N563AM

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AIR METHODS LLC (QMLA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2022-07-11 Matched by certificate designator
ATA 6300

WE WERE RETURNING TO BASE AFTER COMPLETING AN INTERFACILITY TRANSFER. WE WERE FLYING ALONG, MINDING OUR OWN BUSINESS WHEN THE MGB CHIP LIGHT ILLUMINATED. I IMMEDIATELY STARTED LOOKING FOR A SAFE PLACE TO CONDUCT A PRECAUTIONARY LANDING. FOUND AN OPEN LIT AREA AND LANDED WITHOUT FURTHER INCIDENT. MECHANIC CAME OUT AND PULLED THE CHIP PLUG AND FOUND A MEDIUM SIZED PIECE PF METAL FUZZ. HE DETERMINED THAT IT MET THE CRITERIA TO CONTINUE OUR FLIGHT BACK TO BASE.

Source: SDR QMLA2022071220040 · FAA SDRS
B · 2020-10-16 Matched by certificate designator
ATA 7200

ON RUN-UP ONCE I GOT UP TO THE FLY POSITION AND WAS STARTING TO PULL PITCH THE MEDIC ASKED ME WHAT ALL THE SMOKE WAS. I LOOKED TOWARD THE REAR LEFT AND WE WERE ENGULFED IN SMOKE. I IMMEDIATELY SHUT THE ENGINE DOWN. I APPLIED THE ROTOR BRAKE AND ONCE THE ROTORS STOPPED, WE EXITED THE AIRCRAFT. I MADE SURE I COULD NOT SEE ANY FIRE AND THE SMOKE STARTED TO SUBSIDED. I OPENED THE ENGINE COWLING TO INSPECT THE AREA. FOUND OIL ALL OVER THE ENGINE DECK AND COWLING. NOTIFIED AIR COM, AM AND MECHANIC. A REAR BEARING CLEANING WAS RECOMMENDED SO WE WILL ACTUALLY BE CHANGING THE MO3 FOR OUR COMPLIANCE. COKING WAS FOUND AT THE REAR BEARING OIL STRUT.

Source: SDR QMLA2020101920056 · FAA SDRS
J · 2010-08-16 Matched by certificate designator
ATA 6520

ENROUTE TO DROP OFF PATIENT, PILOT REPORTED TAIL ROTOR GEARBOX CHIP WARNING LIGHT IN FLIGHT; FIRST IT FLASHED, THEN REMAINED STEADY. PILOT COMPLETED UNSCHEDULED LANDING AT NEARBY AIRPORT. WHEN MECHANIC INSPECTED T/R GB CHIP DETECTOR; MULTIPLE METAL FLAKES/SPLINTERS WERE FOUND. COULD NOT DETERMINE IF PARTICLES WERE FLAKES OR SPLINTERS, FAULT ISOLATION MANUAL STATES "LEAD TO SERIOUS DAMAGE. 1 AT 3 MM, 1 AT 2 MM, 4 AT .5MM IN SIZE. ALSO FOUND APPROX 12-15 SMALL BUT VISIBLE METALLIC PARTICLES. GEARBOX REPLACEMENT NEEDED. AFTER GEARBOX WAS REPLACED WITH SERVICEABLE UNIT IAW MM, GOUND CHECKS COMPLETED AND CK FLIGHT COMPLETED. ACFT RETURNED TO SERVICE 8/18/10.

Source: SDR QMLA2010081610051 · FAA SDRS
O · 2010-07-28 Matched by certificate designator
ATA 7250

THIRD OCCURANCE OF SILVER PLATING FLAKES FOUND DURING SPECIAL 5 HOUR INSP. AFTER CONSULTATION WITH MFG, CORRECTIVE MX ACTION WAS REQUIRED.

Source: SDR QMLA072810043 · FAA SDRS
O · 2010-07-15 Matched by certificate designator
ATA 2500

ALLS HANDLE CRACKED; SECOND OCCURANCE. FOUND DURING OPERATION OF SYS. PROBABLE CAUSE FOR CRACK IS STRESS FATIGUE; CORRECTIVE ACTION - REMOVED AND REPLACED WITH SERVICEABLE UNIT.

Source: SDR QMLA2010071510036 · FAA SDRS
O · 2010-07-09 Matched by certificate designator
ATA 3160

INCONSISTENT DISPLAY DEGRADATION. OFF COLORS AND INTERMITTENT FLASHING SCREEN. APPEARED ONLY IN HIGH OAT SITUATIONS DURING DAYTIME. COULD NOT PRODUCE A CONSISTENT FAIL OTHER THAN STATED. PROBABLE CAUSE FOR DISPLAY DEGRADATION IS HEAT; REMOVED AND REPLACED WITH SERVICEABLE UNIT.

Source: SDR QMLA2010070910035 · FAA SDRS