N434AM

BELL HELICOPTER TEXTRON CANADA 407 · 2013 · Valid Registration

Registered owner: AIR METHODS LLC, CO (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AIR METHODS LLC (QMLA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2022-11-08 Matched by certificate designator
ATA 6320

WHILE IN THE DECELERATION PHASE FOR LANDING, THE "XMSN CHIP" AND MASTER CAUTION LIGHTS ILLUMINATED. ALL OTHER INDICATIONS - TRANSMISSION PRESSURE, TEMP. WERE NORMAL. NO ABNORMAL NOISE OR VIBRATIONS NOTED. LANDING AND SHUTDOWN WERE NORMAL. INSPECTED CHIP DETECTORS, SMALL SILVER FLAKES LESS THAN 1 MM FOUND ON MGB SUMP. WHICH IS NORMAL FOR A TRANS WITH LESS THAN 100FH AS PER THE BELL MANUAL. CURRENT TRANSMISSION TIME SINCE OVERHAUL / INSTALLATION IS 78+23FH. RETAINED FLAKES FOR HISTORICAL USE. DRAINED AND RESERVICED, FILTER CHANGE, AND PERFORMED GROUND RUN.

Source: SDR QMLA2022110920073 · FAA SDRS
B · 2022-06-17 Matched by certificate designator
ATA 2100

PILOT RECEIVED A CALL FOR AN INTER HOSPITAL TRANSFER. APPROXIMATLY 6 MINUTES POST DEPARTURE FROM BASE THE FLIGHT CREW STARTED SMELLING SMOKE. A SHORT DISCUSSION TOOK PLACE BETWEEN THE CREW VERIFIYING ALL HAD SMELLED "SMOKE" AT WHICH TIME THE PILOT MADE THE DECISION TO PL @ THE LOCAL HIGHSCHOOL PARKING LOT. DURING THE APPROACH PILOT STATES THE SMELL BECAME STRONGER. ONCE ON THE GROUND THE PILOT INSTRUCTED THE MED CREW TO EVAC AND GET CLEAR OF THE AIRCRAFT. PILOT THEN STATED A PUFF OF SMOKE (VISABLE CLOUD) CLEARLY CAME FROM PILOT SIDE BLOWER MOTOR. PILOT SHUT OFF THE A/C SYSTEM/ BLOWERS & FOLLOWED SHUTDOWN PROCEDURES. PILOT STATED THE REMAINDER OF SHUTDOWN WAS NORMAL.

Source: SDR QMLA2022061720034 · FAA SDRS
N · 2014-07-30 Matched by certificate designator
ATA 3150

DURING FLIGHT TORQUE MISCOMP LIGHT ILLUMINATED, REDUCED POWER & LIGHT WENT OUT. ACFT RETURN TO BASE & LIGHT CAME ON AGAIN DURING HOVER FOR LANDING. ACFT LANDED & LIGHT REMAINED ON ALONG WITH AN ALTN DATA FAIL LIGHT. TECH REP RECOMMENDED CHECKING THE PLUGS AT THE PRIMARY & SECONDARY TRANSDUCERS. ALSO STATED IT COULD POSSIBLY BE ONE OF THE SIGNAL CONDITIONERS. THE PLUGS AT THE TRANSDUCERS WERE CLEANED & STABILENT 22 WAS APPLIED TO THE PINS. THE ACFT WAS FLOWN FOR ABOUT 20 MIN AT DIFFERENT TORQUE SETTINGS, SPEEDS & ALTITUDES. THE PROBLEM COULD NOT BE DUPLICATED. ACFT WAS RETURNED TO SERVICE.

