KALININ AVIATION, LLC

Part 135 operator · designator P9KA

Data confidence: Records are linked by certificate number, aircraft registration, or a name match that a reviewer has confirmed. Each record below shows how it was linked.

Also recorded as: ALASKA SEAPLANES, KALININ AVIATION, LLC, KALININ PARTNERS LLC., Kalinin Aviation, LLC

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

Acc · 2017-08-14 Operator named in NTSB report
CESSNA T207 (N745KP) None injury Part 135

Operated by Kalinin Aviation, LLC (per NTSB report)

Source: NTSB case ANC17LA043

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

33 reports on file.

G · 2020-02-07 Matched by certificate designator
N749KP · ATA 8530

ON ENGINE 100 HOUR IT WAS FOUND THAT 4 OF THE 6 CYLINDERS WERE CRACKED. ALL WERE EMANATING FROM THE UPPER SPARK PLUG HOLE TO THE FUEL NOZZLE HOLE

Source: SDR 2020F00131 · FAA SDRS
O · 2017-03-22 Matched by certificate designator
N749KP · ATA 8550

DURING A ROUTINE 100 HOUR INSPECTION, THE OIL COOLER FORWARD DIAGONAL SUPPORT BAR WAS FOUND BROKEN IN TWO, WITH THE LOWER HALF LYING ON THE ENGINE BAFFLING. UPON REMOVAL OF THE COOLER, 2 OTHER CRACKS WERE FOUND NEAR THE MOUNTING BOLT HOLES. THE COOLER WAS REPLACED WITH NEW.

Source: SDR P9KA2017032801 · FAA SDRS
O · 2017-01-30 Matched by certificate designator
N1265U · ATA 5540

DURING A ROUTINE ANNUAL INSPECTION, THE RUDDER TORQUE TUBE WAS FOUND TO HAVE CORROSION ON MULTIPLE AREAS INSIDE THE RUDDER. RUDDER TORQUE TUBE CORROSION IS ADDRESSED IN CAB06-2, BUT THERE ARE 2 PROBLEMS WITH THAT CAB. FIRST, THERE IS NO INSTRUCTION IN THE CAB (OR IN THE CURRENT REVISION OF THE CESSNA MAINTENANCE MANUAL) TO DO REPEATING INSPECTIONS ON THE RUDDER TORQUE TUBE ESPECIALLY UP INSIDE THE RUDDER THROUGH THE ACCESS HOLE ADDED BY CAB06-2, JUST A ONE-TIME MODIFICATION, INSPECTION, AND IF NECESSARY REPLACEMENT OF THE RUDDER TORQUE TUBE. SECOND, THIS AIRCRAFT IS OUTSIDE OF THE APPLICABILITY RANGE OF CAB06-2. THE AIRCRAFT IS OPERATED ON FLOATS FROM SALT WATER. SUGGEST THAT THE MANUFACTURER'S MAINTENANCE MANUAL INCORPORATE A RECURRING INSPECTION AND APPLICATION OF CORROSION-PREVENTION COMPOUND TO THE RUDDER TORQUE TUBE AT LEAST FOR AIRCRAFT OPERATED ON FLOATS.

Source: SDR P9KA17020803 · FAA SDRS
O · 2017-01-30 Matched by certificate designator
N1265U · ATA 2731

DURING ROUTINE INSPECTION, THE LEFT ELEVATOR TRIM ACTUATOR WAS FOUND TO HAVE MULTIPLE PARTS CORRODED BEYOND LIMITS. THE ACTUATOR HAD APPROXIMATELY 800 HOURS AND 12 MONTHS SINCE LAST DISASSEMBLY, INSPECTION, AND LUBRICATION.

Source: SDR P9KA2017020801 · FAA SDRS
O · 2016-11-11 Matched by certificate designator
N755KP · ATA 7230

ROUTINE SOAP SAMPLE WAS FLAGGED FOR M50 STEEL (BEARING MATERIAL) IN FILTER. ENGINE WAS REMOVED AND SENT TO A REPAIR STATION, WHERE IT WAS FOUND THAT THE COMPRESSOR BEARING WAS FAILING. THE ENGINE WAS REPAIRED AND REINSTALLED AND THE AIRCRAFT RETURNED TO SERVICE.

