · 2025-06-18 Matched by certificate designator
ATA 2210

WITH A/P A ENGAGED CLIMBING PASSING FL290 AIRCAFT OSCILATING IN PITCH AXIS AGRESSIVELY CREW REPORTED WITH A/P A DISENGAGED PITCH MOVEMENT STILL EXTREMELY STIFF, LATERAL MOVEMENT NORMAL LOCKING FOR MX FERRY

Source: SDR CALA2025062005759 · FAA SDRS
B · 2025-06-16 Matched by certificate designator
ATA 2530

AIRCRAFT SMELLS OF MILDEW AND IS INC IN INTENSITY. PAX ARE UNCOM FORTABLE DEBRIEFED CREW ON ARRIVAL, CREW SAYS SMELL IS MAINLY COMING FROM MID LAV TO FWD OF CABIN UPON INVESTIGATING ODOR, FOUND FOOD IN FWD GALLEY OVEN TO BE SPOILED AND TO BE THE CAUSE OF BAD SMELL IN THE FWD CABIN. REMOVED THE CONENTS IN THE OVEN OUT OF THE AIRCRAFT AND SMELL DISSIPATED FROM CABIN. REMOVED AND REPLACED OVEN IN FWD GALLEY IN REF WITH AMM 25-34-00. OPS CHECK GOOD AT THIS TIME.

Source: SDR CALA2025061705591 · FAA SDRS
O · 2025-05-30 Matched by certificate designator
ATA 2565

DOOR 1R EMERGENCY SLIDE COMING OUT OF CASE ADJUSTED SLIDE SKIRT, SLIDE OPERATES NORMALLY REF AMM 25-66-01 ADD EMP: U189788

Source: SDR CALA2025060305206 · FAA SDRS
B · 2025-05-08 Matched by certificate designator
ATA 2120

DUE TO REPORTS OF ELECTRICAL ACRID OZONE LIKE SMELL: PLEASE GAIN ACCESS TO THE AREA UNDER THE MID LAV AND INSPECT FOR ANY SIGNS OF GREY WATER OR WASTEWATER LEAKS DUE TO REPORTS OF THE SMELL COMING FROM THE AREA BETWEEN THE MID LAV TO THE OVERWING EXITS. GAINED ACCESS AND INSPECTED AREA UNDER MID LAV NO DEFECTS NOTED AT THIS TIME

Source: SDR CALA2025051204624 · FAA SDRS
B · 2025-05-08 Matched by certificate designator
ATA 2120

DUE TO REPORTS OF ELECTRICAL ACRID OZONE LIKE SMELL: PLEASE PERFORM EMERGENCY EXIT HATCH HEATER OPERATIONAL TEST REF. AMM 21-45-00-700-801, VISUAL INSPECTION MAYBE REQUIRED TO VERIFY PROPER OPERATION, NO DAMAGE AND VERIFY NOT THE CAUSE OF SMELL. PERFORMED OPERATIONAL TEST OF THE EMERGENCY EXIT HATCHES, REF AMM 21-45-00-700-801 .. NO DAMAGE, DEFECTS OR ODOR NOTED AT THIS TIIME

Source: SDR CALA2025050904579 · FAA SDRS
B · 2025-05-08 Matched by certificate designator
ATA 2121

FOUND FAULT LIGHT AND FAN FAULT LIGHT ILLUMINATED ON LTV BIN RACK. REF LOG PAGE 4758986DUE TO A/C HISTORY SLIGHT ELECTRICAL SMELL IN COCKPIT AND CABIN LOG PAGE 4758986 UNABLE TO RESET LTV BIN RACK FAULT LIGHTS, RECOMMENDED ACTIONS R&R LTV BIN RACK PN N23501-105 / R&R FAN ASSEMBLY PN N92002-109. UAL MX MONITORED THE LTV SYSTEM AND REPORTED MULTIPLE TIMES FAULT LIGHTS COME ON LOCKED BY TOMC APPLIED NEF 4410U PULL AND COLLARED IFE SYSTEM. IFE AC POWER 1 I FE AC POWER 2 IFE DC CONTROL. INSUFFICENT TIME TO R&R LTV BIN RA CK AND LTV FAN ASSEMBLY. SYSTEM DEACTIVATED PLACING SYSTEM ON NE F 4410U, DUE TO TECHNICAL ISSUES WITH COORDINATED WITH TOMC THE ITEM COULD NOT GET DEFFERED DUE TO 4410U ITEM NEF NUMBER INVALID . R&R LTV BIN RACK PN N23501-105 / R&R FAN ASSEMBLY PN N92002-10 9. SHOULD BE WORKED 21:00 IAH LOCAL TIME THALES THIRD SHIFT THALES LTV SYSTEM CAN BE DEACTIVATED AND PLACED ON NEF ALL NEF STEPS HAVE BEEN COMPLETED UNLOCKED BY TOMC PLACING ON MEL 4410U. SYSTEM LOCKED OUT BY THALES NOC MEL 4410U APPROVED BY TOMC MEL 4410U DEFERRAL REJECTED BY TOMC. ITEM NEEDS TO BE REPAIRED AND ENSURED THAT THERE IS NO ELEC SMELL. THALES - RACK PN N23501-105 AND FAN FAULT PN N92002-109 WILL NEED TO BE REPLACED R&R FAN ASSEMBLY IAW AMM 44-20-18 & BINR&R FAN FAULT SENSING ASSEMBLY IAW AMM 44-20-18-020-801. OPS CHECK GOOD. NO FAULTS AFTER LTV SYSTEM RUNNING FOR SEVERAL HOURS.

