N436CM

EUROCOPTER DEUTSCHLAND GMBH EC 135 P2+ · 2009 · Valid Registration

Registered owner: CAROLINAS HEALTHCARE SYSTEM DBA, NC (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AIR METHODS LLC (QMLA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2022-03-10 Matched by certificate designator
ATA 5300

DURING 1000-HOUR AIRFRAME INSPECTION FOUND TWO RIVETS MISSING FROM LH FRAME 4 WEBBING APPROX. 39” FROM FLOOR AND WEB DISTORTED IN THE AREA. ON RH SIDE SAME HIGHT 39” ABOVE FLOOR A 6.5-INCH CRACK IN THE WEBBING AT FRAME 4. WHEN DISASSEMBLY FOR REPAIR ON 6.5 -INCH CRACK DISCOVERED LOWER FRAME ANGLE CRACKED. REPAIR OF FRAME 4 WEB DISTORTED SECTION WAS COMPLETED UNDER RDAS-EC135-53-2022-002B. THE REPAIR OF CRACKED LOWER ANGLE WAS INSTALLING NEW DOUBLER PN SK-0085-21 IAW ADAS AHI-135-53-001-22.

Source: SDR QMLA2022031020017 · FAA SDRS
O · 2018-01-24 Matched by certificate designator
ATA 5310

DURING A 400 HOUR INSPECTION, FOUND A CRACK APPROXIMATELY 1.5 INCHES LONG ON THE RT FORWARD MAIN GEARBOX DECK AT THE TRANSITION TO THE CABIN ROOF ABOVE THE NR 4 BULKHEAD. REPAIRED IAW SRM 51-71-53,8-7.

Source: SDR QMLA2018012418007 · FAA SDRS
J · 2010-11-25 Matched by certificate designator
ATA 7397

APPROX 10 MINUTES INTO FLIGHT (LEVEL) EXPERIENCED A FADEC MINOR CAUTION ON THE CAD. CONFIRMED THE NR2 TWIST GRIP WAS IN THE NUETRAL POSITION. THE FADEC MINOR THEN BECAME A FADEC FAIL AND RAN THROUGH THAT CHECKLIST AND PERFORMED A SHALLOW APPROACH. VEMD FAILURE CODES (214R & 214L) INDICATED FADEC FAILURE OR WIRING ISSUE. TROUBLESHOT NR2 ENGINE FADEC SYS AND DISCOVERED AIRFRAME CONNECTOR (113VV2AA) HAD LOST TORQUE. CLEANED, REINSTALLED CONNECTOR, PERFORMED 20 MINUTE GROUND RUN AND OPS CHECK FLIGHT. ALL INDICATIONS WERE NORMAL AND RETURNED ACFT TO SERVICE.

Source: SDR RMXA1126201008001 · FAA SDRS
J · 2010-05-15 Matched by certificate designator
ATA 6240

DURING FLIGHT, THE MAIN TRANSMISSION OIL PRESSURE INDICATION FLUXUATED. PILOT PERFORMED A PRECAUTIONARY LANDING SHORT OF BASE. TECH DETERMINED THE TRANSMISSION OIL PRESSURE TRANSDUCER WAS DEFECTIVE. REPLACEMENT PART ORDERED.

Source: SDR RMXA051520100800 · FAA SDRS