N713WT

PIPER PA-31-350 · 1977 · Valid Registration

Registered owner: WTW AIR LLC, TX (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
Starflite Management Group, Inc. (T8VA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2019-04-01 Matched by certificate designator
ATA 3260

GEAR NOT LOCKED LIGHT ILLUMINATED. FOUND LEFT UPLOCK ROD ASSEMBLY WOULD NOT EXTEND AND ALLOW HOOK TO FULLY CAPTURE ROLLER ON LOWER STRUT ASSEMBLY. CLEANED INSPECTED AND UPLOCK ROD ASSEMBLY, CYCLED GEAR SEVERAL CYLES ON JACKS AND FOUND OPERATION SATISFACTORY.

Source: SDR T8VA2019040200001 · FAA SDRS
R J · 2017-10-19 Matched by certificate designator
ATA 6122

DURING SETUP FOR APPROACH TO LANDING STALL, RIGHT ENGINE FAILED AND WAS SECURED. EMERGENCY WAS DECLARED AND AIRCRAFT RETURNED TO DEPARTURE WITH NO FURTHER INCIDENT. MAINTENANCE DISCOVERED THAT THE WERE LITTLE TO NO CONTROL OF THE PROPELLER AND AFTER INVESTIGATION FOUND THAT THE TEETH ON THE GOVERNOR DRIVE GEAR HAD SHEARED.

Source: SDR T8VA20171121001 · FAA SDRS
C · 2015-07-12 Matched by certificate designator
ATA 3411

AIRCRAFT HIT A BIRD ON APPROACH DURING FAR 61/91 TRAINING. CREW ABANDONED APPROACH AND RETURNED WITH NO PROBLEMS. FOUND BENT RIGHT PITOT TUBE AND 1 LANDING/TAXI LIGHT BROKEN.

Source: SDR T8VA2015FA0000319 · FAA SDRS
J · 2013-02-15 Matched by certificate designator
ATA 3210

NO GREEN LIGHT INDICATION ON LT MAIN GEAR, JACKED ACFT AND FOUND GEAR FULLY DOWN AND SECONDARY LOCK NOT FULLY ENGAGED TO MAKE THE GEAR LOCKED SWITCH. REMOVED SECONDARY LOCK ASSY FOR INSPECTION. FOUND NO MECHANICAL DEFECTS. CLEANED AND LUBRICATED ALL PARTS AND REASSEMBLED SECONDARY LOCK. CONDUCTED MULTIPLE GEAR SWINGS WITH NO DISCREPENCIES AND RETURNED ACFT TO SERVICE.

Source: SDR T8VA20130215001 · FAA SDRS
J · 2013-02-15 Matched by certificate designator
ATA 3230

NO GREEN LIGHT INDICATION ON LT MAIN, JACKED ACFT AND FOUND GEAR FULLY DOWN AND SECONDARY LOCK NOT FULLY ENGAGED TO MAKE THE GEAR LOCKED SWITCH. REMOVED SECONDARY LOCK ASSY FOR INSPECTION. FOUND NO MECHANICAL DEFECTS. CLEANED AND LUBRICATED ALL PARTS AND REASSEMBLED SECONDARY LOCK. CONDUCTED MULTIPLE GEAR SWINGS WITH NO DISCREPENCIES AND RETURNED ACFT TO SERVICE.

Source: SDR 2013FA0000104 · FAA SDRS
R Y · 2012-06-05 Matched by certificate designator
ATA 8500

DURING CRUISE AT 7000FT, THE RIGHT ENGINE BEGAN RUNNING ROUGH AND LOOSING POWER. THE ENGINE STALLED OUT AND COMPLETELY SHUT DOWN. FOLLOWED AIRCRAFT CHECKLIST AND ATTEMPTED TO RESTART THE ENGINE UNSUCCESSFUL. SECURED FAILED ENGINE ACCORDINGLY TO THE AIRCRAFT CHECKLIST. DECLARED AN EMERGENCY AND MADE AN UNSCHEDULED LANDING AT THE NEAREST AIRPORT WITH OUT ANY FURTHER INCIDENTS OR INJURIES.

Source: SDR T8VA20120605002 · FAA SDRS