N4810N

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
CIVIL AIR PATROLOperatoron 2016-08-24Operator named in NTSB report

Accident & incident history

Acc · 2016-08-24 Operator named in NTSB report
CESSNA 182 Minor injury Part 91CIVIL AIR PATROL
Source: NTSB case GAA16CA449

Maintenance disclosures

P · 2004-01-10 Unresolved
ATA 7921

8/22/2002, OIL COOLER TCM 639171. TACH TIME NOT LOGGED. APPROX 830 SMOH. 12/1/2003 A MAJOR OIL LEAK DEVELOPED AROUND THE OIL COOLER AND THE NR 5 CYL PUSH ROD TUBES. ISOLATED LEAK TO OIL COOLER GASKETS. 1036 SMOH. DURING REMOVAL OF OIL COOLER BASE PLATE, IT WAS DETERMINED THAT THE ATTACHING BOLTS WERE IMPROPERLY TORQUED. NEW GASKETS WERE INSTALLED AND COOLER ATTACHING BOLTS PROPERLY TORQUED. PROBLEM CAUSED BY IMPROPERLY TORQUED ATTACHING BOLTS.

Source: SDR 2004FA0000058 · FAA SDRS
J · 2004-01-09 Unresolved
ATA 8520

REBARRELED CYL, ECI PISTONS. LOSS OF OIL PRESSURE, 260 STOH, 1043 SMOH. CAUSE, BROKEN NR 2 PISTON, PARTS BLOCKING OIL PICKUP SCREEN. POSSIBLE CAUSES. DEFECTIVE PISTON CASTING, DROPPED PISTON OR IMPROPERLY MACHINED NR 4 RING GROOVE, SQUARE CUT BOTTOM OF GROOVE. 50 PERCENT OF BOTTOM SKIRT BROKE OFF PISTON. PISTON RING BROKE INTO ABOUT 20 PIECES.

Source: SDR 2004FA0000055 · FAA SDRS
J · 2004-01-09 Unresolved
ATA 8520

ENGINE OVERHAULED. REBARRELED CYL, ECI PISTONS. LOSS OF OIL PRESSURE, 260 STOH, 1043 SMOH. CAUSE, BROKEN NR 2 PISTON, PARTS BLOCKING OIL PICKUP SCREEN. POSSIBLE CAUSES. DEFECTIVE PISTON CASTING, DROPPED PISTON OR IMPROPERLY MACHINED NR 4 RING GROOVE, SQUARE CUT BOTTOM OF GROOVE. 50 PERCENT OF BOTTOM SKIRT BROKE OFF PISTON. PISTON RING BROKE INTO ABOUT 20 PIECES.

Source: SDR 2004FA0000057 · FAA SDRS