BUSINESS AVIATION COURIER, INC.

Part 135 operator · designator DUFA

Data confidence: Records are linked by certificate number, aircraft registration, or a name match that a reviewer has confirmed. Each record below shows how it was linked.

Also recorded as: BUSINESS AVIATION COURIER, INC., Business Aviation Courier, Inc.

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

Acc · 2023-11-24 Matched by aircraft (N-number)
CESSNA 402B (N76MD) Fatal injury NUSN
Source: NTSB case GAA24WA039
Acc · 2016-05-27 Matched by aircraft (N-number)
CESSNA 402B (N76MD) None injury Part 91
Source: NTSB case CEN16LA201
Inc · 2012-12-14 Operator named in NTSB report
SWEARINGEN SA227-AC (N3108B) None injury Part 91

Operated by Business Aviation Courier (per NTSB report)

Source: NTSB case CEN13IA107
Acc · 2009-03-10 Operator named in NTSB report
CESSNA 402B (N402BP) None injury Part 135

Operated by Business Aviation Courier, Inc. (per NTSB report)

Source: NTSB case CEN09LA206
Incident · 1995-12-28 Matched by aircraft (N-number)
Fairchild SA227-AC (N159MC) None injury
Source: NTSB case CHI96IA066
Accident · 1991-09-28 Matched by aircraft (N-number)
Fairchild SW3 (N159MC) None injury
Source: NTSB case NYC91LA248

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

188 reports on file — showing most recent 50.

N · 2020-03-12 Matched by certificate designator
N572GW · ATA 2613

SHORTLY AFTER TAKEOFF FROM FARGO, THE PILOT NOTICED THE RIGHT WING “OVERHEAT” LIGHT ILLUMINATED. FOLLOWING THE CHECKLIST, HE SLOWED THE AIRCRAFT, EXTENDED THE LANDING GEAR, TURNED OFF THE RIGHT HAND BLEED AIR VALVE AND TURNED OFF THE RIGHT HAND GENERATOR. FOLLOWING THE ONE MINUTE TIME LIMIT ALLOWED PER THE CHECKLIST WITH THE “OVERHEAT” LIGHT ON, THE ENGINE WAS SHUTDOWN. THE PILOT TURNED BACK TO RETURN TO FARGO WHERE HE MADE AN UNEVENTFUL LANDING. THE PILOT REPORTED THAT THE “OVERHEAT” LIGHT REMAINED ON EVEN WITH THE ENGINE SHUTDOWN BUT WENT OUT UPON LANDING. HE CALLED OUT MAINTENANCE AND THE TWO OF THEM MADE A THOROUGH INSPECTION OF THE ENGINE, GEAR WELL AND PLENUM AREA WITH NO DISCREPANCIES NOTED. IT IS SUSPECTED THE INDICATOR WIRING MAY HAVE A CHAFE IN THE INSULATION SOMEWHERE, WHICH PROVIDED A GROUND TO ILLUMINATE THE LIGHT, BUT LOST THE GROUND UPON TOUCHDOWN.

Source: SDR DUFA20200313003 · FAA SDRS
B · 2020-01-14 Matched by certificate designator
N3108B · ATA 2697

ON JANUARY 14TH, 2020, DAKOTA 1024 DEPARTED THIEF RIVER FALLS (KTVF) AIRPORT AT 1844 AND CLIMBED TO 17,000 FEET MSL. WHILE APPROACHING THE GOLLF INTERSECTION ON THE GOPHER ONE ARRIVAL, ARTCC ASSIGNED DESCEND AND MAINTAIN 10,000 FEET MSL. AT APPROXIMATELY 11,000 FEET MSL DURING THE DESCENT, A GLOW WAS NOTICED UNDER THE PIC SIDE OF THE INSTRUMENT PANEL. THE GLOW, WHICH WAS ORANGE IN COLOR, GREW IN BRIGHTNESS FOR 0.5 TO 1 SECOND BEFORE DIMMING AGAIN. THE WHOLE EPISODE WAS APPROXIMATELY 3 TO 4 SECONDS. I ADVISED THE CENTER CONTROLLER THAT THERE WAS A SHORT PROBLEM WITH THE ELECTRICAL SYSTEM THAT I WAS TROUBLESHOOTING. WHILE MAKING THIS TRANSMISSION, A SMALL PLUME OF SMOKE CAME FROM THE PANEL AND A DISTINCT, OVERPOWERING SMELL OF ELECTRICAL BURNING WAS NOTED. I IMMEDIATELY DONNED THE OXYGEN MASK AND ELECTED TO DECLARE AN EMERGENCY, WARY OF AN ELECTRICAL FIRE BEHIND THE PANEL. CENTER GAVE ME VECTORS TO ST. CLOUD AIRPORT (KSTC) AND AUTHORIZED A DESCENT TO 3,500 FEET MSL. DURING THE DESCENT, I SEARCHED BOTH VISUALLY AND WITH MY HANDS, ALL CIRCUIT BREAKERS, NOT FINDING THAT ANY HAD BEEN BLOWN. IN ASSESSING THAT NO INSTRUMENTS OR LIGHTS WERE INOPERATIVE, I ELECTED TO DELAY TRANSFERRING POWER BETWEEN ESSENTIAL BUSES AND FOCUS MY EFFORTS ON PROPERLY AND SAFELY EXECUTING THE APPROACH AND LANDING. AT THIS POINT IN MY TROUBLESHOOTING, I WAS ENTERING A CROSSWIND FOR RUNWAY 31 AT KSTC. A NORMAL TRAFFIC PATTERN AND LANDING WERE MADE. FIREFIGHTING PERSONNEL ANALYZED THE AIRCRAFT WITH A THERMAL IMAGING DEVICE AND DEEMED THAT NO IMMINENT THREAT EXISTED. MAINTENANCE WAS CALLED OUT AND A VERY THOROUGH INSPECTION WAS CONDUCTED BEHIND THE INSTRUMENT PANEL. ALL SYSTEMS, LIGHTING AND INSTRUMENTS WERE FUNCTIONAL TESTED AND FOUND TO BE OPERATIONAL. THE ONLY ITEM NOTED DURING THE INSPECTION WAS A RING TERMINAL ON THE WING DEICE LIGHT SWITCH HAD SIGNS OF HEAT DAMAGE. THE RING TERMINALS WERE REPLACED WITH NEW.

