N54178

EUROCOPTER AS 350 B3 · 2006 · Valid Registration

Registered owner: AIR METHODS LLC, CO (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AIR METHODS LLC (QMLA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2022-05-27 Matched by certificate designator
ATA 5312

DAMAGE WAS NOTED TO THE 15 DEGREE BULKHEAD LH WEB (P/N: 350A21-1032.86) IN THE FORM OF CHAFES. THE TWO CHAFING DAMAGE AREAS WERE FOUND NEAR THE X-FRAME AND UPPER CHAFING DAMAGE WAS MEASURED TO BE APPROXIMATELY 0.20” IN LENGTH, 0.3” IN WIDTH AND 0.008” DEPTH; THE LOWER CHAFING DAMAGE WAS MEASURED TO BE APPROXIMATELY 0.20” IN LENGTH, 0.2” IN WIDTH AND 0.010” DEPTH

Source: SDR 2A6D20220527001 · FAA SDRS
O · 2018-11-02 Matched by certificate designator
ATA 5310

RIGHT SIDE LOWER DOOR FRAME FOUND CORRODED.

Source: SDR 2A6R20181102001 · FAA SDRS
O · 2018-11-02 Matched by certificate designator
ATA 5310

RIGHT X FRAME STRUCTURE CHAFED.

Source: SDR 2A6R2018110202 · FAA SDRS
O · 2018-03-01 Matched by certificate designator
ATA 6410

TAIL ROTOR BLADE CRACKED, 7 INCHES DOWN FROM COLLAR, 3 INCHES LONG . FOUND TO BE OUT OF LIMITS IAW AMM 64-10-00,6-1A.

Source: SDR QMLA2018030118026 · FAA SDRS
J · 2015-03-18 Matched by certificate designator
ATA 2435

WHILE ACFT WAS IN FLIGHT WITH A PATIENT ABOARD, PILOT NOTICED A GRADUAL LOSS OF VOLTAGE & AMPERAGE. AFTER SHEDDING SECONDARY ELEC EQUIP, VOLTAGE & AMPERAGE CONTINUED TO DECREASE WHILE A GEN LIGHT ILLUMINATED DURING FINAL DESCENT ON TO A MALL PARKING LOT. REMOVED STARTER GEN FOR INSPECTION & FOUND THAT THE BRUSH BRAID ATTACH POINTS WERE IN PIECES. THE BRAID ATTACH RIVETS ON THE BRUSHES BECAME LOOSE, THEN SEPARATED.

Source: SDR QMLA2015031815018 · FAA SDRS
O · 2014-04-07 Matched by certificate designator
ATA 5302

DISCOVERED CRACKS IN AFT TAIL BOOM MOUNTED BATTERY TRAY. FIRST CRACK WAS LOCATED ON RT BATTERY TRAY. THIS CRACK WAS ON THE RT NUTPLATE DOUBLER FOR THE RT BOLT HOLE THAT ACCOMMODATES THE BATTERY HOLD DOWN BRACKET. SECOND CRACK WAS LOCATED ON THE LT BATTERY TRAY AT THE AFT LT BOLT HOLE LOCATION. THIS CRACK WAS IN THE SHAPE OF A J & TOTALED A LENGTH OF 45 MM. THESE CRACKS APPEAR TO BE STRESS RELATED WHEN THE BATTERY HOLD DOWN BRACKETS ARE INSTALLED & TIGHTENED.

Source: SDR QMLA2014040714034 · FAA SDRS
K · 2013-04-06 Matched by certificate designator
ATA 2910

GROUND RUN HYD FLUID COMING FROM HOSE END FITTING GOING INTO HYD MAINFOLD. NEW HOSE WAS INSTALLED 1:43 HOURS AGO. REPORTED HAVING PROBLEMS WITH THIS HOSE. LOOKS LIKE POSSIBLE BAD CRIMPING OF HOSE ONTO FITTING. INSTALLED SERVICABLE HOSE OF AN OLDER PN. RUN UP NO LEAKS ON GROUND RUN.

Source: SDR QMLA2013040613048 · FAA SDRS
D · 2013-01-06 Matched by certificate designator
ATA 7160

ON THE FDC AIR FILTER SYS, FOUND THE ENCAPSULATED RECEPTACLE, P26R16-1 HAD FAILED. THE CAPSULE WHICH IS HELD IN PLACE BY WHAT LOOKS LIKE "METAL SET" HAD SEPARATED FROM THE .2500 TURN FASTENER AND DROPED INTO THE ENGINE BAY. ON FURTHER INSPECTION SEVERAL OTHER CAPSULES WERE FOUND LOOSE.

Source: SDR QMLA2013010613002 · FAA SDRS
R J · 2011-01-13 Matched by certificate designator
ATA 7603

ACFT WAS LEAVING AIRPORT, DURING FLIGHT ACFT HAD A YAW FLUCTUATION. AFTER SEVERAL YAW FLUCTUATIONS THE WARNING INDICATION PANEL DISPLAYED AN AMBER GOV LIGHT. DURING THIS TIME OF OCCURANCE THE PILOT REPOSITIONED THE ACFT TO AIRPORT AND LANDED WITHOUT INCIDENT.

Source: SDR RMXA350481 · FAA SDRS