Source: SDR QMLA2014073014095 · FAA SDRS
J · 2014-06-08 Matched by certificate designator
ATA 3150

DURING CRUISE FLIGHT THE MGT MISCOMP LIGHT ILLUMINATED. ALERTED THE CREW & ADVISED THEM THAT THEY WOULD BE ABORTING THE FLIGHT & RETURNED TO BASE. THE RFM EMER PROCEDURE STATES TO AVOID HIGH POWER SETTINGS IF POSSIBLE & LAND AS SOON AS PRACTICAL. ONCE ON THE GND MX ARRIVED TO TROUBLESHOOT THIS ISSUE. THIS ACFT REMAINS OUT OF SERVICE AT THE TIME OF THIS SUBMISSION AS MX IS WORKING WITH TO CORRECT THIS ISSUE.

Source: SDR QMLA2014060814068 · FAA SDRS
N · 2014-06-02 Matched by certificate designator
ATA 3150

THE PILOT REPORTED THAT DURING CRUISE FLIGHT THE MGT MISCOMP LIGHT ILLUMINATED. ABORTED THE FLIGHT & RETURNED TO BASE. FOUND NO FAULTS WITH THE PREVIOUS REPAIR THAT WAS REPORTED UNDER SDR QMLA2014053014060 FOR THIS SAME TYPE OF EVENT. AFTER A THOROUGH INSPECTION OF THE SYS THAT CONCLUDED WITH NO FAULTS FOUND, THE HMU CONNECTOR WAS DISCONNECTED, CLEANED & RE-INSTALLED. THIS ACFT HAS SINCE BEEN RETURNED TO SERVICE.

Source: SDR QMLA2014060214061 · FAA SDRS
J · 2014-05-30 Matched by certificate designator
ATA 7600

DURING CRUISE FLIGHT, THE PILOT REPORTED A MGT MISCOMP CAUTION LIGHT ILLUMINATE. ABORTED THE REMAINDER OF THE FLIGHT & RETURNED TO BASE. FOUND A TERMINAL BLOCK LOOSE BEHIND THE INSTRUMENT PANEL. THIS BLOCK & TERMINAL ENDS WERE SECURED & THE ACFT WAS RETURNED TO SERVICE WITH NO ADDITIONAL DEFECTS NOTED.

Source: SDR QMLA2014053014060 · FAA SDRS
J · 2014-03-12 Matched by certificate designator
ATA 7321

DURING FLIGHT FADEC DEGRADE, FADEC FAULT & RESTART ILLUMINATED.

Source: SDR QMLA2014031414025 · FAA SDRS
J · 2014-02-28 Matched by certificate designator
ATA 7321

ON DEPARTURE, THE FADEC DE GRADE LIGHT ILLUMINATED. THE PILOT RETURNED TO BASE & WHEN HE LANDED THE FADEC FAULT LIGHT ILLUMINATED. THE ACFT THEN WENT INTO MANUAL MODE & THE THROTTLE WAS UNRESPONSIVE TO INPUT. THE ENG STAYED AT 100% WHEN THE THROTTLE WAS IN IDLE POSITION. PILOT WAS ABLE TO SHUT DOWN ENG BY CLOSING THE THROTTLE TO THE OFF POSITION & STOPPING FUEL FLOW.

Source: SDR QMLA2014022814019 · FAA SDRS
J · 2014-02-13 Matched by certificate designator
ATA 7321

DURING FLT FADEC DEGRADE LIGHT & RESTART LIGHT ILLUMINATED. AFTER LANDING FADEC FAIL LIGHT ILLUMINATED, SHUT ACFT DOWN.

Source: SDR QMLA2014021314015 · FAA SDRS
J · 2000-02-18 Matched by certificate designator
ATA 6140

7486 - STL - LEFT BETA CAPTION ILLUMINATED IN FLIGHT. MAINTENANCE REPLACED LEFT BETA PRESSURE SWITCH.

