N452ER

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
EMBRY-RIDDLE AERONAUTICAL UNIVERSITY INCOperatoron 2017-11-26Operator named in NTSB report

Accident & incident history

Acc · 2017-11-26 Operator named in NTSB report
CESSNA 172 None injury Part 91EMBRY-RIDDLE AERONAUTICAL UNIVERSITY INC
Source: NTSB case GAA18CA080

Maintenance disclosures

Service Difficulty Reports filed with the FAA for this airframe. Filing is largely voluntary — the number of reports is not a measure of reliability. To verify a report, search its control number at the FAA SDRS site.

6 reports on file, 2006-09-12 – 2009-07-22.

OTHER · 2009-07-22 Unresolved
ATA 2710

Part: CABLE — FRAYED (RT AILERON) · airframe 2,129 hrs

DURING INSP RT AILERON PRIMARY CABLE (PN-0510105-360) WAS FOUND WORN AND FRAYED WHERE IT CONTACTS NYLON PULLEY IN THE CEILING AT FS 65.33. PULLEYS ROTATE FREELY, HOWEVER, CABLE DOESN'T PROVIDE ENOUGH "TRACTION" TO ROTATE IT WHEN AILERON CONTROL IS MOVED FROM STOP TO STOP. THIS RESULTS IN THE CABLE SLIPPING AGAINST PULLEY AND EVENTUALLY WEARING THROUGH THE STRANDS. AREA WITH BROKEN STRANDS APPEARS ONLY AS A SHINY CABLE AND THERE ARE NO OBVIOUS BROKEN STRANDS. IT MUST BE VIEWED WITH A POWERFUL MAGNIFYING GLASS AND BRIGHT LIGHT. IN MANY CASES THE NR OF BROKEN STRANDS FAR EXCEED THE AMOUNT SHOWN IN EITHER MM OR AC 43.13.

Source: SDR 2009FA0000637
OTHER · 2009-07-22 Unresolved
ATA 2710

Part: CABLE — FRAYED (RT AILERON) · airframe 2,129 hrs

DURING A ROUTINE INSP THE RT AILERON CABLE (PN-0510105-365) WAS FOUND WORN AND FRAYED WHERE IT CONTACTS THE NYLON PULLEY IN CEILING AT FS 65.33. PULLEYS ROTATE FREELY, HOWEVER, CABLE DOESN'T PROVIDE ENOUGH "TRACTION" TO ROTATE IT WHEN THE AILERON CONTROL IS MOVED FROM STOP TO STOP. THIS RESULTS IN CABLE SLIPPING AGAINST THE PULLEY AND EVENTUALLY WEARING THROUGH THE STRANDS. AREA WITH THE BROKEN STRANDS APPEARS ONLY AS A SHINY CABLE AND THERE ARE NO OBVIOUS BROKEN STRANDS. IT MUST BE VIEWED WITH A POWERFUL MAGNIFYING GLASS AND BRIGHT LIGHT. IN MANY CASES THE NR OF BROKEN STRANDS FAR EXCEED AMOUNT SHOWN IN EITHER MM OR AC 43.13.

Source: SDR 2009FA0000636
OTHER · 2009-07-22 Unresolved
ATA 2720

Part: CABLE — FRAYED (RT RUDDER) · airframe 2,129 hrs

DURING INSP RT RUDDER CABLE (PN-0510105-338) WAS FOUND WORN AND FRAYED WHERE IT CONTACTS THE FAIRLEAD AT FS 65.33. THE AREA WITH BROKEN STRANDS APPEARS ONLY AS A SHINY CABLE AND THERE ARE NO OBVIOUS BROKEN STRANDS. IT MUST BE VIEWED WITH A POWERFUL MAGNIFYING GLASS AND BRIGHT LIGHT. IN MANY CASES THE NR OF BROKEN STRANDS FAR EXCEED THE AMOUNT SHOWN IN EITHER MM OR AC 43.13.

Source: SDR 2009FA0000638
OTHER · 2009-07-22 Unresolved
ATA 2710

Part: CABLE — FRAYED (ZONE 200) · airframe 2,129 hrs

DURING A ROUTINE INSP THE LT AILERON PRIMARY CABLE (PN-0510105-360) WAS FOUND WORN AND FRAYED WHERE IT CONTACTS THE NYLON PULLEY IN THE CEILING AT FS 65.33. THE PULLEYS ROTATE FREELY, HOWEVER, CABLE DOESN'T PROVIDE ENOUGH"TRACTION" TO ROTATE IT WHEN THE AILERON CONTROL IS MOVED FROM STOP TO STOP. THIS RESULTS IN CABLE SLIPPING AGAINST PULLEY AND EVENTUALLY WEARING THROUGH STRANDS. AREA WITH BROKEN STRANDS APPEARS ONLY AS A SHINY CABLE AND THERE IS NO OBVIOUS BROKEN STRANDS. IT MUST BE VIEWED WITH A POWERFUL MAGNIFYING GLASS AND BRIGHT LIGHT. IN MANY CASES THE NR OF BROKEN STRANDS FAR EXCEED THE AMOUNT SHOWN IN EITHER THE MM OR AC 43.13.

Source: SDR 2009FA0000634
OTHER · 2009-05-27 Unresolved
ATA 2710

Part: CONTROL CABLE — FRAYED (AILERONS) · airframe 2,035 hrs

THIS AILERON CABLE WAS WORN BADLY AT THE CENTER OF THE CABIN ROOF WHERE IS PASSES THROUGH A PULLEY. THERE WERE MANY STRANDS WORN AND SEVERAL BROKEN STRANDS.

Source: SDR 2009FA0000436
INADEQUATE Q C · 2006-09-12 Unresolved
ATA 2497

Part: DIODE — FAULTY (BUSS BAR) · airframe 48 hrs

ON A RECENT LOCAL FLIGHT, ONE OF THESE AIRCRAFT EXPERIENCED THE LOSS OF THE MFD, OR RT DISPLAY AS WELL AS THE COMM 2, NAV 2, AUDIO PANEL AND TRANSPONDER. THE CREW ELECTED TO MAKE A PRECAUTIONARY LANDING AT THE NEAREST AIRPORT. ON INSPECTION, IT WAS DISCOVERED THAT THE POWER TO BUSS 2 WAS NOT PRESENT. THE BUSS 2 CIRCUIT BREAKER WAS REPLACED AND THE SYSTEM FUNCTIONED PROPERLY. SHORTLY AFTER, THE MFD FAILED AGAIN. AFTER CLOSER INSPECTION THE WIRE PROVIDING POWER TO THE MFD BREAKER WAS FOUND LOOSE ON THE TERMINAL. THIS WIRE WAS SECURED AND THE AIRCRAFT INCURRED NO FURTHER PROBLEMS. A FLEET INSPECTION OF THE BUSS WIRING FOR THE ESSENTIAL BUSS, BUSS 1 AND BUSS 2 WAS COMMENCED. ADDITIONAL LOOSE WIRE TERMINALS WERE FOU

Source: SDR 2006FA0000901