Source: SDR P9KA2017020804 · FAA SDRS
K · 2016-05-08 Matched by certificate designator
N749KP · ATA 8520

DURING A ROUTINE ANNUAL INSPECTION, AN ONGOING OIL LEAK WAS TRACED TO A CRACK IN THE RIGHT HALF OF THE CRANKCASE BETWEEN THE NR 5 CYLINDER AND THE ALTERNATOR MOUNTING BOSS. THE ENGINE WAS REPLACED.

Source: SDR P9KA2016070701 · FAA SDRS
R J · 2016-03-23 Matched by certificate designator
N777DH · ATA 2823

THE PILOT OF THE FLOAT-EQUIPPED ACFT DEPARTED ON A VFR CROSS COUNTRY FLIGHT. AS THE REAR TANK APPROACHED EMPTY, MOVED THE FUEL SELECTOR TO THE FRONT TANK POSITION. APPROXIMATELY 5 MINUTES LATER, THE FUEL PRESSURE LOW LIGHT ILLUMINATED, THE ENGINE LOST POWER, AND THE FUEL PRESSURE GAUGE DROPPED OUT OF THE GREEN ARC. THE PILOT ATTEMPTED TO SWITCH TANKS AGAIN BUT THE FUEL SELECTOR DID NOT FEEL RIGHT AND THERE WAS NO CHANGE IN FUEL PRESSURE. HE EXECUTED A POWEROFF LANDING ON THE WATER. CLOSER EXAMINATION REVEALED THAT THE FUEL SELECTOR CONTROL ASSY C2CE781A HAD BROKEN IN THE SHAFT C2CE780 AT 1 OF THE RIVETS SECURING THE HANDLE C2CE481 TO THE SHAFT, PREVENTING THE SELECTOR HANDLE FROM MOVING THE VALVE. THE CONTROL ASSEMBLY WAS REPLACED WITH SERVICEABLE. THE TIME ON THE CONTROL ASSY COULD NOT BE DETERMINED AND OUR INVESTIGATION IS ONGOING.

Source: SDR P9KA2016032301 · FAA SDRS
O · 2016-02-24 Matched by certificate designator
N93021 · ATA 5751

DURING ROUTINE MX, THE RT OTBD AILERON HINGE BRACKET, PN 1220052-18, WAS FOUND TO BE CRACKED THROUGH THE BEND RADIUS OF THE LOWER INBD FLANGE. THE PART WAS REPLACED WITH NEW. THIS IS THE 2ND HINGE BRACKET WE HAVE FOUND CRACKED ON THIS ACFT & THE 4TH IN OUR FLEET. BELIEVE THAT IN THIS CASE THAT THE CRACKING IS A RESULT OF SIMPLE FATIGUE DUE TO THE HIGH NR OF HOURS, EXTENSIVE LOW LEVEL OPERATION & HIGH CYCLES PER HOUR. WE HAVE INSTITUTED A REPEATING DETAILED VISUAL INSPECTION OF ALL AILERON HINGE BRACKETS ON OUR 206 & 207 FLEET FOR ACFT OVER 10000 HOURS TOTAL TIME.

Source: SDR P9KA2016030301 · FAA SDRS
Y · 2015-12-06 Matched by certificate designator
N93021 · ATA 7414

PILOT REPORTED ENG DIED WHEN IGNITION SWITCH MOVED TO LT POSITION. TROUBLESHOOTING REVEALED LT MAGNETO INOPERATIVE. REPLACED LT MAGNETO WITH SERVICEABLE, ALL CHECKED SATISFACTORY. PRELIMINARY INSPECTION SHOWED LT MAGNETO POINTS NOT OPENING, POSSIBLY DUE TO EXCESSIVE CAM FOLLOWER WEAR. THE MAGNETO ONLY HAD 107.6 HOURS SINCE 500 HOUR INSPECTION.

