N770JS

CESSNA 525B · 2011 · Valid Registration

Registered owner: CREATIVE COMMUNICATIONS LLC, WV (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
EXCLUSIVE JETS LLC (3EJA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2024-07-06 Matched by certificate designator
ATA 2130

AFTER TAKEOFF, CLIMBING THROUGH 10,000 FEET WE RECEIVED A RED MASTER CAUTION LIGHT, AND A RED ILLUMINATED CABIN ALT LIGHT. WE RAN THE CHECKLIST. DISPATCH ADVISED US TO RETURN TO PBI. ATC WAS NOTIFIED AND NO EMERGENCY WAS DECLARED.

Source: SDR 3EJA2024070600003 · FAA SDRS
S · 2021-09-19 Matched by certificate designator
ATA 3241

ANTI-SKID LIGHT ILLUMINATED DURING FLIGHT. MAINTENANCE HAS FOUND LANDING GEAR HARNESS DAMAGED FROM BEING MISROUTED AND RUBBING ON TIRE.

Source: SDR 3EJA77009/19/21 · FAA SDRS
O · 2021-09-02 Matched by certificate designator
ATA 7320

#2 ENG SLOWLY ROLLED BACK ON DESCENT UNTIL NIL, COULD NOT RESTART. T/S AND REPLACED FDU. OPS CHECK SATISFACTORY.

Source: SDR 3EJA202109060001 · FAA SDRS
X J · 2021-08-02 Matched by certificate designator
ATA 7320

AS THE THROTTLES WERE DECREASED, THE RIGHT ENGINE N1 CONTINUED DECREASING AT A STEADY SLOW RATE UNTIL CUTOFF.REMOVED AND REPLACED THE RIGHT FUEL DELIVERY UNIT. OPS CK LEAK CHECK GOOD REF F544-31 MM 73-19-01

Source: SDR 3EJA2021080400001 · FAA SDRS
K J · 1999-07-26 Unresolved
ATA 2782

AIRCRAFT WAS FLYING TOUCH-AND-GO PATTERN WORK WHEN THE CREW NOTICED BUFFETING AND LOST THEIR AUX HYD SYSTEM. AFTER LANDING, DISCOVERED NR 6 SPOILER ACTUATOR UPPER MOUNT BOLT HAD SHEARED AND THE ACTUATOR DROPPED DOWN ONTO THE FOREFLAP. AFTER FLAPS WERE LOWERED AND RE-RAISED, THE ACTUATOR PUNCTURED THE FOREFLAP AND BOTH ACTUATOAR HYD B-NUTS WERE SNAPPED OFF CAUSING AUX HYD SYS FAILURE. DISCOVERED THE UPPER ACTUATOR ATTACH BOLT FITTING BUSHINGS WERE NOT INSTALLED AT SPOILER OVERHAUL CAUSING EXCESSIVE PLAY ON THE BOLT LEADING TO ITS FAILURE.

Source: SDR 99ZZZX3412 · FAA SDRS
O · 1995-06-13 Unresolved
ATA 5415

WHILE PERFORMING A C3 CHECK AND THE A.A.C.I.P. SB 3173, FOUND NR 2 AND NR 3 OVERWING FITTING CRACKED FORWARD OF FUSELAGE ATTACHMENT BOLT. INSTALLED NEW TYPE FITTING: NR 1, PYLON AT: ATT 51,029/ATC 20,325, FEB 91. NR 2 AND NR 3, ATT 52,324/ATC 20,629 MAY 95. NR 4, REPLACED, PREVENTIVE ONLY, MAY 95.

Source: SDR 95ZZZX3156 · FAA SDRS
O · 1995-06-13 Unresolved
ATA 5711

DURING A C-CHECK, THE RT WING FORWARD SPAR UPPER CHORD BETWEEN FSS 360 AND FSS 586 FOUND WITH CORROSION AROUND HI-LOCKS. PART REPLACED. ACFT TT 52,324.7 HOURS. ACFT TC 20,628 CYCLES.

Source: SDR 95ZZZX3155 · FAA SDRS
O · 1995-06-13 Unresolved
ATA 5711

DURING A C-CHECK, RT WING FORWARD SPAR LOWER CHORD, FSS 387-640, FOUND WITH CORROSION AROUND HI-LOCKS. PART REPLACED. ACFT TT 52,324.7 HOURS. ACFT TC 20,628 CYCLES.

Source: SDR 95ZZZX3152 · FAA SDRS
O · 1995-04-28 Unresolved
ATA 2752

PERFORMING A FLEET COMPANY INSPECTION, THE LT FILLET FLAP TRANSMISSION SUPPORT FITTING WAS FOUND CRACKED. SUPPORT FITTING IN THE PROCESS TO BE REPLACED IAW BOEING SIB 3251, REV. 2.

Source: SDR 95ZZZX2363 · FAA SDRS