N465TM

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
WHEELS UP PRIVATE JETS LLC (CVGA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

F · 2025-02-15 Matched by certificate designator
ATA 2130

ON TAKEOFF AND CLIMB OUT AIRPLANE NOT PRESSURIZING. CYCLED PRESS SOURCE KNOBS WITH NO CHANGE- EMERGENCY DECLARED.

Source: SDR CVGA20250219005 · FAA SDRS
O · 2025-01-27 Matched by certificate designator
ATA 3240

LEFT BREAK FAILED DURING TAXING. PERFORMED FUNCTIONAL TESTING MANUAL BRAKE SYSTEM AND POWER BRAKE SYSTEM IAW 400A AMM 32-40-00. PERFORMED POWER BRAKE BLEEDING IAW 400A AMM 32-40-00. NO DEFECTS NOTED. GAUGE ID# TL-00509, DUE 10/22/2025, GAUGE ID# TL-00503, DUE 04/09/2025.

Source: SDR CVGA20250129006 · FAA SDRS
O · 2023-12-05 Matched by certificate designator
ATA 3510

O2 NEEDS SERVICE FOR POSSIBLE LEAK. READS 0 ON GAUGE. REMOVED AND REPLACED O2 BOTTLE REF B400 AMM CH 35-11-00. OPS AND LEAK CHECK PASSED AT THIS TIME. NO DEFECTS NOTED. EMERGENCY WAS DECLARED.

Source: SDR CVGA20231211001 · FAA SDRS
O · 2021-05-25 Matched by certificate designator
ATA 3240

LOSS OF BRAKE PRESSURE ON ALL BRAKE PEDALS AFTER LANDING. BRAKE PRESSURE DID COME BACK AFTER ABOUT 1O SECONDS. HYDRAULIC PRESSURE WAS IN THE GREEN.

Source: SDR CVGA20210601001 · FAA SDRS
O · 2020-11-27 Matched by certificate designator
ATA 3240

AFTER A NORMAL LANDING W/NORMAL BRAKING ENTERED THE FBO RAMP LT TURN WHERE LT RUDDER PEDAL AND BRAKING ALONG W/DIFFERENTIAL POWER WAS REQUIRED. LT RUDDER PEDAL BLED TO THE FLOOR WHEN BRAKES WERE APPLIED THIS OCCURRED ONLY ON CAPTAINS SIDE. PERFORMED VISUAL BRAKE COMPONENTS FOR LEAKS, NONE NOTED. VERIFIED PRESENCE OF PRESSURE AT BOTH BRAKES. PERFORMED FUNCTIONAL TEST OF MIXING VALVES/TAXI STRAIGHT AND HARD TURN WITH NO DEFECTS NORMAL BRAKING NOTED FROM PILOT AND COPILOT PEDALS. PERFORMED BRAKE LT/RT BLEEDING TO REMOVE POSSIBLE TRAPPED AIR OPERATIONS CHECK GOOD, LEAK CHECK GOOD. PERFORMED ADDITIONAL TAXI CHECK WITH NO DEFECTS NOTED.

Source: SDR T17A20200811044 · FAA SDRS
O · 2011-08-05 Unresolved
ATA 3020

DURING SCHEDULED INSP, FOUND LT ENGINE INBD SIDE ENGINE PAD TO "Y" DUCT BLEED AIR ANTI-ICING DUCT CRACKED AT BELLOWS, STAINLESS STEEL BRAIDING BLOWN-OUT AND FRAYED. MX HISTORY UNKNOWN, POSSIBLY CAUSED BY MIS-ALIGNMENT. RECOMMEND MFG INVESTIGATE WHETHER THIS IS A HIGH REPLACEMENT COMPONENT OR AN OCCASIONAL ISSUE RELATED TO INSTALLATION. RECOMMEND A NOTE MADE IN THE MM REGARDING DUCT INSTALLATION ALIGNMENT.

Source: SDR E81RJT2309420A · FAA SDRS
O · 2011-08-05 Unresolved
ATA 3020

DURING SCHEDULED INSPECTION, FOUND LT ENGINE NACELLE ANTI-ICE CROSSOVER BLEED AIR DUCT CRACKED AT BELLOWS, STAINLESS STEEL BRAIDING FRAYED AND BLOWN-OUT. MX HISTORY UNKNOWN. MAY POSSIBLY HAVE BEEN CAUSED BY PARTIAL MIS-ALIGNMENT STRESS. RECOMMEND MFG INVESTIGATE WHETHER THIS IS A HIGH REPLACEMENT COMPONENT OR MORE OF AN OCCASIONAL OR ISOLATED REPLACEMENT REQUIREMENT. RECOMMEND A NOTE BE MADE IN THE MM REMINDING INSTALLING TECH TO INSPECT AND ADJUST DUCT ASSY'S, ALIGNMENT DURING INSTALLATION.

Source: SDR E81RJT2309420B · FAA SDRS
R J · 2009-02-06 Unresolved
ATA 7321

CREW REPORTED LT ENGINE WOULD NOT ACHIEVE CALCULATED TAKEOFF POWER N1. VERIFIED COMPLAINT, ENGINE COULD NOT ACHIEVE MORE THAN 94 PERCENT, N1 AND NOTED NO RPM DROP DURING EFC AUTHORITY CHECKS. ALSO NOTED FLUCTUATING ENGINE VIBRATION INDICATION. EFC AUTHORITY ADJUSTMENT HAD MINIMAL EFFECT, WOULD ONLY GET LESS THAN SPECIFIED 1.5 PERCENT N1 DROP, AND THEN COULD ONLY ACHIEVE 92 PERCENT N1. CHECKED T0 PROBE AND EEC, SWAPPED EEC'S, PROBLEM CONTINUED. REPLACED HMU (JET FUEL CONTROL) WITH OVERHAULED UNIT AND ADJUSTED ENGINE RIGGING AS REQUIRED, VERIFIED ENGINE PERFORMANCE NOW WITHIN MM SERVICE LIMITS. SUGGEST HMU MFG AND/OR ENGINE MFG TEARDOWN AND INVESTIGATE HMU FOR INTERNAL FAULT CAUSING LOW POWER, EFC AUTHORITY FAULTS.

Source: SDR 2009F00010 · FAA SDRS