Source: SDR P9KA2015120804 · FAA SDRS
K B · 2015-12-04 Matched by certificate designator
N1301L · ATA 2810

THE ACFT WAS WRITTEN UP & INVESTIGATED MULTIPLE TIMES DUE TO FUEL SMELL IN THE CABIN. AFTER SEVERAL ATTEMPTS TO FIX THE PROBLEM, PROCESS OF ELIMINATION LED TO THE RT WING TANK LEAKING. BECAUSE THE ACFT HAD A FIBERGLASS TANK INSTALLED, THE WING & BUTT RIB HAD TO BE REMOVED TO VERIFY THIS. ON REMOVAL OF THE TANK, 3 AREAS WERE FOUND WITH EVIDENCE OF SUBSTANTIAL LEAKAGE & 3 OR 4 OTHER SMALL SEEPS. BECAUSE OF THE DIFFICULTIES INVOLVED WITH INSPECTING & ACCESSING THE FIBERGLASS TANK FOR REPAIR, IT WILL BE REPLACED WITH THE OEM STYLE FUEL BLADDERS. SUSPECT LEAKS WERE DUE TO THE AGE OF THE TANK & OR POOR QUALITY CONTROL FROM THE MFG LEADING TO POROUS SPOTS IN THE RESIN, BECAUSE THERE WAS NO VISIBLE INDICATION OF CRACKS AT THE LEAK LOCATIONS.

Source: SDR P9KA2015120801 · FAA SDRS
K · 2015-12-04 Matched by certificate designator
N1301L · ATA 2810

DUE TO LEAKAGE OF THE RT WING TANK, THE LT WING WAS REMOVED TO ACCESS & INSPECT IT'S FIBERGLASS TANK. ON TANK REMOVAL, IT WAS FOUND TO HAVE ONE LOCATION OF APPARENT CRACKING & LEAKAGE. DUE TO THE DIFFICULTIES INVOLVED IN ACCESSING THESE TANKS FOR INSPECTION OR REPAIR, THIS TANK WILL BE REPLACED WITH AN OEM STYLE FUEL BLADDER.

Source: SDR P9KA2015120802 · FAA SDRS
L · 2015-10-28 Matched by certificate designator
N4794C · ATA 2562

DURING A ROUTINE ELT INSPECTION IAW 14 CFR 91.207, THE G SWITCH WAS FOUND TO BE INOPERATIVE. THIS IS A RECURRING PROBLEM WITH THESE BEACONS.

Source: SDR P9KA2015103003 · FAA SDRS
L · 2015-10-28 Matched by certificate designator
N7687K · ATA 2562

DURING A ROUTINE ELT INSPECTION IAW 14 CFR 91.207, THE ELT G SWITCH WAS FOUND TO BE INOPERATIVE. THIS IS A RECURRING PROBLEM WITH THESE BEACONS.

Source: SDR P9KA2015103004 · FAA SDRS
L · 2015-10-15 Matched by certificate designator
N8216T · ATA 2562

DURING A ROUTINE ELT INSPECTION IAW 14 CFR 91.207, THE ELT G SWITCH WAS FOUND TO BE INTERMITTENT. THIS IS A RECURRING PROBLEM WITH THESE UNITS.

Source: SDR P9KA2015103005 · FAA SDRS
K · 2015-10-08 Matched by certificate designator
N1265U · ATA 6122

PILOT REPORTED ENG OIL DOWN BELLY OF ACFT. FIRST TROUBLESHOOTING WAS TIGHTENING AN OIL FLEX HOSE THAT WAS SLIGHTLY LOOSE, NO CHANGE. FURTHER INSPECTION REVEALED OIL LEAKING AT BASE OF PROPELLER GOVERNOR. GOVERNOR WAS REMOVED & GOVERNOR BASE GASKET CHANGED, STILL LEAKING OIL. FINALLY A THOROUGH CLEANING & INSPECTION WITH A BLACK LIGHT REVEALED THAT THE GOVERNOR ITSELF WAS LEAKING. THE GOVERNOR WAS REPLACED WITH AN OVERHAULED UNIT WITH NO FURTHER LEAKAGE NOTED.