Source: SDR CALA2025051204621 · FAA SDRS
B · 2025-05-07 Matched by certificate designator
ATA 2497

SLIGHT ELECTRICAL SMELL IN COCKPIT AND CABIN LOCKED BY TOMC CONFIRMED SMELL COMING FROM COCKPIT AIR VENTS, NO SMELL COMIMG FROM FORWARD CARGO COMP, E&E FORWARD OR AFT. WHILE RUNING PACKS SMELL INTENSIFIES SPECIALLY PCK #1. CHECKED APU OIL SERVICE LEVEL AND CHECKED APU FOR EXTERNAL OIL LEAKS NONE FOUND. UPON ENTRY INTO THE CABIN ODOR WAS PRESENT IN 1ST CLASS AND OVERWING EXITS HEAVIEST . STARTED APU RAN BOTH PACKS AND AFTER SEVERAL MINS ODOR DISSAPATED . SHUT DOWN THE APU AND CLOSED AIRCRAFT DOOR RETURNED TO AIRCRACT AN HOUR LATER AND ODOR RETURNED . SUSPECT ODOR IS FROM INSIDE THE CABIN, FOUND FAULT LIGHT AND FAN FAULT LIGHT ILLUMINATED ON LTV BIN RACK PLACING ON NEF REF LOG PAGE 4766031 REMOVED AND INSTALLED ALL CEILING PANELS NO DEFECTS NOTED IN WIRING AND LRUS LOCATED IN OVEFHEAD, CKED ALL ALL SEAT BOXS AND POWER OUTLETS NO DEFECTS NOTED; REPLACED HEPA FILTERS NO DEFECTS NOTED AND SPRAYED DEODERIZED IN THE AREA AS PRECAUTIONARY. INSPECTED UNDER FWD AND AFT LAVS NO DEFECTS NOTED. ALSO UNSED INFRARED TEMP GUN TO DECTECT ANY OVERHEATING IN IFE LRUS AND OVERHEAD LRUS NO DEFECTS NOTED RAN BOTH PACS FOR 3+ HRS SMELL DISAPATES WITHIN 30 MINS

Source: SDR CALA2025050904575 · FAA SDRS
B · 2025-05-06 Matched by certificate designator
ATA 2120

WHEN TURNING ON BOTH PACK WE HEAR LOW RUMBLE AND SMELL SOMETHING ODD. DUCT PRSR DROPS SIGNIFIC RESECURED FLIGHT DECK AIR DISTRIBUTION SYSTEM MUFFLER/DUCT SLEEVE LOCATED AT DISTRIBUTION BAY REF. AMM 21-22-05-400-801, OPS CHECK GOOD, NO FURTHER RUMBLE OR SMELL NOTED.

Source: SDR CALA2025050704516 · FAA SDRS
B · 2025-05-06 Matched by certificate designator
ATA 2121

AIRCRAFT HAS BURNING ELECTRICAL SMELL THROUGH OUT THE CABIN. DEBRIEFED CREW AND CONFIRMED ELECTRICAL SMELL THRU GASPERS IN AFT CABIN WITH PACKS OFF AND RECIRC FANS ON. SUGGEST REPLACING BOTH LT & RT RECIRCULATION FANS & ALSO BOTH CABIN FILTERS WITH NEW UNITS. .AMM TASK 21-25-02-000-801 & TASK 21-25-01-000-801. R & R LT RECIRC FAN & FILTER REF AMM 25-52-17. R & R RT RECIRC FAN IAW AMM 21-25-02-400-801. OPS CHECK GOOD. R & R BOTH RECIRC FILTERS IAW AMM 21-25-01-400-801. RAN BOTH RECIRC FANS WITH PACKS ON AND WITH PACKS OFF. NO ELECTRICAL BURNING SMELL NOTED.

Source: SDR CALA2025050804551 · FAA SDRS
O · 2025-05-04 Matched by certificate designator
ATA 3350

R/H AFT EXTERIOR OVERWING EMERGENCY EXIT DOOR EMERGENCY LIGHT INOP. SUPPORT TASK NSA EMX NR 00001 REVIEWED SDR INFORMATION REMOVED AND REPLACED FUSE ON M1671 BATTERY POWER SUPPLY IAW B737NG AMM 33-51-06-960-804 AND B737NG WDM 33-51-13. EMERGENCY EXIT LIGHT OPERATIONAL CHECKED GOOD IAW B737NG AMM 33-51-00-720-801. DATA WAS TRANSCRIBED FOR NSA EMX N/R 00001.

Source: SDR CALA2025050504454 · FAA SDRS
O · 2025-05-03 Matched by certificate designator
ATA 5340

STATION 663 BULKHEAD VAPOR BARRIER UPPER ATTACH ANGLE IS CRACKED AT APPROXIMATELY RBL 9.0. SUPPORT TASK NSA EMX N/R 00064. REVIEWED ESFR INFORMATION. REPAIR STA. 663 BULKHEAD VAPOR BARRIER UPPER ATTACH ANGLE AT RBL 9.0 IAW SRM 57-10-10-2R-5 AND ACCOMPLISHED FUEL LEAK CH ECK IAW AMM 28-11-0, LEAK CHECK GOOD, F REPAIRED STA. 663 BULKHEAD VAPOR BARRIER UPPER ATTACH ANGLE AT RBL 9.0 IAW SRM 57-10-10-2R-5 AND ACCOMPLISHED FUEL LEAK CHECK IAW B737-900 AMM 28-11-00, LEAK CHECK GOOD,

Source: SDR CALA2025050504451 · FAA SDRS
O · 2025-05-01 Matched by certificate designator
ATA 5310

SHEAR FITTING AT STATION 540 AND RBL 40.87 IS CRACKED. SUPPORT TASK NSA EMX N/R 00094. REMOVED AND REPLACED SHEAR FITTING AT STA. 540 RBL 40.87 IAW B737-900 SRM 51-40-02 AND BAC DWG. 111A2000 REV. ORIGINAL,

Source: SDR CALA2025050504445 · FAA SDRS
O · 2025-05-01 Matched by certificate designator
ATA 5310

B737-57-4-1262 SHEAR FITTING AT STATION 540 AND RBL 32.40 IS CRACKED. REMOVED AND REPLACED SHEAR FITTING AT STA. 540 RBL 32.40 IAW B737-900 SRM 51-40-02 AND BAC DWG. 111A2000 REV. ORIGINAL.

