N651BR

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
MESA AIRLINES, INC. (MASA)Operator2008-02-13 – 2008-02-13Operator named in NTSB report
Mesa AirlinesOperator2008-02-13 – 2008-02-13Operator named in NTSB report

Accident & incident history

Inc · 2008-02-13 Operator named in NTSB report
Bombardier, Inc. CL-600 None injury Part 121MESA AIRLINES, INC.
Source: NTSB case SEA08IA080

Maintenance disclosures

O · 2007-11-02 Matched by certificate designator
ATA 3350

ASH 1034 HNL - LT OVERWING EMERGENCY EXIT LIGHT INOP. RELAMPED.

Source: SDR MASA200700767 · FAA SDRS
O · 2007-07-06 Matched by certificate designator
ATA 3350

ASH 1006 HNL. CABIN DOOR FLOOR EMERGENCY LIGHTS INOP. MAINTENANCE REPLACED THE LIGHT SEGMENT AT ROW 6, OPS CHECK GOOD.

Source: SDR MASA200700403 · FAA SDRS
O · 2007-05-11 Matched by certificate designator
ATA 2561

ASH 1018 HNL - INFANT LIFE VEST WAS MISSING. MX INSTALLED A NEW LIFE VEST.

Source: SDR MASA200700262 · FAA SDRS
O · 2007-05-08 Matched by certificate designator
ATA 2561

ASH 1006 HNL. - MX REPORTED AN INFANT LIFE VEST WAS MISSING. MX INSTALLED A NEW LIFE VEST.

Source: SDR MASA200700248 · FAA SDRS
O · 2007-04-01 Matched by certificate designator
ATA 2561

ASH 1018 HNL. - SEATS 12A AND 12C MISSING THE LIFE VESTS. MX INSTALLED NEW LIFE VESTS.

Source: SDR MASA200700179 · FAA SDRS
O · 2007-01-01 Matched by certificate designator
ATA 3350

ASH 1003 HNL. RT EXTERIOR FWD EMERGENCY LIGHT INOP. MX REPLACED THE LAMP AND OP CHECK WAS GOOD.

Source: SDR MASA200700001 · FAA SDRS
O · 2006-09-08 Matched by certificate designator
ATA 2210

ASH 7109 BNA - CREW RTG DUE TO YAW CAMP NR 1 WILL NOT STAY ENGAGED. MX RESET YAW DAMP AND AUTOPILOT SYSTEMS.

Source: SDR MASA200602244 · FAA SDRS
N · 2006-08-22 Matched by certificate designator
ATA 2760

ASH 1038 HNL - SPOILERON AND INBOARD GROUND SPOILER FAULT. MX RESET SYSTEM.

Source: SDR MASA200602149 · FAA SDRS
F · 2006-08-17 Matched by certificate designator
ATA 2750

ASH 1004 HNL.- PILOT DECLARED EMERGENCY FOR A FLAPS FAIL AT 10 DEGREES IN FLIGHT. MX COMPLIED WITH PART A INSPECTION.

Source: SDR MASA200602120 · FAA SDRS
O · 2006-07-17 Matched by certificate designator
ATA 2561

ASH 1043 HNL - 2 ADULT LIFE VESTS WERE MISSING FROM THE AIRCRAFT. MX INSTALLED 2 NEW LIFE VESTS.

Source: SDR MASA200601873 · FAA SDRS
J · 2006-07-14 Matched by certificate designator
ATA 5210

ASH 1010 HNL - PAX DOOR LATCH CAUTION WARNING IN FLIGHT. MX ADJUSTED UPPER STOP.

Source: SDR MASA200601849 · FAA SDRS
N · 2006-06-16 Matched by certificate designator
ATA 2700

GLD UNSAFE CAUTION MESSAGE IN FLIGHT. MX RESET THE SECUS. OPS CHECK GOOD.

Source: SDR MASA200601623 · FAA SDRS
N · 2005-01-26 Unresolved
ATA 3418

EVENT SUMMARY STATED THAT STALL FAIL MSG ON CLIMB-OUT. NO FAULT CODES IN MDC. RESET SPS. INSPECTED BOTH AOA VANES. OPS CHK GOOD.

Source: SDR 05026651 · FAA SDRS
N · 2005-01-23 Unresolved
ATA 2611

TOILET SMOKE EICAS MESSAGE. INSPECTED LAV LIGHTS, PACK COALESCER BAGS AND PERFORMED RUNS. NO DEFECT NOTED. REMOVED AND REPLACED SMOKE DETECTOR.

Source: SDR 05023651 · FAA SDRS
J · 2005-01-20 Unresolved
ATA 3260

EVENT SUMMARY STATED GEAR DISAGREE. REMOVED AND REPLACED MLG PRIORITY VALVE IN REF TO CRJ MM 32-32-15, NO FIX. FOUND AIR IN NR 3 HYD SYSTEM, DRAINED AIR AND SERVICED HYD SYSTEM IAW CRJ AMM 12-12-29. CREW WROTE THE FOLLOWING, LEFT GEAR UP DISAGREE ON RETRACTION, CLEARED ITSELF IN 1 MINUTE, HYD PUMP 3 WAS 2300 LBS. D/L CODES FROM PSEU AND A HARD FAIL WAS DISCOVERED ON LT MLG CODES WAS LEFT GEAR UPLOCK FAR. DID NOT HAVE A CHANCE TO DO GEAR SWINGS BUT BELIEVED GEAR WAS SLOW TO COME UP. FOUND NR 3 ACCUMULATOR LOW, SERVICED NR 3 ACCUMULATOR IAW CRJ AMM 12-12-29 D/L LOADED CODES FROM PSEU AND RESET PSEU. GEAR SWINGS OP CHECK GOOD. MLG SELECTOR VALVE, NO LEAK NOTED.

