N4282

EUROCOPTER AS 350 B3 · 2007 · Valid Registration

Registered owner: AIR METHODS LLC, CO (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AIR METHODS LLC (QMLA)Certificate holderMatched by certificate designator
OMNIFLIGHT HELICOPTERS INCOperator2010-03-16 – 2010-03-16Operator named in NTSB report

Accident & incident history

Acc · 2010-03-16 Operator named in NTSB report
EUROCOPTER AS 350 B3 None injury Part 91OMNIFLIGHT HELICOPTERS INC
Source: NTSB case WPR10CA164

Maintenance disclosures

O · 2022-01-18 Matched by certificate designator
ATA 5302

TAIL BOOM SERVO RH BEAM (PN: 350A23-4015.24) IN THE FORM OF A CHAFE. THE CHAFE DAMAGE WAS MEASURED TO BE APPROXIMATELY 0.50” X 0.10” AND 0.015” DEEP.

Source: SDR 2022FA0000034 · FAA SDRS
O · 2022-01-18 Matched by certificate designator
ATA 5302

TAILBOOM P/N 350A23-0000-0705 S/N TB4490 SKIN DAMAGE AT APPROXIMATELY X1219 RBL 228. THE DAMAGE IS MINOR CHAFING MEASURING 0.005” AT ITS DEEPEST.

Source: SDR 2022FA0000033 · FAA SDRS
O · 2021-12-27 Matched by certificate designator
ATA 5300

DAMAGE TO THE ENGINE DECK (PN: 350A21-1239.21) IN THE FORM OF 3EA DENTS AND A CHAFE. THE CHAFE DAMAGE AREA WAS DISCOVERED TO BE NEAR THE SCUPPER DRAIN HOLE.

Source: SDR 2021FA0000426 · FAA SDRS
O · 2020-01-07 Matched by certificate designator
ATA 5311

L/H INBOARD SIDE OF AFT LOWER LEG OF THE X-FRAME HAS CHAFFING MEASURING APPROXIMATELY 0.011" DEEP AND 0.3" WIDE BY 2.4".

Source: SDR 2A6R202001104282 · FAA SDRS
E W · 2016-03-21 Matched by certificate designator
ATA 5340

THE TRANSMISSION SUPPORT FRAME, PN 350A21-1041-143, HAS CHAFING DAMAGE ON THE LOWER FLANGE FROM AN UNSECURED CABLE, PN 704A34-1302-23. PN 350A38-1040-20 ATTACHES TO PN 350A21-1041-143.

Source: SDR QMLA2016032116025 · FAA SDRS
E · 2011-05-02 Matched by certificate designator
ATA 6410

UPON APPROACH, ACFT SUSTAINED A BIRD STRIKE ON THE PILOT SIDE WIND SCREEN AND WAS PROJECTED INTO THE TAIL ROTOR DUE TO THE DOWN WASH OF THE MAIN ROTOR SYS TECH INSPECTED WINDSCREEN WITH NO DEFECTS NOTED. TAIL ROTOR BLADE AND SPIDER ASSY HAD EVIDENCE OF THE BIRD IMPACT AND WAS INSPECTED, CLEANED, AND TAP TESTED WITH NO DEFECTS NOTED. AFTER GROUND RUNS AND OPS CHECK FLIGHT THERE WERE NO DEFECTS NOTED AND ACFT WAS RETURNED TO SERVICE. ALL WORK WAS PERFORMED IAW MET 05.53.00.604.

Source: SDR RMXA383298 · FAA SDRS
J · 2011-04-28 Matched by certificate designator
ATA 3160

DURING APPROACH TO AIRPORT, ACFT INDICATED AN AMBER GOV LIGHT. DOWNLOADED VEMD FAIL 1 CODE OF 0008 AND A FAIL 2 CODE OF 0200. AFTER CONTACTING MFG REPRESENTATIVE IT WAS VERIFIED THAT THESE DISTURBANCES ARE KNOWN AS NUISANCE CODES. CONNECTOR PLUGS WERE CLEANED BEHIND VEMD, BATTERY WAS RESET AND CODES DISTINGUISHED. AFTER SEVERAL POWER CYCLES, CODES DID NOT APPEAR AND ACFT WAS RETURNED TO SERVICE WITH NO FURTHER DEFECTS NOTED. ALL WORK WAS PERFORMED IAW CUURENT SPM 20.04.01 AND MET 31.60.00.

Source: SDR RMXA383295 · FAA SDRS
J · 2011-03-05 Matched by certificate designator
ATA 6700

ACFT INDICATED AN AMBER GOV LIGHT IN FLIGHT, WITH NO ENGINE, MAIN ROTOR, OR TAIL ROTOR FLUCTUATIONS IN FLIGHT. TECH RETRIEVED AN INTERMITTENT FAILURE CODE 122 FOR THE COLLECTIVE POTENTIOMETER. WHEN THE ACFT WAS POWERED BACK UP AFTER LANDING THE AMBER GOV LIGHT EXTINGUISHED AND NO FURTHER CODES DETECTED. CHECKED RIGGING AND OPERATION OF COLLECTIVE POTENTIOMETER IAW MET 76.00.00.502, SEC 5.4 WITH NO FAULT FOUND. CONTACTED TECH REP TO VERIFY FAILURE AND IT WAS NOTED THAT THERE ARE SEVERAL OCCURRENCES WITH THIS FAILURE OUT IN THE FIELD. THERE IS A POSSIBLE EMI PROBLEM WITH THE WIRE BUNDLE DUE TO THE FACT THAT IT IS THE SAME BUNDLE THAT THE AIR-CONDITIONING WIRING IS LOCATED. WE ARE CURRENTLY WORKING WITH INTEGRATED FLIGHT SYS ON AN INSTALLATION OF AN EMI FILTER THAT GOES IN LINE ON THE CONDENSER BLOWER MOTOR. ACFT PERFORMED A GROUND RUN AND OPS CHECK FLIGHT WITH NO DEFECTS NOTED, AND RTS.

Source: SDR RMXA363942 · FAA SDRS