Source: SDR CALA2025050504446 · FAA SDRS
O · 2025-04-06 Matched by certificate designator
ATA 2560

DOOR 1L ESCAPE SLIDE FLAP DRAGS ON FLOOR WHEN ARMED. REF AMM 25-66-01-400 FOR ADJUSTING AN EXCESS OF GIRT MATERIAL ON 1L SLIDE

Source: SDR CALA2025040803633 · FAA SDRS
L · 2025-02-11 Matched by certificate designator
ATA 3350

EMERGENCY LIGHTS INOP FWD GALLEY. REMOVED AND REPLACED BATTERY PACK ON FWD GALLEY PER AMM TASK 33-51-06-960-805. PERFORMED OPS CHECK, ALL GOOD.

Source: SDR CALA2025021302313 · FAA SDRS
O · 2025-01-10 Matched by certificate designator
ATA 3350

FA, REPORTS BROKEN EMERGENCY LIGHT LAST ROW OF SEATS ROW 39 SEAT C EMERGENCY LIGHT MODUAL BRACKET BROKEN. ALL OTHER EMERGENCY LIGHTS OPS NORMAL. OK TO CONTINUE... MEL 3319E APPROVED BY TOMC SECURED MODUAL UNDER SEAT, NO RISK TO PAX. ITEM PLACED ON MEL. OK TO CONTINUE... EMERGENCY LIGHT AND HOUSING GOOD. NEEDS BUMPER ENDBAY. PART NIS AT MSY. UPDATED PARTS LIST. R&R BUMPER END CAP IAW AMM 25-22-55 AND OPS CHECK EMERGANCY LIGHT IAW AMM 33-51-00-710-801 OPS CHECK GOOD OK FOR SERVICE.

Source: SDR CALA2025011401895 · FAA SDRS
L · 2024-11-17 Matched by certificate designator
ATA 3350

EMERGENCY AILSE LIGHT INOP AT ROWS 32DEF TO 35DEF. REF MM 33-51-06. REMOVED AND REPLACED BATTERY PACK M1899. OPS CHK GOOD.

Source: SDR CALA2024111901187 · FAA SDRS
J · 2024-10-11 Matched by certificate designator
ATA 2133

AUTO FAIL PACK CONTROL CW WITH MEL 2114B. PULL (OPEN) AND SAFETY PRESSURIZATION CONTROL-AUTO 2 CIRCUIT BREAKER ON P6-4 PANEL. MEL 2114B APPROVED. FOUND CODE 068 OFV LRU FAIL. DDP CW MEL 2114B. *DM* SUGGEST FIM 21-31 TASK 802, SEE M/L FOR OUTFLOW VALVE V48, OR OUTFLOW VALVE GASKET, AS NEEDED. REF ELB LP 9537130 AND 9531980 REMOVED AND REPLACED THE OUTFLOW VALVE AND THE NO.1 AND NO.2 CABIN PRESSURE CONTROLLERS REF AMM 21-31-03-400-801, 21-31-00-710-801 TEST PASSED AND AMM 21-31-02 TEST PASSED WORK ACCOMPLISHED BY V900455

Source: SDR CALA2024101400830 · FAA SDRS
O · 2024-10-05 Matched by certificate designator
ATA 5330

CORROSION VACCUME WASTE TANK PAN ASSY INNER SKIN AT LOWER OF DRAIN AND THE AFT LOWER CORNER REF AAR N/R 9909822 REMOVED VACUUM WASTE TANK PAN ASSY AND INSTALLED NEW VACUUM WAST E TANK PAN ASSY P/N 146A7401-21 AS PER SRM 51-40-02-0G-0 AND BOE ING DWG 146A7400 SHEET 34 AND 417A8650 SHEET 1

Source: SDR CALA2024100702593 · FAA SDRS
O · 2024-10-04 Matched by certificate designator
ATA 5310

REF EA 5310-08195 OP001 CRACK FOUND ON SECOND LOWER FASTNERB AT L/H NO.3 WINDOW FRAME REF AAR N/R 9909580 ACCOMPLISHED L/H SIDE NO.3 WINDOW FRAME POST PERMANENT REPAIR PATTERN PERMANENT REPAIR INSTALLATION I.A.W EA 5310-08195 REV ORIG OP003 WHICH CONSIST ON L/H NO.3 WORK ACCOMPLISHED BY V936290 WINDOW FRAME INSPECTION COLD WORKING AND FREEZE PLUGE INSTALL FRAME CUTTING INTERNAL DOUBLER INSTALL AND STRAIGHT FASTNER

Source: SDR CALA2024100702586 · FAA SDRS
O · 2024-10-04 Matched by certificate designator
ATA 5330

