N697AM

BELL HELICOPTER TEXTRON CANADA 407 · 2015 · Valid Registration

Registered owner: AIR METHODS LLC, CO (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AIR METHODS LLC (QMLA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2025-03-17 Matched by certificate designator
ATA 6320

INTERMITTENT TRANSMISSION CHIP LIGHT IN FLIGHT. FOUND SMALL SLIVERS ON LOWER CHIP DETECTOR. AMOUNT AND TYPE CONSIDERED NEGLIGIBLE. - CHANGED FILTER.

Source: SDR QMLA2025031720036 · FAA SDRS
J · 2024-06-26 Matched by certificate designator
ATA 7200

ENGINE CHIP LIGHT ON TAKE OFF. ENGINE CHANGE INITIATED.

Source: SDR QMLA2024062620074 · FAA SDRS
J · 2024-04-13 Matched by certificate designator
ATA 6320

MAIN TRANSMISSION CHIP LIGHT ILLUMINATED IN FLIGHT DURING CLIMB SHORTLY AFTER TAKEOFF. PILOT ABORTED FLIGHT AND RETURNED TO THE BASE. MECHANIC PERFORMED UNWANTED PARTICLE INSPECTION AND FOUND ONE SLIVER. NORMAL FINDINGS AFTER MAJOR MAINTENANCE (MAST REPLACEMENT) IAW BH407GX MM DMC-407-A-63-00-00-01A-310A-A TABLE 1. NO ACTION REQUIRED. HOWEVER, MECHANIC PERFORMED DRAIN AND FLUSH, CHANGED TRANSMISSION OIL FILTER. PILOT PERFORMED GROUND RUN AFTERWARDS WITH NO FURTHER CHIP INDICATIONS.

Source: SDR QMLA2024042220040 · FAA SDRS
B · 2024-03-21 Matched by certificate designator
ATA 2170

DURING FLIGHT, PILOT EXPERIENCE SMOKE COMING FRONG THE COCKPIT AC VENTS. PERFORMED PRECAUTIONARY LANDING AT HUNTER ARMY AIRFIELD, GA. 3/21/2024 APPROX 1700. MECHANIC PERFORMED A VISUAL INSPECTION OF THE AC EVAPORATOR BLOWERS AND CONFIRMED THAT THE RH FWD EVAPORATOR BLOWER MOTOR HAD FAILED. DEFERRED IAW AMC MEL 2140-02.2 CATEGORY C REV 22 DATED 02/12/2019. PARTS PLACED ON ORDER UNDER MR-020421-24.

Source: SDR QMLA2024032120032 · FAA SDRS
J · 2023-12-24 Matched by certificate designator
ATA 7200

DURING RETURN FLIGHT FROM PATIENT DROP OFF ENGINE CHIP WARNING LIGHT ILLUMINATED. LANDED WITHOUT ISSUE. MECHANIC REMOVED CHIP DETECTOR AND FOUND MULTIPLE METAL PARTICLES AND PARTICLES IN FILTER. PERFORMED DRAIN AND FLUSH AND ATTEMPTED 30 MIN PENALTY RUN. ENGINE WAS MAKING LOUD HIGH PITCHED NOISE AND AIRCRAFT WAS SHAKING VIOLENTLY. PERFOMED NORMAL SHUT DOWN AND REINSPECTED CHIP DETECTORS AND FOUND MORE METAL PARTICLES. REPLACED ENGINE WITH SN CAE-848586 IAW BH407GX MM DMC-407-A-71-00-00-00A-720A-A ISSUE 002 - 2021. MOC OK. AIRCRAFT RETURNED TO SERVICE.

Source: SDR QMLA2023122620120 · FAA SDRS
J · 2019-04-26 Matched by certificate designator
ATA 7200

DURING 2ND START OF THE DAY WITH PATIENT AND MEDICAL CREW LOADED, WITH ENGINE AT GROUND IDLE, ENG CHIP CAUTION ILLLUMINATED, EXTINGUISHED, THEN REAPPEARED. AIRCRAFT WAS SHUT DOWN AND MAINTENANCE NOTIFIED. AIRCAFT WAS PLACED OUT OF SERVICE FOLLOWING INSPECTION OF MAGNETIC CHIP DETECTORS BY BASE MECHANIC.

Source: SDR QMLA2019043059043 · FAA SDRS