Source: SDR P9KA2015103001 · FAA SDRS
O · 2015-10-07 Matched by certificate designator
N1301L · ATA 6122

DURING A PREFLIGHT RUN UP, THE GOVERNOR WOULD NOT CYCLE THE PROPELLER EVEN WHEN LT IN THE LOW RPM POSITION FOR 10+ SECONDS. THE PROPELLER GOVERNOR WAS REPLACED WITH SERVICEABLE & OPERATIONS WERE NORMAL. THE GOVERNOR ONLY HAD 29.5 HOURS SINCE OVERHAUL & THE REPAIR STATION WAS UNABLE TO DUPLICATE THE ISSUE WHEN THE GOVERNOR WAS RETURNED TO THEM. SUSPECT INTERMITTENT TEMP RELATED PROBLEM WITH GOVERNOR.

Source: SDR P9KA2015120803 · FAA SDRS
L · 2015-10-01 Matched by certificate designator
N777DH · ATA 2562

DURING A ROUTINE ELT INSPECTION IAW 14 CFR 91.207, THE ELT G SWITCH WAS FOUND TO BE NON-FUNCTIONAL. THIS IS A RECURRING PROBLEM WITH THESE BEACONS.

Source: SDR P9KA2015103002 · FAA SDRS
O · 2015-09-14 Matched by certificate designator
N1265U · ATA 3457

NEITHER GPS WOULD ACQUIRE POSITION. TROUBLESHOOTING REVEALED THAT THE NR 2 GPS ANTENNA WAS FAILED & RADIATING ON GPS FREQUENCY, CAUSING INTERFERENCE FOR NR 1 GPS. IT IS APPARENT THAT THIS ANTENNA FAILURE MODE IS NOT UNCOMMON. CONSIDERING THAT THE EFFECTED GPS UNITS ARE CERTIFIED AS SOLE MEANS OF NAVIGATION, A KNOWN PROBLEM OF THIS TYPE IS VERY CONCERNING. THE NR 2 GPS ANTENNA WAS REPLACED WITH NEW WITH NO ABNORMALITIES NOTED.

Source: SDR P9KA2015091601 · FAA SDRS
O · 2015-09-08 Matched by certificate designator
N8419Q · ATA 8520

WHILE PERFORMING A ROUTINE OIL & FILTER CHANGE, MECHANIC SAW LARGE AMOUNTS OF LEAKED OIL & A CRANKCASE THROUGH BOLT NUT IN THE COWLING. FURTHER INVESTIGATION REVEALED THAT THE LOWER FWD THROUGH BOLT HAD BROKEN AT THE NR 6 CYLINDER. UPON REMOVING THE REMAINS OF THE THROUGH BOLT, IT WAS FOUND TO BE QUITE RUSTED AT THE NR 6 CYLINDER END & RUST PITTING WAS OBSERVED WHERE THE CRACK HAD STARTED. THE UPPER THROUGH BOLT SHOWED NO SIGNS OF SIMILAR CORROSION. ACCORDING TO THE LOGBOOKS, BOTH THROUGH BOLTS HAD BEEN REPLACED WITH NEW PARTS AT THE LAST OVERHAUL 8 YEARS AGO. BOTH THROUGH BOLTS WERE REPLACED WITH NEW PARTS & THE ACFT WAS RETURNED TO SERVICE.

Source: SDR P9KA2015091401 · FAA SDRS
O · 2015-08-10 Matched by certificate designator
N750KP · ATA 5312

DURING A ROUTINE 100 HOUR INSPECTION, A COMPANY MECHANIC FOUND THE CANTED BULKHEAD, PN 2612060-5, CRACKED AT THE CUT OUT FOR THE ELEVATOR PUSHROD. THE BULKHEAD WAS REPAIRED IAW THE APPLICABLE PORTIONS OF THE MANUFACTURER'S STRUCTURAL REPAIR MANUAL. POSSIBLE CONTRIBUTING FACTORS INCLUDE THE AIRCRAFT'S HIGH TOTAL TIME & HIGH CYCLES, AS WELL AS 2 INCIDENTS OF TAIL DAMAGE, A TAIL CONE STRIKE DURING LOADING & A HORIZONTAL STABILIZER STRIKE DURING ACFT REPOSITIONING UNDER TOW.