Source: SDR 05020651 · FAA SDRS
J · 2005-01-11 Unresolved
ATA 2740

CREW REPORT ON 01/11 STATED THAT IMMEDIATELY AFTER T/O THE STAB TRIM AND MACH TRIM CAUTION MSGS POSTED AT THE SAME TIME. RETRIEVED FAULT CODES FROM MDC. PERFORMED HSTCU OPS TEST PER 27-40-00. OPS CHECK GOOD.

Source: SDR 05011651 · FAA SDRS
F · 2004-12-30 Unresolved
ATA 2750

FLAPS FAIL AT ZERO. RETRIEVED FAULT CODES 1 JAM 2. PDU DIFF 3 UNSPECIFIED, CLEARED FAULTS OPS CHECKS GOOD AT THIS TIME REF 27-51-00.

Source: SDR 04365651 · FAA SDRS
B · 2004-12-20 Unresolved
ATA 2150

LAV SMOKE INDICATION AT 200FT. NO SMOKE OR FUMES BUT ODOR. SUSPECT GLYCOL IN AIR CONDITIONING. MX PERFORMED HIGH POWER RUNS. NO DEFECT NOTED.

Source: SDR 04355651 · FAA SDRS
J · 2004-09-28 Unresolved
ATA 3020

EVENT SUMMARY STATED REJECTED TAKEOFF AT 40KT DUE TO LT COWL ANTI-ICE CAUTION MSG. TROUBLESHOOTING CONFIRMED THE PROBLEM, AND RTG. REMOVED AND REPLACED LT COWL ANTI ICE VALVE REF AMM 30-22-01. PERFORMED OPS CHECK OF ANTI ICE. OPS CHECK GOOD.

Source: SDR 09272651 · FAA SDRS
O · 2004-04-14 Unresolved
ATA 3350

DURING INSPECTION THE FOWARD FLOOR EMERGENCY FLOOD LIGHT WAS FOUND INOPERATIVE. THE BULB WAS REPLACED AND A SATISFACTORY OPERATIONAL CHECK WAS PERFORMED.

Source: SDR 04105651 · FAA SDRS
O · 2004-03-05 Unresolved
ATA 2750

DURING FLAP EXTENSION, THE FLAPS WOULD NOT EXTEND BEYOND 20 DEGREES. THE MALFUNCTION DID NOT INTERFERE WITH THE SAFE OPERATION OF THE FLIGHT. THE FLIGHT WAS COMPLETED NORMALLY AND PASSENGERS DEPLANED NORMALLY. THE FLAP CONTROL LEVER WAS REPLACED. A SATISFACTORY OPERATIONAL CHECK WAS PERFORMED AND AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 04065651 · FAA SDRS
J · 2004-02-23 Unresolved
ATA 2750

DURING APPROACH OF FLIGHT 7522 CREW REPORTED A FLAP SYSTEM FAILURE WITH FLAPS A 8 DEGREES. FLIGHT LANDED UNEVENTFULLY. A SYSTEM OPERATIONAL CHECK WAS PERFORMED AND AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 04054651 · FAA SDRS
O · 2004-02-09 Unresolved
ATA 3350

DURING INSPECTION THE LEFT FORWARD EMERGENCY LIGHT WAS FOUND INOPERATIVE. THE BULB WAS FOUND FAULTY AND REPLACED. A SATISFACTORY OPERATIONAL CHECK WAS PERFORMED AND AIRCRAFT RETURNED TO SERVICE.

Source: SDR 04040651 · FAA SDRS
C F · 2004-01-03 Unresolved
ATA 2741

DURING CLIMB OF FLIGHT 7267 CREW REPORTED STABILIZER TRIM SYSTEM 1 AND 2 FAILURE MESSAGES. CREW DECLARED EMERGENCY AND RETURNED TO ORD. FLIGHT LANDED WITHOUT INCIDENT AND PASSENGERS DEPLANED NORMALLY. THE DISCONNECT SWITCHES WERE FOUND ENGAGED DUE TO FOD AND WERE CLEANED. A SATISFACTORY OPERATIONAL CHECK WAS PERFORMED AND AIRCRAFT RETURNED TO SERVICE.

Source: SDR 04003651 · FAA SDRS
J · 2002-01-22 Unresolved
ATA 3234

DURING CLIMB OF THE FLIGHT FROM IAD TO GSP, THE CREW REPORTED THAT UPON LANDING GEAR RETRACTION HAD NO INDICATION OF GEAR RETRACTION ON THE FLIGHT DECK. THE THREE GREEN GEAR DOWN/LOCKED INDICATORS REMAINED ILLUMINATED. THE CREW REPORTED, RECEIVED ANTI-SKID OUTBOARD AND PARKING BRAKE SOV FAIL MESSAGES. MAINTENANCE PERSONNEL REMOVED AND REPLACED THE LANDING GEAR SELECTOR. LANDING GEAR EXTENSION/RETRACTION OPERATIONAL CHECKS WERE SATISFACTORY AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 02022651 · FAA SDRS