INITIATE DIP PER ECRA 5331-03128 STEP 2, A/C 0408, FUSELAGE SKIN STA 847 ? 867, STR 24L ? 26L INTERIM REPAIR. BETWEEN STA 847 - 867, STR 24L - 26L ON AIRCRAFT N37408 IN 5331-03128. ACCORDANCE WITH PART 2 OF THE LATEST REVISION OF ECRA AFTER THE ACCUMULATION OF 49,900 TOTAL AIRCRAFT FLIGHT CYCLES, BUT BEFORE 50,000, PERFORM AN INSPECTION OF THE FUSELAGE SKIN CORROSION WAS FOUND AT THE VACUUM WASTE SKIN CUTOUT ON SKIN PANE TOMC-APPROVAL FROM SC1ELBYC COMMENT L (P/N 146A3231-14) OUTER SURFACE AT STA 847. PLACED ON DIP TO A FTER THE ACCUMULATION OF 49,900 TOTAL AIRCRAFT FLIGHT CYCLES, BU T BEFORE 50,000, PERFORM AN INSP. OF THE FUSELAGE SKIN BETWEEN S TA 847 ? 867, STR 24L ? 26L ON AIRCRAFT N37408 IN ACCORDANCE WIT H PART 2 OF THE LATEST REVISION OF ECRA 5331-03128 QC RECORDS UPDATE QC REVIEW T/A: >49,900<50,000 TAFC

Source: SDR CALA2024100702594 · FAA SDRS
O · 2024-10-04 Matched by certificate designator
ATA 5310

REF EA 5310-08195 OP002 CRACK FOUND ON SECOND LOWER FASTNER AT R/ H NO.3 WINDOW FRAME REF AAR N/R 9909581 ACCOMPLISHED R/H SIDE NO.3 WINDOW FRAME POST PERMANENT REPAIR. EA 5310-08195 REV ORIG OP004 WHICH CONSIST ON R/H NO.3 WINDOW FRAME INSP COLD WORKING AND FREEZE PLUG INSTALLATION AND FRAME STRAIGHT FASTNER PATTERN PERMANENT REPAIR INSTALLATION

Source: SDR CALA2024100702589 · FAA SDRS
O · 2024-10-03 Matched by certificate designator
ATA 5313

PER EC/RA 5360-01873 PART 1, STEP 3. INITIATE A NEW DIP LOGPAGE FOR THE INTERIM REPAIR. AT FUSELAGE STRINGER 25L, STA 807 AND 847. FUSELAGE STRINGER 25L REPAIR BETWEEN STA 807 & 847 ON AIRCRAFT 5360-01873. N37408 IN ACCORDANCE WITH PART 2 OF THE LATEST REVISION OF ECRA AFTER JUNE 30, 2026, BUT BEFORE JULY 30, 2026, PLANNING TO CONTACT ENGINEERING FOR THE INSPECTION REQUIREMENTS OF THE AFTER JUNE 30, 2026, BUT BEFORE JULY 30, 2026, PLANNING TO TOMC-APPROVAL FROM SC1ELBYC COMMENT CONTACT ENGINEERING FOR THE INSPECTION REQUIREMENTS OF THE FUSELAGE STRINGER 25L REPAIR BETWEEN STA 807 & 847 ON AIRCRAFT N37408 IN ACCORDANCE WITH PART 2 OF THE LATEST REVISION OF ECRA 5360-01873.REF LP 9445872, QC RECORDS UPDATE RECORDS UPDATE QC REVIEW T/A: PLN/ENG >30JUN26<30JUL26.....KNB REF LP 9445872

Source: SDR CALA2024100702567 · FAA SDRS
O · 2024-10-03 Matched by certificate designator
ATA 5313

PER EC/RA 5360-01873 PART 1, STEP 2. INITIATE A NEW DIP LOGPAGE FOR THE INTERIM REPAIR. AT FUSELAGE STRINGER 25L, STA 807 AND 847. 847 ON AIRCRAFT N37408 IN ACCORDANCE WITH PART 2 OF THE LATEST REVISION OF ECRA 5360-01873. AFTER AUGUST 30, 2026, BUT BEFORE SEPTEMBER 30, 2026, PERFORM AN INSPECTION OF THE FUSELAGE STRINGER 25L REPAIR BETWEEN STA 807 & AFTER AUGUST 30, 2026, BUT BEFORE SEPTEMBER 30, 2026, PERFORM AN TOMC-APPROVAL FROM SC1ELBYC COMMENT INSPECTION OF THE FUSELAGE STRINGER 25L REPAIR BETWEEN STA 807 & 847 ON AIRCRAFT N37408 IN ACCORDANCE WITH PART 2 OF THE LATEST REVISION OF ECRA 5360-01873.

Source: SDR CALA2024100702566 · FAA SDRS
O · 2024-10-03 Matched by certificate designator
ATA 5330

REF ELB LP 5384043 PERFORM PART 3 OF ECRA 5370-01085 REF AAR N/R 9909483 PERFORMED CAT B REPAIR TO DAMAGE FUSELAGE SKIN I.A.W ECRA 5331-03126 PART 1 PARA 1 BETWEEN ST907 TO 947 AFT WATER SERVICE AREA REVISED LP 5384043 AND DIP MADE ON LP 9446226 WORK ACCOMPLISHED BY 936290 INSP C/W

Source: SDR CALA2024100702569 · FAA SDRS
L · 2024-09-27 Matched by certificate designator
ATA 3350

FOUND SEVERAL EMERGENCY LIGHTS INOP IN THE PASSENGER CABIN. REMOVED AND REPLACED THE EMERGENCY LIGHT POWER SUPPLY AND BATTERY PACK M1690 INSTALLATION TEST NORMAL REF AMM 33-51-06-960 AND 33-51-06-960-805.

