N71

BEECH 300 · 1988 · Valid Registration

Registered owner: FEDERAL AVIATION ADMINISTRATION, OK (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
FLIGHT PROGRAM OPERATIONS (RU3A)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

K B · 2021-10-05 Matched by certificate designator
ATA 2810

DEFECT: STRONG FUEL SMELL/ODOR AFTER TAKE-OFF, ACFT DECLARED IFE AND RETURNED BACK TO DEPARTURE AIRPORT (BNA). MXC PLAN: N71’S RT AUX FUEL BLADDER WAS JUST REPLACED. LOCATING LOCAL MX TO INSPECT FOR FUEL LEAKS.

Source: SDR RU3A2021100600014 · FAA SDRS
Z · 2020-10-05 Matched by certificate designator
ATA 3213

RIGHT MAIN LANDING GEAR COLLAPSED ON LANDING ROLLOUT.

Source: SDR RU3A2020100500032 · FAA SDRS
O · 2019-12-13 Matched by certificate designator
ATA 5313

MAJOR REPAIR ENGINEERING ORDER TO REPAIR DAMAGE FOUND DURING INSPECTION IN THE WEB OF STRINGER CAUSED BY SCREW THREADS, WHICH IMPINGED ON THE STRINGER WEB DUE TO AN IMPROPERLY LOCATED NUTPLATE

Source: SDR RU3A201912163074 · FAA SDRS
J · 2019-10-18 Matched by certificate designator
ATA 2820

RT FUEL XFER AMBER LIGHT CAME ON IN FLIGHT LONG WITH LOW PRESSURE LIGHT. MAINTENANCE REPLACED RIGHT ENGINE LOW FUEL PRESSURE SWITCH.

Source: SDR RU3A201910218053 · FAA SDRS
J · 2018-05-29 Matched by certificate designator
ATA 3610

RIGHT BLEED AIR FAIL ILLUMINATED IN FLIGHT, WENT OUT DURING DESCENT. FOUND EVA TUBING CHAFED ON THE METAL TAPE AROUND BLEED LINE, OTBD OF RT INBD WING. NO EVIDENCE OF BLEED AIR LEAK. REPAIRED WITH SPLICE TUBE.

Source: SDR RU3A2018053029023 · FAA SDRS
O · 2017-09-07 Matched by certificate designator
ATA 5312

UPPER LEFT ZONE OF AFT PRESSURE BULKHEAD IS GOUGED. REPAIRED IAW EO 15-28-10.

Source: SDR RU3A20170907027 · FAA SDRS
O · 2017-09-07 Matched by certificate designator
ATA 5312

MID RIGHT ZONE OF THE AFT PRESSURE BULKHEAD IS GOUGED. REPAIRED IAW EO 15-28-10.

Source: SDR RU3A20170907028 · FAA SDRS
O · 2017-09-06 Matched by certificate designator
ATA 5312

UPPER RIGHT ZONE OF THE AFT PRESSURE BULKHEAD IS GOUGED. REPAIRED IAW EO 15-28-10.

Source: SDR RU3A20170907026 · FAA SDRS
J · 2015-09-25 Matched by certificate designator
ATA 2120

LEFT BLEED AIR FAIL & MASTER CAUTION ILLUMINATED. WARNING LIGHT EXTINGUISHED AFTER COMPLETING IMMEDIATE ACTION ITEMS. FOUND EVA TUBING IN NEED OF REPAIR. REPAIRED TUBING. NO FURTHER ACTION REQUIRED.

Source: SDR RU3A20150925018 · FAA SDRS
N · 2015-09-18 Matched by certificate designator
ATA 2613

RIGHT BLEED AIR FAIL & MC ILLUMINATED. A HOLE WAS DISCOVERED IN THE EVA SENSE LINE IN RT NACELLE LE. LINE WAS REPLACED WITH NO DEFECTS NOTED.

Source: SDR RU3A20150918019 · FAA SDRS
J · 2015-02-05 Matched by certificate designator
ATA 5210

CABIN DOOR ANNUNCIATOR ILLUMINATED DURING FLIGHT. ADJUSTED CABIN DOOR LOCK SWITCH.

Source: SDR RU3A20140205007 · FAA SDRS
J · 2015-02-04 Matched by certificate designator
ATA 7500

WITH RT BLEED AIR PNEUMATIC ENV OFF, RT BLEED FAIL LIGHT INTERMITTENT ON & OFF. FOUND & REPLACED RUPTURED EVA TUBE.