Source: SDR P9KA2015081001 · FAA SDRS
O · 2015-06-10 Matched by certificate designator
N70SB · ATA 5751

DURING ROUTINE MX, THE RT INBD AILERON HINGE, PN 1220053-12, WAS FOUND TO BE CRACKED IN THE VERTICAL WEB OF THE OTBD BRACKET THAT ATTACHES THE HINGE ASSEMBLY TO THE AFT WING SPAR. THE AILERON HINGE BRACKET WAS REPLACED WITH NEW. THE ACFT HAS HIGH TOTAL TIME & THOUGH CYCLES ARE NOT TRACKED, THIS ACFT HAS A HIGH NR OF CYCLES IAW FLIGHT HOUR, IS OPERATED SEASONALLY ON FLOATS & HAS FREQUENT TURBULENCE ENCOUNTERS. THIS ACFT IS ALSO EQUIPPED WITH A STOL KIT THAT INVOLVES DROOPING THE AILERONS WITH THE FLAPS & SUSPECT THAT THIS INCREASES THE STRESSES ON THE AILERON HINGE POINTS. AS THIS IS ONE OF SEVERAL SIMILAR BRACKETS THAT HAVE BEEN FOUND CRACKED ON OUR FLEET, CONDUCT A VISUAL & TACTILE INSPECTION OF THE INTEGRITY OF THE AILERON HINGE BRACKETS ON THESE ACFT AT REGULAR INTERVALS.

Source: SDR P9KA2015082002 · FAA SDRS
O · 2015-05-18 Matched by certificate designator
N93021 · ATA 5751

DURING A ROUTINE 100 HOUR INSPECTION, THE LT OTBD AILERON HINGE PN 1220052-17 WAS FOUND TO BE CRACKED IN THE VERTICAL WEB OF THE OTBD BRACKET THAT ATTACHES THE HINGE ASSEMBLY TO THE AFT WING SPAR. FURTHERMORE, UPON REMOVAL OF THE HINGE BRACKET ASSEMBLY THE AFT WING SPAR CHANNEL PN 1222106-13 WAS FOUND TO BE CRACKED ADJACENT TO ONE OF THE AILERON HINGE ASSEMBLY ATTACHING RIVETS. BOTH THE WING SPAR CHANNEL & THE AILERON HINGE BRACKET WERE REPLACED WITH NEW PARTS. THE ACFT HAS HIGH TOTAL TIME & THOUGH CYCLES ARE NOT TRACKED, THIS OPERATION HAS A HIGH NR OF CYCLES PER FLIGHT HOUR AS WELL AS FREQUENT TURBULENCE ENCOUNTERS. ALSO THE TWO RIVETS THAT ATTACH THE LOWER FLANGE OF THE AILERON HINGE BRACKET TO THE LOWER FLANGE OF THE SPAR CHANNEL HAD EVIDENTLY BEEN LOOSE FOR QUITE SOME TIME. I SUSPECT THAT THIS LOOSENESS CONTRIBUTED TO THE CRACKS IN THE BRACKET & THE SPAR CHANNEL. THIS IS ONE OF SEVERAL SIMILAR BRACKETS THAT HAVE BEEN FOUND CRACKED ON OUR FLEET, I RECOMMEND THAT OPERATORS OF HIGH TIME & HIGH FATIGUE ENVIRONMENT ACFT CONDUCT A VISUAL & TACTILE INSPECTION OF THE INTEGRITY OF THE AILERON HINGE BRACKETS ON THESE ACFT AT REGULAR INTERVALS.

Source: SDR P9KA2015082001 · FAA SDRS
O · 2015-03-12 Matched by certificate designator
N93021 · ATA 5551

THE HORIZONTAL STABILIZER WAS REMOVED AS PART OF A ROUTINE ANNUAL INSPECTION. DURING INSPECTION THE LT HORIZONTAL STABILIZER ATTACH BRACKET PN 1212128-1 WAS FOUND CRACKED JUST ABOVE THE BOLT HOLE. THE PART WAS REPLACED WITH NEW. NEITHER THE TOTAL TIME NOR THE TOTAL CYCLES ON THE BRACKET COULD BE DETERMINED. SUSPECT EITHER POOR PART FIT, ABUSE OF ACFT BY PUSHING ON THE HORIZONTAL STABILIZER TO MOVE & LIFT THE ACFT OR SIMPLE FATIGUE AS FACTORS IN THIS FAILURE. THIS STRUCTURE IS THE SAME AS FOUND ON THE 206, 207 & 210, SIMILAR TO THE 180 & 185. CRACKS IN SIMILAR PARTS ON THE 180 & 185 ARE A KNOWN ISSUE & THIS IS THE SECOND 207 IN OUR FLEET ON WHICH WE HAVE FOUND THESE CRACKS. RECOMMEND PERIODIC INSPECTION OF THE HORIZONTAL STABILIZER ATTACH STRUCTURE, TO INCLUDE DISASSEMBLY AS NECESSARY ESPECIALLY IN ACFT OPERATED IN HIGH FATIGUE OPERATIONS SUCH AS FREQUENT TURBULENCE ENCOUNTERS, HIGH CYCLES PER HOUR & HIGH GROSS WEIGHT OPERATION.

