N80BS

CESSNA 404 · 1977 · Valid Registration

Registered owner: SONRISE AVIATION LLC, IN (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
BUSINESS AVIATION COURIER, INC. (DUFA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

K B · 2017-03-28 Matched by certificate designator
ATA 2910

DEPARTED, SELECTED GEAR UP AND SHORTLY AFTER BEGAN TO GET A PETROLEUM ODOR IN THE CABIN. IMMEDIATELY AFTER THAT THE LEFT HYD FLOW ANNUNCIATOR LIGHT ILLUMINATED, FOLLOWED BY THE RIGHT. ACTIVATED THE EMERGENCY LANDING GEAR EXTENSION BLOW DOWN SYSTEM AND MADE AN UNEVENTFUL LANDING. DURING INVESTIGATION, IT WAS DISCOVERED THAT ONE OF THE MAIN HYDRAULIC PRESSURE LINES HAD RUPTURED AT A BEND RADIUS.

Source: SDR DUFA20170330001 · FAA SDRS
E · 2007-04-10 Matched by certificate designator
ATA 8530

WHILE ON APPROACH TO AIRPORT, THE PILOT NOTICED MANIFOLD PRESSURE DROPPING AS WELL AS OIL PRESSURE FROM THE RIGHT ENGINE. HE ALSO BEGAN TO FEEL A VIBRATION FROM THE SAME ENGINE. HE ELECTED TO SHUT THE ENGINE DOWN AND MADE AN UNEVENTFUL LANDING. UPON INSPECTION, THE NR 5 CYLINDER HOLD DOWN STUDS HAD SHEARED AND ALLOWED THE CYLINDER TO HAMMER AGAINST THE ENGINE CASE AND COWLING. THIS IN TURN RIPPED THE RT EXHAUST STACK FROM THE NR 1 AND NR 5 CYLINDERS CAUSING HEAT DISTRESS AT THE COWL DOOR.

Source: SDR DUFA20070002 · FAA SDRS
E · 2007-04-10 Matched by certificate designator
ATA 8530

WHILE ON APPROACH TO AIRPORT, THE PILOT NOTICED MANIFOLD PRESSURE DROPPING AS WELL AS OIL PRESSURE FROM THE RT ENGINE. HE ALSO BEGAN TO FEEL A VIBRATION FROM THE SAME ENGINE. HE ELECTED TO SHUT THE ENGINE DOWN AND MADE AN UNEVENTFUL LANDING. UPON INSPECTION, THE NR 5 CYLINDER HOLD DOWN STUDS HAD SHEARED AND ALLOWED THE CYLINDER TO HAMMER AGAINST THE ENGINE CASE AND COWLING. THIS IN TURN RIPPED THE RT EXHAUST STACK FROM THE NR 1 AND NR 5 CYLINDERS CAUSING HEAT DISTRESS AT THE COWL DOOR.

Source: SDR DUFA041007001 · FAA SDRS
R · 2006-08-02 Matched by certificate designator
ATA 2844

PILOT REPORTED THAT WHILE IN CRUISE FLIGHT THE LT ENGINE FUEL FLOW SUDDENLY DROPPED OFF AND THE ENGINE BEGAN TO RUN ROUGH AND LOSE POWER. THE BOOST PUMP WAS SELECTED TO HIGH AND MIXTURE INCREASED TO FULL RICH WHICH HAD LITTLE EFFECT. THE PILOT CONTACTED DISPATCH AND MAINTENANCE AND AFTER A SHORT DISCUSSION, MAINTENANCE RECOMMENDED THE ENGINE BE SHUTDOWN AND SECURED TO PREVENT THE POSSIBILITY OF FIRE. THE PILOT SHUT THE ENGINE DOWN AND MADE AN UNEVENTFUL LANDING. THE ENGINE WAS UNCOWLED AND IT WAS DISCOVERED THE UPPER DECK PRESSURE LINE HAD PULLED OUT OF IT'S FITTING AT THE LT AND RT JUNCTION TEE. THE LINE WAS REPAIRED AND GROUND RUNS REVEALED NO OTHER ABNORMALITIES.

Source: SDR BAC005 · FAA SDRS
R · 2006-08-02 Matched by certificate designator
ATA 7310

PILOT REPORTED THAT WHILE IN CRUISE FLIGHT THE LEFT ENGINE FUEL FLOW SUDDENLY DROPPED OFF AND THE ENGINE BEGAN TO RUN ROUGH AND LOSE POWER. THE BOOST PUMP WAS SELECTED TO HIGH AND THE MIXTURE INCREASED TO FULL RICH WHICH HAD LITTLE EFFECT. THE PILOT CONTACTED DISPATCH AND MAINTENANCE AND AFTER A SHORT DISCUSSION, MAINTENANCE RECOMMENDED THE ENGINE BE SHUT DOWN AND SECURED TO PREVENT THE POSSIBILITY OF FIRE. THE PILOT SHUT DOWN THE ENGINE AND MADE AN UNEVENTFUL LANDING. THE ENGINE WAS UNCOWLED AND IT WAS DISCOVERED THAT THE UPPER DECK PRESSURE LINE HAD PULLED OUT OF THE FITTING AT THE LEFT AND RIGHT JUNCTION TEE. THE LINE WAS REPAIRED AND GROUND RUNS REVEALED NO OTHER ABNORMALITIES.

Source: SDR BAC001 · FAA SDRS
B · 2004-11-29 Matched by certificate designator
ATA 2434

WHILE IN CRUISE FLIGHT, THE PILOT NOTICED SPARKS COMING FROM THE LEFT ENGINE FORWARD COWL AREA. AS A PRECAUTION, THE ENGINE WAS SHUTDOWN AND SECURED. THE AIRCRAFT THEN MADE AN UNEVENTFUL LANDING. UPON INVESTIGATION, IT WAS DISCOVERED THAT THE ALTERNATOR OUT SENSOR SHORTED INTERNALLY AND HAD BURNED A HOLE THROUGH THE END OF IT'S CASE. THE SENSOR WAS REPLACED AND AN OPS CHECK PROVED SATISFACTORY.

Source: SDR 2004F00429 · FAA SDRS