N66

BEECH 300 · 1987 · Valid Registration

Registered owner: FEDERAL AVIATION ADMINISTRATION, OK (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
FLIGHT PROGRAM OPERATIONS (RU3A)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

B · 2020-02-07 Matched by certificate designator
ATA 3454

ELECTRICAL SMELL NOTED DURING GROUND OPERATION FROM FLIGHT INSPECTION SYSTEM. #2 FLIGHT INSPECTION VOR/ILS RECEIVER FAILED AT SAME TIME ODOR WAS DETECTED.

Source: SDR RU3A202002107009 · FAA SDRS
J · 2020-02-01 Matched by certificate designator
ATA 2130

AIRCRAFT FAILED TO PRESSURIZE DURING CLIMBOUT

Source: SDR RU3A20200201008 · FAA SDRS
O · 2018-08-08 Matched by certificate designator
ATA 5740

A CRACK WAS FOUND IN THE RADIUS OF A LEFT WING ROOT RIB ATTACH CHANNEL. REPAIRED IAW EO 18-28-40, MAJOR REPAIR.

Source: SDR RU3A201808098035 · FAA SDRS
O · 2017-10-27 Matched by certificate designator
ATA 3240

BRAKES WEAK. REMOVED AND REPLACED ALL FOUR BRAKE ASSEMBLIES.

Source: SDR RU3A20171102036 · FAA SDRS
J · 2017-05-25 Matched by certificate designator
ATA 6120

LEFT PROPELLER PITCH LIGHT ILLUMINATED INTERMITTENTLY DURING FLIGHT,

Source: SDR RU3A20170525011 · FAA SDRS
F · 2016-12-09 Matched by certificate designator
ATA 6120

DURING APPROACH TO FULL-STOP LANDING, ATTEMPTED TO ADVANCE PROP LEVERS FROM 1500 RPM SETTING TO 1700 RMP. PROP LEVERS WOULD NOT ADVANCE FURTHER THAN 1540 RPM. BOTH PROP LEVERS WERE EXERCISED AND BINDING RELEASED.

Source: SDR RU3A20161209013 · FAA SDRS
O · 2014-02-28 Matched by certificate designator
ATA 5330

SEVERE CORROSION ON LOWER FUSELAGE SKIN & ANTENNA DOUBLER AT APPROXIMATELY STATION 265.75.

Source: SDR RU3A20140228008 · FAA SDRS
O · 2009-08-17 Matched by certificate designator
ATA 5540

DURING D-CHECK DISCOVERED RUDDER CRACKED AT LOWER HINGE, LT ATTACH BOLT HOLE.

Source: SDR RU3A0913 · FAA SDRS
O · 2009-01-15 Matched by certificate designator
ATA 5610

PILOT NOT FLYING, NOTICED ENLARGED AREA OF DELAMINATION IN LOWER LEFT CORNER OF RIGHT WINDSHIELD. FLIGHT WAS ABOUT 50 NM NORTHWEST OF AIRPORT AT FL 230 WHEN THE PROBLEM WAS NOTICED. FLIGHT DIVERTED BACK TO AIRPORT UNEVENTFULLY.

Source: SDR RU3A0902 · FAA SDRS
X · 2007-05-18 Matched by certificate designator
ATA 7320

APPROXIMATELY 2 TO 2 1/2 MINUTES AFTER TAKEOFF, NOTICED THE LEFT TORQUE GAUGE GOES TO APPROX 10 PERCENT OR LESS, FOLLOWED BY THE LEFT NO FUEL TRANSFER LIGHT ILLUMINATING, FOLLOWED BY THE AIRCRAFT YAWING TO THE LEFT AND THEN THE OTHER ENGINE GAUGES REFLECTING THE LEFT ENGINE FAILED. NO FIRE LIGHT WAS ILLUMINATED. UNEVENTFUL SINGLE ENGINE LANDING ACCOMPLISHED. REPLACED THE LEFT ENGINE PY LINE GOING TO THE PROP GOVERNOR WITH SERVICEABLE ASSEMBLY P/N 3032125. GROUND RUN OPS CHECKED GOOD.

Source: SDR RU3A0703001 · FAA SDRS
C · 2004-06-25 Matched by certificate designator
ATA 7200

WHILE CONDUCTING CLEARANCE BELOW PATH RUN, A PAIR OF PIGEONS DIVED AND STRUCK LEFT ENGINE AREA. HEARD A THUMP AND ALL CREW MEMBERS STARTED NOTICING A BURNING SMELL. NO ABNORMAL ENGINE INDICATIONS WERE OBSERVED. CREW REQUESTED IMMEDIATE LANDING AND WAS GIVEN A LANDING CLEARANCE. AIRCRAFT LANDED WITHOUT INCIDENT, TAXIED CLEAR OF RUNWAY AND SHUTDOWN. FIRE DEPARTMENT CHECKED AC AND RELEASED IT TO BE TOWED. PIGEON REMAINS WERE FOUND ON THE LEFT ENGINE INTAKE, INSIDE THE ENGINE IN THE SCREEN, ON THE LEFT WING LEADING EDGE, AND ON THE RT SIDE OF THE RUDDER.

Source: SDR RU32004F00000 · FAA SDRS
J · 2003-01-10 Matched by certificate designator
ATA 3234

ON 12/31/2002, REPLACED LANDING GEAR CONTROL SWITCH. SWITCH S/N 1669A, WAS INSTALLED AND SYSTEM CYCLED THREE TIMES WITH NO APPARENT PROBLEM. ON 1/09/2003, AIRCRAFT LEFT FOR MAINTENANCE TEST FLIGHT BECAUSE RIGHT ELEVATOR HAD BEEN REMOVED AND REINSTALLED AFTER BALANCE CHECK AFTER HARDWARE REPLACEMENT. ON TAKEOFF RELEASE LEVER FAILED TO RETRACT SO GEAR HANDLE COULD BE RAISED NORMALLY. WHEN CHECKED ON JACKS WITH SQUAT SWITCH DISCONNECTED RELEASE STILL DID NOT OPERATED. REMOVED FROM AIRCRAFT AND TRIED AGAIN ANS WITH JUMPER WIRES UNIT STILL FAILED TO RELEASE SO LEVER COULD BE RAISED. THIS CONTROL SWITCH FAILED ON THE FOURTH TIME IT WAS OPERATED SINCE LAST REPAIR. SWITCH WAS REPLACED AND PROBLEM CORRECTED. (M)

Source: SDR RU3A03002 · FAA SDRS