Source: SDR CALA2024093002525 · FAA SDRS
L · 2023-12-02 Matched by certificate designator
ATA 3350

EMERGENCY LIGHTING SYSTEM OPERATIONAL CHECK {B737-33-3-0235} - DOOR 1L EMERGENCY ESCAPE SLIDE LIGHT INOP REPLACED DOOR 1L EMERGENCY ESCAPE SLIDE LIGHT WITH NEW IAW AMM TASK 33-51-04-960-801, OPS CHECKED OKAY IDT C/W FOR 1L ESCAPE SLIDE LIGHT REF GMM 09-10-05

Source: SDR CALA2023120403535 · FAA SDRS
O · 2023-06-14 Matched by certificate designator
ATA 5400

PILOT REPORTS PNL MISSING FROM #2 ENGINE. ADDED PHOTO REMOVED AND REPLACED #2 ENGINE LEFT HAND COWLING IDG ACCESS DOOR ASSY PER IPC 71-11-02 DOOR OPS CHKS NORMAL MANUAL REFER TASK 71-11-04/401 AND 71-11-04-820-802-FOO

Source: SDR CALA2023061601891 · FAA SDRS
O · 2022-12-07 Matched by certificate designator
ATA 3100

REMOVAL AND REPLACEMENT OF OPTICAL DISK IN DFDAU - WOULD NOT TEST PER OP 7. R & R DFDAU OPTICAL DISK .

Source: SDR CALA2022120703326 · FAA SDRS
O · 2022-05-20 Matched by certificate designator
ATA 5710

CTR WING VERTICAL PRESSURE WEB CRACKED ON L/H SIDE @ APPROX. LBL INSPECTION THRESHOLD 56,000 FLT CYCLES. REPAIRED CENTER WING VERTICAL PRESSURE WEB PER SRM 57-10-10.DEFE RED TO PEFORM AN INSP PER SAME SRM STEP6 SUB STEP B.56,000 FLT C VERTICAL PRESSURE DECK REPAIR FROM LBL 24.92 TO LBL 45.64. REPAI R SIZE IS 22"X"8. FABRICATED PER TABLE 202. REFERENCE TABLE 205 FOR INSPECTION REPAIR. PERFORM A LFEC AND HFEC REPEAT INSPECTION AT 36,000 REQUIREMENTS. INSPECTION THRESHOLD OF 56,000 FLIGHT CYCLES AFTER FLIGHT CYCLES PER TABLE 205. PERFORMED WING CENTER SECTION REAR SPAR VERTICAL PRESSURE DECK WEB REPAIR PER SRM 57-10-10-2R-3, REPAIR 3, ALTERNATIVE 2. PARTS DIP 57-DIP NEEDS MANUAL REF AND WHICH REPAIR REPAIRED VERTICAL PRESSURE DECK PER SRM 57-10-10-2R REPAIR 3 ALT ERNATIVE 2. REPAIR PARTS FABRICATED PER TABLE 202. REFERENCE TAB LE 205 FOR CATEGORY B REPAIR INSPECTION REQUIREMENTS. LOG PAGE NOT REQUIRE RII INSPECTION 000 FLT CYCLES AFTER REPAIR INSTALLATION, HFEC AND LFEC INSPECTI BLE 206/REPAIR 3 AND FIGURE 209/REPAIR 3 FOR CATEGORY B REPAIR I 6,000 FLT CYCLES AFTER REPAIR INSTALLATION, HFEC AND LFEC INSPEC 9809108 FOR WORK PERFORMED BY. ON AFTER 36,000 FLT CYCLES INTERVAL. REFERENCE FLEET CYCLE N/R 9 N SPECTION REQUIREMENTS. PLACE ON DIP FOR INSPECTION THRESHOLD 5 TION AFTER 36,000 FLT CYCLES INTERVAL. REFERENCE FLEET CYCLE N/R 809108 FOR WORK PERFORMED BY. REPAIRED VERTICAL PRESSURE DECK PER SRM 57-10-10-2R REPAIR 3 ALT ERNATIVE 3. REPAIR PARTS FABRICATED PER TABLE 203. REFEREN

Source: SDR CALA2022052001301 · FAA SDRS
O · 2022-05-19 Matched by certificate designator
ATA 5311

INTERIM REPAIR TO R1 WINDOW FRAME WAS ACCOMPLISHED PER ECRA 5311-02811 PART 1, INSPECTION REQUIREMENTS ARE STATED IN PART 2. REFERENCE FLEET CYCLE NON-ROUTINE 9809923. OR BEFORE THE AIRCRAFT REACHES 50,000 TOTAL AIRCRAFT FLIGHT PART 2, SECTION A AT INTERVALS NOT TO EXCEED 18,000 FLIGHT CYCLES. ACCOMPLISH REPETITIVE INSPECTIONS PER ECRA 5311-02811 CYCLES THEREAFTER. INITIATE A DTA DIP FOR THE R1 WINDOW FRAME REPAIR TO ACCOMPLISH AN INITIAL INSPECTION PER ECRA 5311-02811 PART 2, SECTION A ON APPROVAL, INTERIM REPAIR TO R1 WINDOW FRAME WAS ACCOMPLISHED PER TOMC-APPROVAL FROM SC1ELBYC COMMENT ECRA 5311-02811 PART 1.INITIATE A DTA DIP FOR THE R1 WINDOW FRA ME REPAIR TO ACCOMPLISH AN INITIAL INSPECTION PER PART 2, SECTIO N A ON OR BEFORE THE ACFT REACHES 50,000 TOTAL AIRCRAFT FLT CYCL ES. ACCOMPLISH REPETITIVE INSPECTIONS PER PART 2, SECTION A AT I NTERVALS NOT TO EXCEED 18,000 FLT CYCLES THEREAFTER. QC REVIEWED QC REVIEWED INIT: ON OR BEFORE 50,OOO TAFC INIT(-0868) WILL ITO TO RIR (-0869) RIR: INTERVALS NOT TO EXCEED 18,000 FC THEREAFTER....LN/U253409 RECORDS UPDATE

Source: SDR CALA2022052001291 · FAA SDRS
O · 2022-05-19 Matched by certificate designator
ATA 5311