Source: SDR RU3A20140204006 · FAA SDRS
O · 2014-04-01 Matched by certificate designator
ATA 5330

CRACKS SUSPECTED IN FUSELAGE SKIN VERIFIED BY NDT. THE DAMAGED AREA IS LOCATED INBD OF STRINGER 14L & NEAR FRAME 177.5. THE TWO FORE AFT CRACKS IN THE BELLY SKIN ARE APPROX 3.5 INCHES LONG & RUN FROM APPROX 1.5 INCH AFT TO 1.8 INCH FWD OF FRAME 177.5 & ARE ROUGHLY 1 INCH INBD OF STRINGER 14LH. THE SIDE TO SIDE CRACK IN THE SKIN UNDER FRAME 177.5 RUNS FROM ROUGHLY 1.5 INCH INBD TO 3.5 INCH INBD OF STRINGER 14LH. THE CRACK IN THE FS 177.5 FRAME IS IN THE BEND RADIUS BETWEEN THE WEB & CHORD & RUNS APPROX 4 INCH INBD FROM THE STRINGER 14LH. REPAIRED USING EO.

Source: SDR RU3A20140401037 · FAA SDRS
N · 2011-01-20 Matched by certificate designator
ATA 3260

ON APPROACH, LANDING GEAR EXTENDED. LANDING GEAR APPEARED TO EXTEND NORMALLY, HOWEVER RIGHT MAIN GEAR INDICATED UNSAFE (GREEN DOWN AND LOCKED LIGHT NOT ILLUMINATED). ATC ADVISED OF INTENTION TO HOLD WEST OF AIRPORT IN ORDER TO UTILIZE "LANDING GEAR UNSAFE INDICATION" ABNORMAL CHECKLIST. EXECUTED LANDING GEAR MANUAL EXTENSION IAW CHECKLIST. FLIGHT CREW DECLARED AN EMERGENCY AND REQUESTED CRASH/FIRE/RESCUE EQUIPMENT. REQUESTED AND RECEIVED CLEARANCE FOR FLY-BY. TOWER ADVISED THAT RIGHT MAIN LANDING GEAR APPEARED TO BE DOWN AND IN PLACE. AN UNEVENTFUL LANDING FOLLOWED. MAINTENANCE FOUND RIGHT MAIN GEAR DOWN GREEN LIGHT BULB BAD. INSTALLED NEW BULB. JACKED AIRCRAFT AND PERFORMED MLG RETRACTION. OPS CHECKED GOOD.

Source: SDR RU3A1101 · FAA SDRS
J · 2007-07-18 Matched by certificate designator
ATA 3150

DURING FLARE FOR LANDING, THE AIRCRAFT ABRUPTLY AND WITHOUT WARNING YAWED HARD RIGHT. TOUCHDOWN OCCURRED DURING THE GO-AROUND. THE PILOT NOT FLYING REPORTED THAT THE RIGHT PROP PITCH LIGHT ILLUMINATED IMMEDIATELY PRIOR TO THE EXCURSION. AFTER THE GO-AROUND, THE PROPELLERS WERE RESET TO 1500 RPM AND A POWER-ON APPROACH TO LANDING WAS ACCOMPLISHED. DURING THAT TOUCHDOWN, THE RIGHT PROP PITCH LIGHT ILLUMINATED AGAIN.

Source: SDR RU3A0706 · FAA SDRS
J · 2007-05-16 Matched by certificate designator
ATA 6120

RT PROP PITCH LIGHT ILLUMINATED IN FLIGHT. AIRCRAFT YAWED RIGHT. POWER INCREASED TO MAINTAIN CONTROL. WHEN RETURNED TO IDLE FOR LANDING IT WAS OK. TROUBLESHOT AND NO FAULT FOUND. DURING FLARE FOR LANDING, RT PROP APPEARED TO GO INTO GROUND RANGE, NO PROP PITCH LIGHT NOTED. AFTER LANDING, CONDUCTED GND IDLE LOW PITCH CHECK PER CFM, NO ANOMALY NOTED. ADJUSTED BETA RODS AND SET FLIGHT IDLE TORQUE. ALL CHECKS NORMAL.

Source: SDR RU3A0702 · FAA SDRS
O · 1999-12-10 Matched by certificate designator
ATA 3234

LANDING GEAR FAILED TO EXTEND WHEN 'GEAR DOWN' SELECTED.. RESULTED IN EMERGENCY EXTENSION OF LANDING GEAR. THE MICRO-SWITCH IN THE LANDING GEAR CONTROL SWITCH ASSEMBLY WAS FOUND TO BE STICKING. THE LANDING GEAR CONTROL SWITCH WAS REPLACED AND SYSTEM OPERATED NORMALLY. (M)

Source: SDR RU3A99014 · FAA SDRS
P · 1995-03-28 Matched by certificate designator
ATA 3260

PRECAUTIONARY LANDING WAS MADE AFTER NOSE AND RT MLG LIGHTS FAILED TO LIGHT DURING MANUAL EXTENSION. LIGHT BULBS IN GEAR LIGHTS WERE FOUND BURNED OUT. LIGHT BULBS WERE REPLACED AND GEAR WAS OPERATIONALLY CHECKED THROUGH 6 CYCLES, CHECKED OKAY. COMPONENT PN 3086070843004. (X)

Source: SDR RU3A95005 · FAA SDRS