Source: SDR P9KA2015031701 · FAA SDRS
O · 2015-03-12 Matched by certificate designator
N93021 · ATA 5551

THE HORIZONTAL STABILIZER WAS REMOVED AS PART OF A ROUTINE ANNUAL INSPECTION. DURING INSPECTION THE RT HORIZONTAL STABILIZER ATTACH BRACKET PN 1212128-2 WAS FOUND CRACKED JUST ABOVE THE BOLT HOLE. THE PART WAS REPLACED WITH NEW. NEITHER THE TOTAL TIME NOR THE TOTAL CYCLES ON THE BRACKET COULD BE DETERMINED. SUSPECT EITHER POOR PART FIT, ABUSE OF ACFT BY PUSHING ON THE HORIZONTAL STABILIZER TO MOVE & LIFT THE ACFT OR SIMPLE FATIGUE AS FACTORS IN THIS FAILURE. THIS STRUCTURE IS THE SAME AS FOUND ON THE 206, 207, 210 & SIMILAR TO THE 180 & 185. CRACKS IN SIMILAR PARTS ON THE 180 & 185 ARE A KNOWN ISSUE & THIS IS THE SECOND 207 IN OUR FLEET ON WHICH WE HAVE FOUND THESE CRACKS. RECOMMEND PERIODIC INSPECTION OF THE HORIZONTAL STABILIZER ATTACH STRUCTURE, TO INCLUDE DISASSEMBLY AS NECESSARY ESPECIALLY IN ACFT OPERATED IN HIGH FATIGUE OPERATIONS SUCH AS FREQUENT TURBULENCE ENCOUNTERS, HIGH CYCLES PER HOUR & HIGH GROSS WEIGHT OPERATION.

Source: SDR P9KA2015031702 · FAA SDRS
O · 2015-02-23 Matched by certificate designator
N1301L · ATA 5551

THE HORIZONTAL STABILIZER WAS REMOVED AS PART OF A ROUTINE ANNUAL INSPECTION. DURING INSPECTION THE LT HORIZONTAL STABILIZER ATTACH BRACKET PN 1212128-1 WAS FOUND CRACKED JUST ABOVE THE BOLT HOLE. THE PART WAS REPLACED WITH NEW. ACCORDING TO THE ACFT LOGS THE PART WAS REPLACED APPROX 1500 FLIGHT HOURS & AN UNDETERMINED NR OF CYCLES AGO. SUSPECT EITHER POOR PART FIT, ABUSE OF ACFT BY PUSHING ON THE HORIZONTAL STABILIZER TO MOVE & LIFT THE ACFT OR SIMPLE FATIGUE AS FACTORS IN THIS FAILURE. THIS STRUCTURE IS THE SAME AS FOUND ON THE 206, 207, 210 & SIMILAR TO THE 180 & 185. CRACKS IN SIMILAR PARTS ON THE 180 & 185 ARE A KNOWN ISSUE. RECOMMEND PERIODIC INSPECTION OF THE HORIZONTAL STABILIZER ATTACH STRUCTURE, TO INCLUDE DISASSEMBLY AS NECESSARY ESPECIALLY IN ACFT OPERATED IN HIGH FATIGUE OPERATIONS SUCH AS FREQUENT TURBULENCE ENCOUNTERS, HIGH CYCLES PER HOUR & HIGH GROSS WEIGHT OPERATION.