Source: SDR RAIA0002008 · FAA SDRS
O · 1998-12-13 Matched by certificate designator
ATA 3416

FLT 7508 - STL - CAPTAINS ALTIMETER FLAGGED. MAINTENANCE REPLACED CAPTAINS ALTIMETER. (M)

Source: SDR RAIA981208 · FAA SDRS
E · 1998-03-05 Matched by certificate designator
ATA 6113

FLT 7486 - STL - LEFT PROPELLER SPINNER WOBBLES IN FLT. MAINTENANCE INSPECTED AND REPLACED LEFT PROPELLER SPINNER O-RING. (M)

Source: SDR RAIA980303 · FAA SDRS
N · 1998-01-07 Matched by certificate designator
ATA 2612

FLT 7100 - STL - LEFT ENGINE FIRE LIGHT ILLUMINATED, CREW DISCHARGED BOTH FIRE BOTTLES, SHUT ENGINE DOWN, UNLOADED PASSENGERS. MAINTENANCE REPLACED LEFT ENGINE FIRE WIRE CONTROLLER. (M)

Source: SDR RAIA980105 · FAA SDRS
J · 1997-09-09 Matched by certificate designator
ATA 2420

STL - FLT 7023 - RIGHT GENERATOR CAPTION ILLUMINATED, GENERATOR WOULD NOT RESET. MAINTENANCE REPLACED RIGHT START CONTACTOR. (X)

Source: SDR RAIA970912 · FAA SDRS
J · 1997-09-09 Matched by certificate designator
ATA 3425

FWA - FLT 7509 - CAPTAIN'S ADI FLAGGED IN CLIMB. MAINTENANCE REPLACED CAPTAIN'S ADI. (X)

Source: SDR RAIA970910 · FAA SDRS
O · 1997-03-26 Matched by certificate designator
ATA 7722

STL - FLT 7344 - RIGHT ENGINE EGT ERRATIC THEN INDICATOR DROPPED TO ZERO. MAINTENANCE REPLACED RIGHT EGT INDICATOR. (X)

Source: SDR RAIA970315 · FAA SDRS
O · 1996-07-18 Matched by certificate designator
ATA 7712

STL - FLT 7061 - LEFT ENGINE WOULD NOT PRODUCE TARGET TORQUE. MAINTENANCE ADJUSTED THE LEFT TORQUE SIGNAL CONDITIONER. (X)

Source: SDR RAIA960712 · FAA SDRS
R · 1996-06-19 Matched by certificate designator
ATA 7200

STL - FLT 7096 - RIGHT ENGINE FAILED TO ACHIEVE TARGET TORQUE. MAINTENANCE REPLACED RIGHT ENGINE. (M)

Source: SDR RAIA960610 · FAA SDRS
J · 1996-05-07 Matched by certificate designator
ATA 7603

STL - FLT 7464 - NR 1 ENGINE WOULD NOT PRODUCE TARGET TORQUE. ADJUSTED ENGINE POWER CONTROL LINKAGE. (M)

Source: SDR RAIA960510 · FAA SDRS
O · 1996-01-19 Matched by certificate designator
ATA 7320

BMI - FLT 7325 - LEFT ENGINE RPM WOULD NOT COME ABOVE 98.5 PERCENT - 99 PERCENT ON TAKEOFF. FERRY FLIGHT TO STL. MAINTENANCE ADJUSTED RPM, GROUND RUNS GOOD. ENGINE TT, 6,994.1 HOURS. (X)

Source: SDR RAIA960133 · FAA SDRS
J · 1995-12-22 Matched by certificate designator
ATA 3230

COU - FLT 7042 - LANDING GEAR WOULD NOT RETRACT. MAINTENANCE CLEANED AND LUBED NOSE GEAR SQUAT SWITCH. GEAR SWINGS REVEALED NORMAL OPERATION. (X)

Source: SDR RAIA951228 · FAA SDRS
N · 1995-10-18 Matched by certificate designator
ATA 7712

