N490H

AMERICAN EUROCOPTER LLC AS350B3 · 2008 · Valid Registration

Registered owner: AIR METHODS LLC, CO (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AIR METHODS LLC (QMLA)Certificate holderMatched by certificate designator

Accident & incident history

Accident · 1984-05-25 Unresolved
Enstrom F-28A None injuryoperator not yet resolved
Source: NTSB case CHI84LA209

Maintenance disclosures

O · 2024-12-10 Matched by certificate designator
ATA 5312

AS350 S/N 4539 NOTED CHAFING DAMAGE ON THE LH LATERAL BULKHEAD (X FRAME) ON THE INBOARD FACE AS SHOWN IN FIGURE 1. THE LH X-FRAME HAS ONE CHAFED AREA LOCATED ON ITS INBD BEADED FACE MEASURING APPROXIMATELY 0.90” LONG AND 0.30” WIDE WITH A MAX DEPTH OF 0.024”

Source: SDR 2024FA0000956 · FAA SDRS
O · 2024-12-10 Matched by certificate designator
ATA 5310

THE TRANSMISSION SUPPORT FRAME (PN 350A21-1041-143) HAS CHAFING DAMAGE ON THE LOWER FLANGE FROM AN UNSECURED CABLE.

Source: SDR 2024F00314 · FAA SDRS
O · 2024-12-10 Matched by certificate designator
ATA 5302

TAIL GEARBOX MOUNTING PLATE CHAFE DAMAGE.

Source: SDR 2024FA0000955 · FAA SDRS
B S · 2023-10-02 Matched by certificate designator
ATA 2150

PILOT REPORTED SMOKE SMELL IN CABIN, TURNED OFF THE A/C SYSTEM AND SMELL WENT AWAY. LANDED AT BASE WITH NO FURTHER ISSUES. MECHANIC ON SITE FOUND WHERE A/C COMPRESSOR CLUTCH WAS INOP.

Source: SDR QMLA2023100420081 · FAA SDRS
B · 2023-01-21 Matched by certificate designator
ATA 3310

FOUND THAT THE RTV USED ON A RECENTLY INSTALLED LIGHT WAS EMITTING A SMELL FROM THE OVERHEAD CABIN LIGHTS. APPLIED 10 DAY MEL TO THOSE LIGHTS IN ORDER TO ORDER A SEALANT THAT IS MORE SUITABLE (HIGHER TEMP),AND PULLED CIRCUIT BREAKER TO THESE LIGHTS. THE TEMPERATURE OF THESE LIGHTS WAS COMPLETELY RESEARCHED TO FIND THIS IS NORMAL OPERATION.

Source: SDR QMLA 202301242000 · FAA SDRS
O · 2020-06-17 Matched by certificate designator
ATA 5302

AC 4539 HAS CHAFFING ON THE RT BATTERY TRAY SUPPORT AND ON THE INTERNAL SIDE OF THE TAIL BOOM SKIN. DAMAGE BEING OVER 12 INCHES LONG WITH A MAX DEPTH OF .020 . DAMAGE BEING LOCATED AT APPROXIMATELY BS 7948, BL 190R, AND WL 2039. IT HAS A MAX DEPTH OF .010 IN AND AREA 2.5 LONG BY .65.

Source: SDR 2A6D202006176001 · FAA SDRS
B · 2020-05-02 Matched by certificate designator
ATA 3120

PILOT REPORTED A BURNT SMELL IN THE CABIN UPON APPROACH AND NOTICED THE CLOCK LIGHT HAD GONE OUT. UPON ARRIVAL AT THE AIRCRAFT, THE MECHANIC PERFORMED A VISUAL INSPECTION OF ALL WIRING BEHIND THE INSTRUMENT PANEL, AND ALL WIRING LOOKED TO BE IN A SERVICABLE CONDITON. HE THEN HAD THE PILOT PERFORM A GROUND RUN AND CONFIGURED THE AIRCRAFT AS IT WAS DURING FLIGHT TO TRY AND DUPLICATE THE DISCREPANCY. AGAIN THERE WERE NO DEFECTS NOTED. THE BURNT SMELL WAS ATTRIBUTED TO THE INTERNAL CLOCK LIGHTING BULB BURNING OUT ON APPROACH. THIS SYSTEM HAS SINCE BEEN DEFERRED, AND THE AIRCRAFT WAS PLACED BACK INTO SERVICE.