Source: SDR P9KA15022601 · FAA SDRS
O · 2015-02-23 Matched by certificate designator
N1301L · ATA 5551

THE HORIZONTAL STABILIZER WAS REMOVED AS PART OF A ROUTINE ANNUAL INSPECTION. DURING INSPECTION THE RT HORIZONTAL STABILIZER ATTACH BRACKET PN 1212128-2 WAS FOUND CRACKED JUST ABOVE THE BOLT HOLE. THE PART WAS REPLACED WITH NEW. ACCORDING TO THE ACFT LOGS THE PART WAS REPLACED APPROX 1500 FLIGHT HOURS & AN UNDETERMINED NR OF CYCLES AGO. SUSPECT EITHER POOR PART FIT, ABUSE OF ACFT BY PUSHING ON THE HORIZONTAL STABILIZER TO MOVE & LIFT THE ACFT OR SIMPLE FATIGUE AS FACTORS IN THIS FAILURE. THIS STRUCTURE IS THE SAME AS FOUND ON THE 206, 207 & 210, SIMILAR TO THE 180 & 185. CRACKS IN SIMILAR PARTS ON THE 180 & 185 ARE A KNOWN ISSUE. RECOMMEND PERIODIC INSPECTION OF THE HORIZONTAL STABILIZER ATTACH STRUCTURE, TO INCLUDE DISASSEMBLY AS NECESSARY ESPECIALLY IN ACFT OPERATED IN HIGH FATIGUE OPERATIONS SUCH AS FREQUENT TURBULENCE ENCOUNTERS, HIGH CYCLES PER HOUR & HIGH GROSS WEIGHT OPERATION.

Source: SDR P9KA15022602 · FAA SDRS
K · 2015-01-13 Matched by certificate designator
N4794C · ATA 3233

AS THE AMPHIBIOUS FLOAT EQUIPPED ACFT CONDUCTED ITS LANDING APPROACH, THE PILOT ATTEMPTED TO EXTEND THE LG. BOTH MLG EXTENDED & BOTH NLG REMAINED RETRACTED. THE PILOT THEN ATTEMPTED TO RETRACT THE MLG & THEY REMAINED EXTENDED. THE ACFT LANDED ON THE RUNWAY ON BOTH MLG & THE FLOATS. THE ACFT SUSTAINED DAMAGE TO THE RUB STRIP & THE OUTER SKIN ON THE LT FLOAT. INSPECTION REVEALED THAT THE SHAFT SEAL O RING ON THE RT MLG ACTUATOR WAS DAMAGED, ALLOWING LOSS OF HYD FLUID. THE PLUG THAT HOLDS SAID O RING WAS CORRODED, WHICH MAY HAVE CONTRIBUTED TO THE DAMAGED O RING. NEITHER THE TOTAL TIME IN SERVICE OF THE ACTUATOR NOR THE TOTAL TIME SINCE DISASSEMBLY & RE SEAL OF THE ACTUATOR COULD BE DETERMINED.

Source: SDR P9KA20150113001 · FAA SDRS
O · 2015-01-06 Matched by certificate designator
N1301L · ATA 3222

DURING A ROUTINE 100 HOUR INSPECTION, CRACKS WERE NOTED IN THE NLG FORK. THE CRACKS EXTENDED FROM THE FWD 2 BOLT HOLES FWD TO THE EDGE OF THE PART & AFT APPROXIMATELY 1/2 INCH ON EACH SIDE. DISASSEMBLY REVEALED SEVERAL MORE CRACKS THAT DID NOT EXTEND PAST THE WASHERS UNDER THE BOLT HEADS. THE PART IS A VERY EARLY MODEL STC'D PART WHICH THE MANUFACTURER HAS LONG SINCE BEEFED UP. THE PART TOTAL TIME & TOTAL CYCLES COULD NOT BE DETERMINED.

