N788KL

FAIRCHILD SA227-AC · 1991 · Valid Registration

Registered owner: C B G LLC, OR (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
KEY LIME AIR CORPORATION (KY7A)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2021-05-11 Matched by certificate designator
ATA 2450

PILOT REPORTED SMOKE IN THE COCKPIT AND #1 CURRENT LIMITER FAILED. MX REPLACED CURRENT LIMITER AND PERFORMED GROUND RUN AND OPS CHECK GOOD. AIRCRAFT IS NOW AIRWORTHY.

Source: SDR KY7A20210511004 · FAA SDRS
K · 2021-04-14 Matched by certificate designator
ATA 3233

HYDRAULIC SYSTEM FAILURE IN FLIGHT DURING CRUISE AND CREW LANDED AT DESTINATION. MX DISCOVERED THE L/H OUTBOARD MLG ACTUATOR HAD A CRACK IN IT AND REPLACED WITH SERVICEABLE L/H OUTBOARD MLG ACTUATOR. OPERATIONAL AND LEAK CHECKS GOOD.

Source: SDR KY7A20210416004 · FAA SDRS
K · 2020-07-15 Matched by certificate designator
ATA 7261

PILOT REPORTED NR 1 ENGINE LOST OIL. MX TROUBLESHOT AND LOCATED A LEAK AT 7/16 OIL MANIFOLD TO PROP GOVERNOR LINE. MX REMOVED AND REPLACED LINE AND REPOSITIONED MANIFOLD AS REQUIRED FOR FIT. POST ACTION OPS AND LEAK CHECKED GOOD AND SERVICED OIL.

Source: SDR KY7A2020072215002 · FAA SDRS
K · 2020-07-01 Matched by certificate designator
ATA 2910

PILOT REPORTED LOSS OF HYDRAULIC PRESSURE IN FLIGHT. MX REMOVED AND REPLACED FLAP UP HYDRAULIC LINE WITH NEW IAW MM CHAPTER 20-40-00 GROUND OPS AND LEAK CHECK GOOD.

Source: SDR KY7A202007021001 · FAA SDRS
O · 2020-04-04 Matched by certificate designator
ATA 7920

PILOT SHUTDOWN E1 AS PRECAUTION DUE TO LOW OIL PRESSURE. MX REMOVED AN REPLACED E1 PROP GOVERNOR LUBRICATION OIL LINE WITH SERVICEABLE. GROUND OPS AND LEAK CHECK GOOD.

Source: SDR KY7A2020041404001 · FAA SDRS
O · 2017-10-25 Matched by certificate designator
ATA 5340

INSPECTION PERSONNEL FOUND BRACKET BROKEN. THE BRACKET SUPPORTS THE POWER AND SPEED CONTROL TELEFLEX CABLES. AN FCD WAS INITIATED TO DETECT OTHER OCCURRENCES OF THE PROBLEM IN THE FLEET IAW SERVICE LETTER 227-SL-067. CARRIER IS INVESTIGATING AMENDMENT OF MAINTENANCE/INSPECTION INTERVALS ON THIS ITEM.

Source: SDR KY7A20171025001 · FAA SDRS
J · 2016-02-15 Matched by certificate designator
ATA 3234

FLIGHT CREW REPORTED THAT ALL THREE LANDING GEARS UNLOCKED & PARTIALLY EXTENDED DURING FLIGHT WITH GEAR SELECTOR IN THE UP POSITION. MX FOUND DEFECTIVE LG HANDLE & SWITCH ASSEMBLY, SN 445. REPLACED WITH SERVICEABLE UNIT, SN 519, 8130-3 FROM M7 AEROSPACE. ON SUBSEQUENT FLIGHT, NEW GEAR HANDLE STUCK IN THE DOWN POSITION. MX FOUND HANDLE DOWN LOCK MECHANISM DEFECTIVE. SECOND NEW HANDLE ASSEMBLY, SN 276, WAS INSTALLED & NO FURTHER ISSUES WERE NOTED.

Source: SDR KY7A20160215001 · FAA SDRS
O · 2015-04-21 Matched by certificate designator
ATA 3211

PILOT FOUND RT MLG UPLOCK ROLLER BROKEN. RT MLG TRUNNION ASSEMBLY REPLACED.

Source: SDR KY7A20150421001 · FAA SDRS