INTERIM REPAIR TO L1 WINDOW FRAME WAS ACCOMPLISH PER ECRA 5311-02812 PART 1. REFERENCE FLEETCYCLE NON-ROUTINE 9809922. THE INSPECTION REQUIREMENTS PER ECRA 5311-02812 PART 1 STEP G.2. INITIATE DIP FOR PLANNING TO CONTACT ENGINEERING AFTER 43,000 TOTAL FLIGHT CYCLES BUT BEFORE 44,000 TOTAL FLIGHT CYCLES FOR APPROVED DIP FOR PLANNING TO CONTACT ENGINEERING AFTER 43,000 TOMC-APPROVAL FROM SC1ELBYC COMMENT TOTAL FLIGHT CYCLES BUT BEFORE 44,000 TOTAL FLIGHT CYCLES FOR THE INSPECTION REQUIREMENTS PER ECRA 5311-02812 PART 1 STEP G.2 L-1 WINDOW INTERIM REPAIR TOMC APPROVED : QC REVIEWED. RECORDS UPDATE TOMC APPROVED : QC REVIEWED. T/A; PLN/ENG >43,000 <44,000 TAFC....LN/U253409

Source: SDR CALA2022052001292 · FAA SDRS
O · 2022-05-14 Matched by certificate designator
ATA 5710

CTR WING VERTICAL PRESSURE WEB CRACKED ON L/H SIDE @ APPROX. LBL INSPECTION THRESHOLD 56,000 FLT CYCLES. REPAIRED CENTER WING VERTICAL PRESSURE WEB PER SRM 57-10-10.DEFE RED TO PEFORM AN INSP PER SAME SRM STEP6 SUB STEP B.56,000 FLT C VERTICAL PRESSURE DECK REPAIR FROM LBL 24.92 TO LBL 45.64. REPAI R SIZE IS 22"X"8. FABRICATED PER TABLE 202. REFERENCE TABLE 205 FOR INSPECTION REPAIR. PERFORM A LFEC AND HFEC REPEAT INSPECTION AT 36,000 REQUIREMENTS. INSPECTION THRESHOLD OF 56,000 FLIGHT CYCLES AFTER FLIGHT CYCLES PER TABLE 205. PERFORMED WING CENTER SECTION REAR SPAR VERTICAL PRESSURE DECK WEB REPAIR PER SRM 57-10-10-2R-3, REPAIR 3, ALTERNATIVE 2. PARTS DIP 57-DIP NEEDS MANUAL REF AND WHICH REPAIR REPAIRED VERTICAL PRESSURE DECK PER SRM 57-10-10-2R REPAIR 3 ALT ERNATIVE 2. REPAIR PARTS FABRICATED PER TABLE 202. REFERENCE TAB LE 205 FOR CATEGORY B REPAIR INSPECTION REQUIREMENTS. LOG PAGE NOT REQUIRE RII INSPECTION

Source: SDR CALA2022051601243 · FAA SDRS
O · 2022-05-09 Matched by certificate designator
ATA 5700

FLEET CYLCE N/R 9809108 CTR WING VERTICAL PRESSURE WEB CRACKED O N L/H 2 APPOX LBL 35.

Source: SDR CALA2022051101199 · FAA SDRS
O · 2018-06-15 Matched by certificate designator
ATA 5512

RT STAB LOWER SKIN CRACK AT STA 101.90 12" FROM REAR SPAR HAS BEEN REPAIRED IAW SRM 55-10-01 REP 11. ORIG DOUBLER HAS BEEN REMOVED AND REPLACED WITH A LARGER DOUBLER COVE RING BOTH REPAIR AREAS ( STA 92.70 + STA 101.90 ) INSTALLED.

Source: SDR CALA2018062901527 · FAA SDRS
O · 2018-06-15 Matched by certificate designator
ATA 5512

RT STAB LOWER SKIN CRACK AT STA 101.90 12" FROM REAR SPAR HAS BEEN REPAIRED IAW SRM 55-10-01 REP 11. ORIG DOUBLER HAS BEEN REMOVED AND REPLACED WITH A LARGER DOUBLER COVE RING BOTH REPAIR AREAS ( STA 92.70 + STA 101.90 ) INSTALLED.

Source: SDR CALA2018062901526 · FAA SDRS
O · 2018-02-19 Matched by certificate designator
ATA 5512

LT HORIZONTAL STAB LOWER SKIN AT STA 193.90 HAS CRACK INDICATION 3/4" INCH LONG AND 10" INCH FROM REAR SPAR. REF. EA 5510-0184 3 REV "F". REPAIRED LT HORIZONTAL STAB LO WER SKIN IAW SRM 55-10-01 REPAIR 11, SEE ALL WIPS AND TASKS FOR ALL WORK PERFORMED.

Source: SDR CALA2018022000703 · FAA SDRS
O · 2017-10-14 Matched by certificate designator
ATA 3350

RIGHT MID EMERGENCY LIGHTS INOPERATIVE. REMOVED AND REPLACED THE BATTERY PACK IAW AMM 33-51-00. OPS CHECKED GOOD.

Source: SDR CALA2017101403622 · FAA SDRS
O · 2017-07-10 Matched by certificate designator
ATA 3416

STANBY ALTIMETER STICKS DURING CLIMB AND WILL JUMP BY AS MUCH AS 600 FEET AT A TIME. FOUND ALTERNATE VIBRATOR CIRCUIT BREAKER OUT. RESET ONCE. VIBRATOR OPERATES NORMAL AND IS ACCURATE WITH ATIS BARO.

Source: SDR CALA2017071002128 · FAA SDRS
L · 2017-01-22 Matched by certificate designator
ATA 3350

EMERGENCY LIGHT’S AT ROW 22 ABC TO 26 ABC IS INOP. REMOVED AND REPLACED BATTERY PACK S/N 184763 IAW AMM 33 -51-06. OP'S CHECK GOOD IAW AMM 33-51-00 STA 727C.

