N72

BEECH 300 · 1988 · Valid Registration

Registered owner: FEDERAL AVIATION ADMINISTRATION, OK (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
FLIGHT PROGRAM OPERATIONS (RU3A)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2019-07-08 Matched by certificate designator
ATA 6123

NO AUTO FEATHER RT ENG DURING T/O ROLL.

Source: SDR RU3A20190709032 · FAA SDRS
J · 2019-02-22 Matched by certificate designator
ATA 2131

ALT WARN ANNUNCIATOR PASSING 12K, CABIN PRESSURE WAS 12K. PAX. 02 MASK DROPPED. UNABLE TO CONTROL CABIN ALTITUDE BELOW FLIGHT ALTITUDE. THE PRESSURE CONTROLLER WAS THE CAUSE. PRESSURE CONTROLLER WAS REPLACED. NO FURTHER ACTION REQUIRED.

Source: SDR RU3A20190222005 · FAA SDRS
O · 2019-01-24 Matched by certificate designator
ATA 5210

MS HEARD LOUD AIR-LEAK COMING FROM THE CABIN DOOR. NOISE INCREASED AS DIFFERENTIAL PRESSURE INCREASED. CABIN DOOR SEAL WAS REPLACED.

Source: SDR RU3A20190124002 · FAA SDRS
J · 2018-12-04 Matched by certificate designator
ATA 6140

RIGHT PROP PITCH ANNUNCIATOR ILLUMINATED IN FLIGHT. THE PROBLEM WAS SOLVED BY ADJUSTING THE PROXIMITY SWITCH. NO FURTHER ACTION REQUIRED.

Source: SDR RU3A20181204049 · FAA SDRS
B · 2018-09-30 Matched by certificate designator
ATA 3160

HOT SMELL/ FUMES IN COCKPIT AFTER BATTERY ON AND GEN TIES CLOSED. VERIFIED FUME/ELECTRICAL BURNT SMELL COMING FROM MFD. REMOVED AND REPLACED MFD.

Source: SDR RU3A2018100930046 · FAA SDRS
N · 2018-09-19 Matched by certificate designator
ATA 6140

RT PROP PITCH LIGHT ILLUMINATED IN FLIGHT CAUSED BY A FAULTY PROXIMITY SWITCH. PROXIMITY SWITCH WAS REPLACED. OPERATIONAL CHECK WAS GOOD.

Source: SDR RU3A2018092119041 · FAA SDRS
J · 2018-05-16 Matched by certificate designator
ATA 6140

RIGHT PROPELLER PITCH LIGHT ILLUMINATED AFTER TAKEOFF. REPLACED A FAULTY PROPELLER SWITCH. NO FURTHER ACTION REQUIRED.

Source: SDR RU3A201805216018 · FAA SDRS
J · 2018-05-14 Matched by certificate designator
ATA 3234

GEAR FAILED TO RETRACT. REPLACE FAULTY LANDING GEAR CONTROL HANDLE.

Source: SDR RU3A201805214015 · FAA SDRS
O · 2018-05-14 Matched by certificate designator
ATA 3234

GEAR FAILED TO RETRACT. REPLACED A FAULTY LANDING GEAR CONTROL HANDLE. NO FURTHER ACTION REQUIRED

Source: SDR RU3A201805184015 · FAA SDRS
O · 2017-10-03 Matched by certificate designator
ATA 5312

SCRATCH FOUND IN THE AFT PRESSURE BULKHEAD. REPAIRED IAW EO 15-28-16.

Source: SDR RU3A20171003032 · FAA SDRS
O · 2017-08-15 Matched by certificate designator
ATA 5330

LEFT-HAND FUSELAGE SKIN UNDER FORWARD WING TO BODY FAIRING CORRODED. MAJOR REPAIR ENGINEERING ORDER 17-28-43 "LOWER FUSELAGE MULTIPLE BAY SKIN REPAIR" ISSUED TO REPAIR THE CORROSION DAMAGE TO LOWER FUSELAGE SKIN BEHIND THE WING-TO-BODY FAIRING. THE DAMAGE EXTENDS OVER TWO BAYS FROM APPROXIMATELY FS188 TO FS202.

Source: SDR RU3A20170815024 · FAA SDRS
F · 2016-01-05 Matched by certificate designator
ATA 2731

AN INFLIGHT OUT OF TRIM SITUATION WHICH WAS DESCRIBED AS, AN EXCESSIVE NOSE UP PITCH, ON TAKEOFF REQUIRING AN IMMEDIATE ACTION. FOUND THE BRASS DRIVE GEAR LOOSE ON THE ELEVATOR TRIM WHEEL. THIS RESULTED IN THE TRIM POSITION INDICATING DIAL SLIPPING DURING TRIM WHEEL OPERATION & GIVING A FALSE INDICATION OF THE ELEVATOR TRIM TAB POSITION. MX SHOULD BE AWARE OF THE POSSIBILITY OF SLIPPAGE, BETWEEN THE ELEVATOR TRIM WHEEL & THE DIAL ASSEMBLY. A MX ADVISORY CONTAINING INSTRUCTIONS ON HOW TO CHECK FOR & CORRECT THIS HAS BEEN ISSUED.

Source: SDR RU3A20160105001 · FAA SDRS
J · 2014-01-22 Matched by certificate designator
ATA 3230

DURING CLIMB OUT AFTER ILS APPROACH, CREW NOTED RED LIGHTS IN THE GEAR HANDLE & A BLINKING LDG TAXI LIGHT CAUTION ADVISORY ANNUNCIATOR. THE LG RELAY CB WAS POPPED. VISUALLY CONFIRMED THE RT MLG WAS PARTIALLY UP. BEECH 300 POH ABNORMAL PROCEDURES FOLLOWED. UNSAFE INDICATION CORRECTED, ATC NOTIFIED. SAFE LANDING ACCOMPLISHED WITHOUT FURTHER INCIDENT. CHECKED ACFT ON GND & WAS UNABLE TO DUPLICATE PROBLEM.