STL - FLT 7448 - LEFT ENGINE 5 PERCENT SHY TARGET TORQUE. MAINTENANCE RECALIBRATED LEFT TORQUE SIGNAL CONDITIONER AS PER GARRETT DSC SHEETS. GROUND RUNS CHECK GOOD. (M)

Source: SDR RAIA951025 · FAA SDRS
O · 1995-10-09 Matched by certificate designator
ATA 7500

STL - FLT NR 7304 - LEFT ENGINE DID NOT MAKE TARGET TORQUE. MAINTENANCE REPLACED LEFT ENGINE BLEED AIR GASKETS. GROUND PERFORMANCE RUNS REVEALED NORMAL ENGINE PARAMETERS. (M)

Source: SDR RAIA951013 · FAA SDRS
O · 1995-09-19 Matched by certificate designator
ATA 3242

STL - FLT NR 7089 - RIGHT BRAKE IS NOT OPERATING. MAINTENANCE REPLACED RIGHT BRAKE MAXARET. TAXI CHECK AND LEAK CHECK GOOD. (M)

Source: SDR RAIA950938 · FAA SDRS
N · 1995-08-22 Matched by certificate designator
ATA 7320

STL - FLT NR 7067 - LEFT ENGINE TORQUE DROPPED FROM 80 PERCENT TO 40 PERCENT. MAINTENANCE ADJUSTED LEFT ENGINE MAX RPM. GROUND RUNS REVEALED NORMAL OPERATION. (M)

Source: SDR RAIA950837 · FAA SDRS
L · 1995-07-16 Matched by certificate designator
ATA 3350

STL - EMERGENCY LIGHTS INOP. MAINTENANCE REPLACED EMERGENCY LIGHT BATTERY. (M)

Source: SDR RAIA950718 · FAA SDRS
N · 1995-06-28 Matched by certificate designator
ATA 7712

STL- FLT 7446 - LEFT ENGINE LOW TORQUE, WITH TTL ON AT 80 PERCENT. MAITNENANCE ADJUSTED LEFT ENGINE TORQUE SIGNAL CONDITIONER. GROUND POWER RUNS REVEALED NORMAL OPERATION. (X)

Source: SDR RAIA950642 · FAA SDRS
K · 1995-02-25 Matched by certificate designator
ATA 2910

ALO - FLT 7454 - THE CREW NOTICED HYDRAULIC PUMP PRESSURE ZERO ON BOTH SIDES. CREW PERFORMED EMERGENCY CHECKLIST AND LANDED ACFT. MAINTENANCE DISCOVERED BROKEN HYDRAULIC LINE AT THE MAIN HYD FILTER. REPLACED LINE, AND LEAK CHECK GOOD ON GROUND RUN. (W)

Source: SDR RAIA950246 · FAA SDRS
O · 1995-02-17 Matched by certificate designator
ATA 7120

STL - LEFT ENGINE LOWER INBOARD FWD ENGINE TRUSS TUBE IS CHAFED. MX REPLACED LEFT ENGINE LOWER INBOARD FWD ENGINE TRUSS TUBE. (Z)

Source: SDR RAIA950223 · FAA SDRS
N · 1995-01-28 Matched by certificate designator
ATA 5270

STL - FLT 7508 - PASSENGER DOOR LIGHT ILLUMINATED IN FLIGHT. MAINTENANCE DISCOVERED PINCHED WIRING AT PASSENGER DOOR HANDRAIL. MAINTENANCE REPLACED PINCHED SECTION OF THE WIRING. SYSTEM TEST GOOD. (X)

Source: SDR RAIA950135 · FAA SDRS
N · 1995-01-28 Matched by certificate designator
ATA 5270

STL - FLT 7508 - PASSENGER DOOR LIGHT ILLUMINATED IN FLIGHT. MAINTENANCE REPAIRED CHAFED WIRE AT PASSENGER DOOR. TEST REVEALED NORMAL OPERATION. (X)

Source: SDR RAIA950134 · FAA SDRS