Source: SDR QMLA2020050520018 · FAA SDRS
W · 2012-10-09 Matched by certificate designator
ATA 7261

DURING A ROUTINE 600 HR ENGINE INSPECTION, IT WAS NOTED THAT THE ENGINE INTERNAL OIL FILTER WAS MISSING. DETERMINED THAT THE ENGINE WAS OPERATED FOR THE LAST 600 HRS WITHOUT A FILTER ELEMENT INSTALLED. A NEW FILTER ELEMENT WAS INSTALLED AND THE OIL SYS WAS FLUSHED AND SERVICED. PULLED AN OIL SAMPLE BEFORE DRAINING THE SYS AND SEND IT FOR EVALUATION. EVALUATION WAS RETURNED WITH ALL NORMAL WEAR INDICATED.

Source: SDR QMLA2012100912167 · FAA SDRS
J · 2012-09-19 Matched by certificate designator
ATA 6520

WHILE TRANSITIONING OVER AIRPORT, TAIL ROTOR GEAR BOX CHIP LIGHT ILLUMINATED. DECLARED AN EMERGENCY AND LANDED. ON FINAL, CHIP LIGHT EXTINGUISHED. LANDING WAS WITH OUT INCIDENT. FELT NO UNUSUAL PRESSURE OR VIBRATION IN THE CONTROLS. MECHANIC FOUND AN INSIGNIFICANT AMOUNT OF METAL SHAVINGS ON THE CHIP DETECTOR WHEN IT WAS INSPECTED. FLUSHED THE GEARBOX, PERFORMED THE REQUIRED HOVER CHECK AND RETURNED TO SERVICE.

Source: SDR QMLA2012091912156 · FAA SDRS
F · 2011-03-11 Matched by certificate designator
ATA 6230

PILOT EXPERIENCED A BINDING OR HARD POINT PREVENTING CYCLIC TRAVEL IN THE AFT LT QUADRANT OF TRAVEL DURING HOVER TAXI/FWD FLIGHT IN GROUND EFFECT. THE PILOT PERFORMED A RUN ON LANDING. THE PILOT SELECTED IDLE AND PERFORMED A CONTROL FREEDOM CHECK WITH CYCLIC FRICTION REMOVED AND THE SYMPTOMS WERE STILL PRESENT. NO "SERVO" LIGHT, HYD LIGHT OR ANY OTHER SECONDARY INDICATIONS WERE PRESENT. IN COLLABORATION WITH MFG TECH SUPPORT, DISCONNECTED THE INPUT RODS AT THE SERVO CONTROLS OF THE MAIN ROTOR, CLEANED CYCLIC FRICTION CUP, INSPECTED CONTROL RODS OF CYCLIC AND COLLECTIVE FROM CONTROLS TO SERVOS FOR ANY BINDING, VISUALLY AND BY FEEL. RECONNECTED RODS TO MAIN ROTOR SERVOS. NO MECHANICAL BINDING WAS FOUND. VISUALLY INSPECTED SWASH PLATE, MAST TAPE AND SURROUNDING AREAS FOR ANY SIGNS OF BINDING, NONE NOTED. PERFORMED GROUND RUN FOR OPS CHECK OF MAIN ROTOR CONTROLS. OPS CHECK WAS GOOD. PERFORMED FLIGHT CONTROL CHECK FOR CONTINUED SERVICE ALL FLIGHT CONTROLS OPERATED NORMAL NO SIGNS OF ANY BINDING OR RESTRICTION OF MOTION. SUSPECT DIRTY SWASHPLATE FRICTION CUPS AS THE CULPRIT FOR UNUSUAL CONTROL FEEL.

Source: SDR RMXA110314194936 · FAA SDRS