Source: SDR RU3A20140127001 · FAA SDRS
B · 2010-10-07 Matched by certificate designator
ATA 2312

WHILE CONDUCTING AN ILS-1, STRONG ELECTRICAL FUMES (NO SMOKE) FILLED THE FUSELAGE. DETERMINED FUMES WERE EMANATING FROM FLIGHT INSPECTION PANEL. RAN SMOKE AND FUME ELIMINATION CHECKLIST AND EXECUTED IMMEDIATE LANDING. MAINTENANCE VHF COMM NR 3 WAS BURNED OUT.

Source: SDR RU3A1023 · FAA SDRS
B · 2010-07-07 Matched by certificate designator
ATA 2120

WHILE AT CRUISE, TECHNICIAN NOTICED A BURNING SMELL, WITHIN A FEW SECONDS SMOKE BEGAN TO FORM IN THE BACK OF THE AIRCRAFT. PIC DIRECTED EVERYONE TO DON OXYGEN AND RUN APPROPRIATE EMERGENCY CHECKLIST. CREW DECLARED EMERGENCY WITH ATC AND BEGAN VFR DESCENT TO CLOSEST SUITABLE AIRFIELD. LANDED UNEVENTFULLY WITHIN APPROX 5 MINUTES OF THE EMERGENCY. CLEARED THE RUNWAY AND EVACUATED AIRCRAFT. SOURCE OF SMOKE UNDETERMINED AT THIS TIME.

Source: SDR RU3A1017 · FAA SDRS
N · 2010-03-22 Matched by certificate designator
ATA 5270

WHILE CLIMBING TO EN ROUTE CRUISING ALTITUDE OF FL190, CABIN DOOR ANNUNCIATOR ILLUMINATED AT APPROXIMATELY 18,700 FT. EXECUTED EMERGENCY DESCENT AND "CABIN DOOR UNLOCK" EMERGENCY PROCEDURES. AT 9000 MSL CABIN DOOR ANNUNCIATOR EXTINGUISHED. AIRCRAFT LANDED UNEVENTFULLY. INSPECTION OF DOOR AFTER LANDING INDICATED IT WAS SECURELY LATCHED. MAINTENANCE FOUND UPPER AFT DOOR SWITCH OUT OF ADJUSTMENT. ADJUSTED AFT DOOR SWITCH. PRESSURIZED AIRCRAFT TO 6 PSI. DOOR WARNING SYSTEM CHECKED SAT.

Source: SDR RU3A1010 · FAA SDRS
O · 2010-02-05 Matched by certificate designator
ATA 5610

AFTER 45 MINUTES FROM DEPARTING JEFFERSON CITY, MO EN ROUTE TO OKC, OK AT FL260, THERE WAS A LOUD SOUND (LIKE A GUN SHOT) AND THE PILOT SIDE WINDSHIELD WAS SHATTERED WITH SHROUDS OF GLASS FALLING OUT. INFORMED KANSAS CITY CENTER AND REQUESTED IMMEDIATE DESCENT TO CLOSEST VFR AIRPORT WITH 6000 FT RUNWAY. ABNORMAL SHATTERED WINDSHIELD CHECKLIST PERFORMED AND PNF LANDED THE AIRCRAFT.

Source: SDR RU3A1004 · FAA SDRS
E R J · 2008-08-14 Matched by certificate designator
ATA 7200

CLIMBING THRU 7300`, AT CLIMB POWER, HEARD A PRONOUNCED POP, FELT THE ACFT YAW LT AND FELT A DECELERATION. THE PILOT FLYING CONFIRMED THAT THE LT ENGINE HAD SHUTDOWN AND THE PROP HAD FEATHERED. ATC WAS NOTIFIED AND EMERGENCY WAS DECLARED. THE ENGINE FAILURE IN FLIGHT EMERGENCY CHECKLIST WAS COMPLETED AS WELL AS THE SINGLE ENGINE LANDING CHECKLIST. AFTER AN UNEVENTFUL LANDING AND TAXI OFF OF THE RUNWAY, THE SHUTDOWN CHECKLIST WAS ACCOMPLISHED AND THE ACFT WAS TOWED TO THE HANGER. (K)

Source: SDR RU32008F00000 · FAA SDRS
B · 2007-08-08 Matched by certificate designator
ATA 3497

PILOT DU1 POPPED CB, CREW COULD DETECT BURNING EQUIPMENT ODOR. FOUND SHORTED WIRE AT CONNECTOR ON DISPLAY UNIT.

Source: SDR RU3A0707 · FAA SDRS
B · 2001-04-04 Matched by certificate designator
ATA 2120

ACRID FOUL SMELLING SMOKE PERMEATED CABIN, ENVIROMENTAL TEMP CIRCUIT BREAKER POPPED. DECLARED EMERGENCY AND DIVERTED. SMOKE DISSIPATED. CABIN TEMP INCREASED BECAUSE FORWARD AND AFT BLOWER MOTORS WERE INOPERATIVE. DID NOT REQUEST CRASH EQUIPMENT. LANDED UNEVENTFULLY. MECHANIC COULD NOT DUPLICATE AFTER 30 MINUTE RUN UP WITH CREW PRESENT. ALL SYSTEMS OPERATING. AIRCRAFT RETURNED TO AIRWORTHY CONDITION.

Source: SDR RU3A0101 · FAA SDRS