Source: SDR P9KA2015010801 · FAA SDRS
O · 2014-12-22 Matched by certificate designator
N8216T · ATA 8530

DURING A ROUTINE 100 HOUR INSPECTION, THE NR 2 CYLINDER WAS FOUND TO HAVE COMPRESSION OF 30/80 WITH LEAKAGE OUT THE INTAKE VLV. THIS IS THE THIRD OCCURRENCE OF THE SAME PROBLEM ON THIS FACTORY OVERHAULED ENG IN LESS THAN 500 HOURS SINCE OVERHAUL. THE FIRST TWO WERE THE NR 3 CYLINDER AT 294 HOURS SINCE OVERHAUL, FOLLOWED BY NR 5 AT 384 HOURS SINCE OVERHAUL. FOR COMPARISON, PRIOR TO THIS IN OVER 10,000 HOURS OF ENG OPERATION WITH IO540K SERIES WE HAD NOT HAD TO PULL A CYLINDER DUE TO LOW COMPRESSION.

Source: SDR P9KA2014122201 · FAA SDRS
O · 2014-12-19 Matched by certificate designator
N93021 · ATA 8520

DURING A CYLINDER CHANGE, THE SMALL END BUSHING IN THE CONNECTING ROD WAS FOUND SHIFTED & ROTATED IN ITS BORE IN THE NR 1 CONNECTING ROD. THE ENG WAS REBUILT TO ZERO TIME, 1290 OPERATING HOURS AGO.

Source: SDR P9KA2014121901 · FAA SDRS
O · 2012-03-14 Matched by certificate designator
N60077 · ATA 3210

EDO AMPHIBIOUS 4580 FLOATS, FOUND NOSE GEAR CONTROL QUADRANT, LOWER END WHERE THE CABLE ROUTS AROUND THE QUADRANT A CRACK THAT FORMED AT THE CABLE END AND RAN THROUGH TO THE INSIDE OF THE LIGHTNING HOLE THEN IN THE DIRECTION OF CABLE RUN ABOUT 1" LONG THE CRACK WAS SEPARATING THE QUADRANT INTO HALF'S AND COMPLETE FAILURE OF THE PART WOULD HAVE HAPPENED SOON THERE AFTER.

Source: SDR P9KA2012F00065 · FAA SDRS
O · 2011-07-20 Matched by certificate designator
N777DH · ATA 8530

ON ENGINE SHUTDOWN A SUCKING SOUND WAS HEARD AS ENGINE DIED. CYLINDER COMPRESSION CHECK WAS 0/80. AFTER STAKING THE VALVE THE COMPRESSION WAS STILL 0/80. AIR WAS HEARD COMING FROM THE EXHAUST PIPE. AFTER REMOVING THE EXHAUST STACK FROM THE CYLINDER, A CRACK AROUND THE VALVE STEM WAS NOTICED BY THE MX. CYLINDER WAS REMOVED FROM THE ACFT AND A SERVICEABLE CYLINDER WAS INSTALLED. VALVE WAS REMOVED FROM CYLINDER AND A CRACK WAS SEEN AROUND ABOUT 2/3 OF THE VALVE FACE. THE VALVE REMAINED INTACT.

Source: SDR P9KA2011F00167 · FAA SDRS
O · 2007-12-12 Matched by certificate designator
N777DH · ATA 8530

CYLINDER CRACKED IN THE AREA OF EXHAUST VALVE.

Source: SDR 2008FA0000042 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N1265UOperator named in NTSB report
N264KPCESSNA 2082004Valid RegistrationMatched by certificate designator
N265KPCESSNA 208Valid RegistrationMatched by certificate designator
N265KPCESSNA 208Valid RegistrationOperator named in NTSB report
N4794CDEHAVILLAND BEAVER DHC-2 MK.11951Valid RegistrationMatched by certificate designator
N743KPDEHAVILLAND DHC-21960Valid RegistrationMatched by certificate designator
N745KPCESSNA T2071974Valid RegistrationOperator named in NTSB report
N748KPCESSNA U206F1976Valid RegistrationMatched by certificate designator
N749KPCESSNA U206G1980Valid RegistrationMatched by certificate designator
N750KPCESSNA 208B199718Matched by certificate designator
N753KPCESSNA 208B2007Valid RegistrationMatched by certificate designator
N754KPCESSNA 208B2007Valid RegistrationOperator named in NTSB report
N754KPCESSNA 208B2007Valid RegistrationMatched by certificate designator
N755KPCESSNA 208B1999Valid RegistrationMatched by certificate designator
N777DHDEHAVILLAND DHC-21949Valid RegistrationMatched by certificate designator