N777DH

DEHAVILLAND DHC-2 · 1949 · Valid Registration

Registered owner: KALININ PARTNERS LLC, AK (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
KALININ AVIATION, LLC (P9KA)Certificate holderMatched by certificate designator

Accident & incident history

Accident · 1991-06-03 Unresolved
Cessna 210M Fatal injuryoperator not yet resolved
Source: NTSB case DEN91FA079

Maintenance disclosures

R J · 2016-03-23 Matched by certificate designator
ATA 2823

THE PILOT OF THE FLOAT-EQUIPPED ACFT DEPARTED ON A VFR CROSS COUNTRY FLIGHT. AS THE REAR TANK APPROACHED EMPTY, MOVED THE FUEL SELECTOR TO THE FRONT TANK POSITION. APPROXIMATELY 5 MINUTES LATER, THE FUEL PRESSURE LOW LIGHT ILLUMINATED, THE ENGINE LOST POWER, AND THE FUEL PRESSURE GAUGE DROPPED OUT OF THE GREEN ARC. THE PILOT ATTEMPTED TO SWITCH TANKS AGAIN BUT THE FUEL SELECTOR DID NOT FEEL RIGHT AND THERE WAS NO CHANGE IN FUEL PRESSURE. HE EXECUTED A POWEROFF LANDING ON THE WATER. CLOSER EXAMINATION REVEALED THAT THE FUEL SELECTOR CONTROL ASSY C2CE781A HAD BROKEN IN THE SHAFT C2CE780 AT 1 OF THE RIVETS SECURING THE HANDLE C2CE481 TO THE SHAFT, PREVENTING THE SELECTOR HANDLE FROM MOVING THE VALVE. THE CONTROL ASSEMBLY WAS REPLACED WITH SERVICEABLE. THE TIME ON THE CONTROL ASSY COULD NOT BE DETERMINED AND OUR INVESTIGATION IS ONGOING.

Source: SDR P9KA2016032301 · FAA SDRS
L · 2015-10-01 Matched by certificate designator
ATA 2562

DURING A ROUTINE ELT INSPECTION IAW 14 CFR 91.207, THE ELT G SWITCH WAS FOUND TO BE NON-FUNCTIONAL. THIS IS A RECURRING PROBLEM WITH THESE BEACONS.

Source: SDR P9KA2015103002 · FAA SDRS
O · 2011-07-20 Matched by certificate designator
ATA 8530

ON ENGINE SHUTDOWN A SUCKING SOUND WAS HEARD AS ENGINE DIED. CYLINDER COMPRESSION CHECK WAS 0/80. AFTER STAKING THE VALVE THE COMPRESSION WAS STILL 0/80. AIR WAS HEARD COMING FROM THE EXHAUST PIPE. AFTER REMOVING THE EXHAUST STACK FROM THE CYLINDER, A CRACK AROUND THE VALVE STEM WAS NOTICED BY THE MX. CYLINDER WAS REMOVED FROM THE ACFT AND A SERVICEABLE CYLINDER WAS INSTALLED. VALVE WAS REMOVED FROM CYLINDER AND A CRACK WAS SEEN AROUND ABOUT 2/3 OF THE VALVE FACE. THE VALVE REMAINED INTACT.

Source: SDR P9KA2011F00167 · FAA SDRS
O · 2007-12-12 Matched by certificate designator
ATA 8530

CYLINDER CRACKED IN THE AREA OF EXHAUST VALVE.

Source: SDR 2008FA0000042 · FAA SDRS