N530LN

EUROCOPTER DEUTSCHLAND GMBH EC 135 P2 · Valid Registration

Registered owner: AIR METHODS LLC, CO (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AIR METHODS LLC (QMLA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2021-05-10 Matched by certificate designator
ATA 5314

DURING A 1000 HOUR INSPECTION FOUND THE LEFT HAND KEEL BEAM TOP EXTRUSION AT F.S. 5700, LBL 500 EXFOLIATED AT THE END.

Source: SDR 2A6R2021051060502 · FAA SDRS
O · 2021-05-10 Matched by certificate designator
ATA 5310

DURING A 1000 HOUR INSPECTION FOUND THE LEFT SIDE OF COCKPIT FLOOR BEHIND THE PILOT'S SEAT JUST FORWARD OF F.S. 3150 AND INBOARD OF L.B.L 500 SEVERAL MEDIUM SIZED DENTS AND DELAMINATE UPPER SKIN.

Source: SDR 2A6R2021051060503 · FAA SDRS
O · 2021-05-10 Matched by certificate designator
ATA 5310

DURING 1000 HOUR INSPECTION FOUND THE PILOT'S SIDE COCKPIT FLOOR GROUND BRACKET AND UPPER AND LOWER SKIN CORRODED AT F.S. 1700

Source: SDR 2A6R2021051060504 · FAA SDRS
O · 2021-05-07 Matched by certificate designator
ATA 5311

DURING A 1000 HOUR INSPECTION FOUND THE RIGHT SIDE OF THE 5 ALPHA FRAME CRACKED. INSTALLING A DOUBLER P/N L533M1105103 OVER THE EXISTING 5 ALPHA FRAME AS PER THE SRM

Source: SDR 2A6R2021050760501 · FAA SDRS
B · 2018-04-04 Matched by certificate designator
ATA 6321

ABOUT 18 MINUTES INTO FLIGHT, ROTOR BRAKE CAUTION LIGHT ILLUMINATED WITH AN ACCOMPANYING ODOR. LANDED AIRCRAFT AND SHUTDOWN AND VERIFIED THERE WAS NO SMOKE OR FIRE. CALLED MAINTENANCE. MAINTENANCE INSPECTED ROTOR BRAKE, FOUND TO BE FREE AND OPERATING NORMAL, HOWEVER BRAKE PADS LOOKED WORN BEYOND LIMITS. MEL'D THE ROTOR BRAKE AND DEACTIVATED IT.

Source: SDR QMLA2018040418040 · FAA SDRS
J · 2017-09-06 Matched by certificate designator
ATA 6320

AIRCRAFT EXPERIENCED A COCKPIT MGB CHIP LIGHT AFTER ENGINE START AND BEFORE TAKE-OFF. SERVICEABILITY CHECKS AND MGB OIL FLUSH WAS ACCOMPLISHED AND AIRCRAFT RETURNED TO AIRWORTHY CONDITION AND RELOCATED TO MAINTENANCE FACILITY IAW AMM AND ASB EC135-63A-012. DURING THE POST CHIP EVENT REQUIRED INSPECTIONS OF THE MGB INPUT DRIVE PINION ASSEMBLIES PITTING WAS FOUND ON THE TEETH.

Source: SDR QMLA2017090617088 · FAA SDRS
B · 2007-06-17 Matched by certificate designator
ATA 2120

AIRCRAFT AND CREW RETURNING FROM A MEDICAL RUN WHEN A SUDDEN STRONG ODOR OF BURNING FILLED THE COCKPIT AND CREW AREA. NO SMOKE WAS NOTED IN THE AIRCRAFT. PILOT DECLARED AN EMERGENCY AND LANDED. AS OF TIME OF THIS REPORT AIRCRAFT IS GROUNDED WITH A MECHANIC AND PILOT ATTEMPTING TO ISOLATE PROBLEM AND NO DETERMINATION HAS BEEN MADE.

Source: SDR 47106172007 · FAA SDRS