Source: SDR CALA2017012200150 · FAA SDRS
K J · 2016-05-09 Matched by certificate designator
ATA 2913

FL 350 INTERMITTENT LOW PRESS ON NR 1 ENG HYD PUMP & MASTER CAUTION TO DROP TO ZERO. GOOD PRESS 3000 PSI ON A SYS THROUGHOUT TOUCHDOWN. QTY BOUNCED TO 16 AFTER LANDING. FOUND ACOUSTIC FILTER HOUSING LEAKING FOR HYD A SYS. R & R HYD A ACOUSTIC FILTER ASSEMBLY IAW AMM 29-11-27. LEAK CHECKED GOOD. DURING OPERATIONS CHECK FOUND NR 1 ENG HYD PUMP NOT PRODUCING ENOUGH PRESS. R & R NR 1 ENG HYD PUMP IAW AMM 29-11-11. OPERATIONS & LEAK CHECKED GOOD. EMER DECLARED.

Source: SDR CALA2016050900292 · FAA SDRS
N · 2015-04-07 Matched by certificate designator
ATA 2797

FLAPS 25 DEGREES TAKEOFF. FLAPS WOULD NOT RETRACT TO LESS THAN 15 DEGREES. FOUND LT FLAP POSITION TRANSMITTER CONNECTOR D400241 VIBRATED LOOSE CAUSING ERRATIC FLAP INDICATIONS. SECURED D400241 CONNECTOR IAW AMM 27-58-01 & WDM 27-52-11 PG 1 SHEET 2. OPERATIONS CHECK OF FLAP SYS NORMAL IAW AMM 27-51-00.

Source: SDR CALA2015040700258 · FAA SDRS
O · 2015-04-02 Matched by certificate designator
ATA 5313

AFT CARGO, FUSELAGE STRINGER & LONGERON S-27R HAS A 4 INCH CRACK, STATION 727+3. MARKED LINE CUT OUT DAMAGE SECTION OF KEEL CHORD BETWEEN BS 727 - 727A, RB 6.3. FABRICATED & INSTALLED REPAIR T CHORD SECTION & REPAIR ANGLES IAW ECRA 5310-06467 PARA A B & C.

Source: SDR CALA2015040200237 · FAA SDRS
O · 2015-03-24 Matched by certificate designator
ATA 5347

FASTENER HOLES COMMON TO THE SPLICE STRAP & FWD SEAT TRACK FLANGES INDICATE CRACK FWD OF STATION 727B, LBL 45.50. REPAIRED SEAT TRACK IAW ECRA 5320-02431.

Source: SDR CALA2015032500198 · FAA SDRS
O · 2015-03-24 Matched by certificate designator
ATA 5347

FASTENER HOLES COMMON TO THE SPLICE STRAP & FWD SEAT TRACK FLANGES INDICATE CRACK FWD OF STATION 727B, RBL 24.75. REPAIRED SEAT TRACK IAW ECRA 5320-02429.

Source: SDR CALA2015032500202 · FAA SDRS
O · 2015-03-24 Matched by certificate designator
ATA 5347

FASTENER HOLES COMMON TO THE SPLICE STRAP & FWD SEAT TRACK FLANGES INDICATE CRACK FWD OF STATION 727B, RBL 45.50. REPAIRED SEAT TRACK IAW ECRA 5320-02428.

Source: SDR CALA2015032500201 · FAA SDRS
O · 2015-03-24 Matched by certificate designator
ATA 5347

FASTENER HOLES COMMON TO THE SPLICE STRAP & FWD SEAT TRACK FLANGES INDICATE CRACK FWD OF STATION 727B, LBL 24.75. REPAIRED SEAT TRACK IAW ECRA 5320-02430.

Source: SDR CALA2015032500200 · FAA SDRS
O · 2015-03-18 Matched by certificate designator
ATA 5311

HFEC CRACK INDICATION ON CABIN FRAME AT STATION 500 F RT BETWEEN STRINGERS 8 & 9. REPAIRED CABIN FRAME IAW EA 5310-04716 REV I.

Source: SDR CALA2015032000187 · FAA SDRS
O · 2015-03-18 Matched by certificate designator
ATA 5311

HFEC CRACK INDICATION ON CABIN FRAME STATION 500 A RT BETWEEN STRINGERS 8 & 9. REPAIRED CABIN FRAME IAW EA 5310-04716 REV I.

Source: SDR CALA2015032000179 · FAA SDRS
O · 2015-03-18 Matched by certificate designator
ATA 5311

HFEC CRACK INDICATION ON CABIN FRAME AT STATION 400 RT BETWEEN STRINGERS 8 & 9. REPAIRED FRAME IAW EA 5310-04716 REV I.

Source: SDR CALA2015032000178 · FAA SDRS
O · 2015-03-18 Matched by certificate designator
ATA 5311

HFEC CRACK INDICATION ON CABIN FRAME STATION 480 RT BETWEEN STRINGERS 8 & 9. REPAIRED CABIN FRAME IAW EA 5310-04716 REV I.

Source: SDR CALA2015032000177 · FAA SDRS
O · 2015-03-18 Matched by certificate designator
ATA 5311

HFEC CRACK INDICATION AT STATION 500H LT BETWEEEN STRINGERS 8 & 9. REPAIRED FRAME IAW EA 5310-04716 REV I.

Source: SDR CALA2015032000176 · FAA SDRS
O · 2015-03-18 Matched by certificate designator
ATA 5311

HFEC CRACK INDICATION ON CABIN FRAME AT STATION 867 RT BETWEEN STRINGERS 8 & 9. REPAIRED CABIN FRAME IAW EA 5310-04716 REV I.

Source: SDR CALA2015032000185 · FAA SDRS
O · 2015-03-18 Matched by certificate designator
ATA 5311

HFEC CRACK INDICATION ON CABIN FRAME AT STATION 500H RT BETWEEN STRINGERS 8 & 9. REPAIRED CABIN FRAME IAW EA 5310-04716 REV I.

Source: SDR CALA2015032000184 · FAA SDRS
O · 2015-03-18 Matched by certificate designator
ATA 5311

HFEC CRACK INDICATION ON CABIN FRAME STATION 827 RT BETWEEN STRINGERS 8 & 9. REPAIRED CABIN FRAME IAW EA 5310-04716 REV I.

Source: SDR CALA2015032000183 · FAA SDRS
O · 2015-03-18 Matched by certificate designator
ATA 5311

HFEC CRACK INDICATION ON CABIN FRAME AT STATION 787 RT BETWEEN STRINGERS 8 & 9. REPAIRED CABIN FRAME IAW EA 5310-04716 REV I.

Source: SDR CALA2015032000182 · FAA SDRS
O · 2015-03-18 Matched by certificate designator
ATA 5311

HFEC CRACK INDICATION ON CABIN FRAME STATION 440 RT BETWEEN STRINGERS 8 & 9. REPAIRED FRAME IAW EA 5310-04716 REV I.

Source: SDR CALA2015032000181 · FAA SDRS
O · 2015-03-18 Matched by certificate designator
ATA 5311

HFEC CRACK INDICATION ON CABIN FRAME AT STATION 727B RT BETWEEN STRINGERS 8 & 9. REPAIRED CABIN FRAME IAW EA 5310-04716 REV I.

Source: SDR CALA2015032000180 · FAA SDRS
L · 2012-10-23 Matched by certificate designator
ATA 3397

WHILE PERFORMING EMERGENCY LIGHT CHECK, ROW 37 ABC EMERGENCY SEAT LIGHT DID NOT COME ON. FOUND EMERGENCY LIGHT SEAT HARNESS DAMAGED. R & R HARNESS IAW CMM 25-27-43. EMERGENCY LIGHTS OPS CHECKED GOOD.

Source: SDR CALA2012102300683 · FAA SDRS
O · 2012-09-27 Matched by certificate designator
ATA 5512

RT STABILIZER LOWER SKIN APPEARS TO HAVE A CRACK INDICATION AT STA 184.7 AND 26" FROM FRONT SPAR, WITH THE C-SCAN INSTALLED REPAIR DOUBLER REF SRM 55-10-01, REPAIR 11, FIG 204. INITIATED DIP CONTROL 17598 TO INSPECT REPAIR INSTALLATION AFTER 56000 FLIGHT CYCLES AND EVERY 9000 FLIGHT CYCLES THEREAFTER REF TABLE 204, QC PERFORM NDT/DV OF RT STABILIZER LWR SKIN STA 184.70,26" AFT OF FRONT SPAR AFTER 56,000 FLIGHT CYCLES AFTER REPAIR AND REPEAT EVERY 9000 FLIGHT CYC THEREAFTER IAW SRM 55-10-01. REPAIR 11, DIP CTL 017598.

Source: SDR CALA2012092800629 · FAA SDRS
O · 2010-09-09 Matched by certificate designator
ATA 5315

FLOORBEAM AT STA 986.5 RT SIDE HAS CORROSION AT FASTENER HOLE APPROX RBL 4.5 (MARKED). REMOVED DAMAGED SECTION OF FLOORBEAM, FAB'D REPAIR PIECES, TREATED, PRIMED AND INSTALLED IN REF TO SRM 53-00-51 REPAIR 1.

Source: SDR CALA2010091700427 · FAA SDRS
O · 2009-05-10 Matched by certificate designator
ATA 2497

TERMINAL BLOCK TB5060E BEHIND P6-4 PANEL SHOWS EVIDENCE OF WIRES ARCING. REMOVED AND REPLACED TERMINAL BLOCK 5060E AND TERMINAL LUGS ON WIRE NR'S W40-6120-14, W406133-14, W5901-902-10, W40-0043-8, W40- 6154-8, W40-6145-14 IAW SWPM 20-30-00 AND 20-30-11 WORK ACCOMPLISHED IAW B737-789 WDM 24-51-21 ON P6-4 PANEL. SYSTEM OPS CHECKED GOOD IAW B737-789 24-41-21 AND 24-34-00.

Source: SDR CALA2009051900256 · FAA SDRS
O · 2009-03-16 Matched by certificate designator
ATA 5320

CABIN FLOOR INTERCOSTAL IS CRACKED BETWEEN STATION 277 AND 294, LBL 0. REMOVED AND REPLACED INTERCOSTAL STATION 277 AND 294, LBL 0 REF SRM 51-40-02.

Source: SDR CALA2009031700145 · FAA SDRS
O · 2009-03-16 Matched by certificate designator
ATA 5320

CABIN FLOOR INTERCOSTAL IS CRACKED BETWEEN STATION 312 AND 328, RBL 37. REMOVED AND REPLACED INTERCOSTAL BETWEEN STATION 312 AND 328, RBL 37 REF SRM 51-40-02.

Source: SDR CALA2009031700146 · FAA SDRS
O · 2009-03-16 Matched by certificate designator
ATA 5320

CABIN FLOOR CRACKED INTERCOSTAL BETWEEN STATION 312 AND 328, LBL 45. REMOVED AND REPLACED INTERCOSTAL BETWEEN STATION 312 AND 328, LBL 45. REF SRM 51-40-02.

Source: SDR CALA2009031700144 · FAA SDRS