Source: SDR DUFA20200116002 · FAA SDRS
B · 2020-01-07 Matched by certificate designator
N3116N · ATA 2120

ON JANUARY 7TH, 2020, DAKOTA 1023 DEPARTED THIEF RIVER FALLS (KTVF) AIRPORT ON SCHEDULE AT 14:57 AND BEGAN A CLIMB TO 17,000 FT MSL. AT 500 FT AGL, BLEED AIR WAS TURNED ON AND AIR CONDITIONING RHEOSTAT WAS SET TO APPROXIMATELY 75% HOT WITH THE TEMPERATURE CONTROLLER IN THE “AUTO” POSITION. AT 15:03, THE AIRCRAFT HAD REACHED 13,700 FT MSL WHEN THE PILOT LOOKED AT THE RIGHT COCKPIT SIDE WINDOW AND NOTICED LIGHT SMOKE. BRIEFLY INVESTIGATING FOR A POSSIBLE CAUSE, THE PILOT LOOKED TO THE JUMP SEAT AREA BY THE MAIN CABIN DOOR AND NOTED SMOKE IN THIS SECTION OF THE AIRCRAFT AS WELL. THE SMOKE WAS HAZY, NOT THICK AND DID NOT HAVE A DISTINCT ODOR. THE PILOT BEGAN AN EMERGENCY DESCENT AND REQUESTED IMMEDIATE VECTORS FROM AIR TRAFFIC CONTROL (ATC) BACK TO KTVF. WHILE DOING SO, THE BLEED AIR WAS TURNED TO THE OFF POSITION, CABIN PRESSURE DUMPED UPON REACHING 10,000 FT MSL AND FRESH AIR FAN PLACED IN THE OVERRIDE POSITION. THE SMOKE CLEARED AS A RESULT OF THESE MEASURES AND NO FURTHER SMOKE WAS NOTED. WHILE TAKING THESE ACTIONS, THE PILOT STATED THE NATURE OF THE SITUATION TO ATC AND DECLARED AN EMERGENCY AS A PRECAUTIONARY MEASURE. THE PILOT PROCEEDED TO MAKE AN UNEVENTFUL LANDING. MAINTENANCE WAS CALLED OUT AND A THOROUGH INSPECTION WAS CONDUCTED IN THE CABIN AND COCKPIT AREA WITH NO EVIDENCE OF SMOKE OR OVERHEATING NOTED. WITH NO INDICATIONS PRESENT, EXTENSIVE GROUND RUNS WERE CONDUCTED WITH THE CABIN TEMP CONTROLS PLACED TO MAXIMUM HEAT WITH NO ADVERSE RESULTS. WITH NO DEFINITIVE RESULTS, IT IS SUSPECTED THE CABIN MAY HAVE HAD CONDENSATION ACCUMULATING WHICH RESEMBLED A FOG OR HAZY CONDITION.

Source: SDR DUFA20200108001 · FAA SDRS
E · 2019-06-15 Matched by certificate designator
N103RC · ATA 8500

WHILE ON A ONE MILE FINAL APPROACH, THE RIGHT HAND ENGINE DEVELOPED A SEVERE VIBRATION AND BEGAN TO LOSE POWER. THE AUXILIARY FUEL PUMP WAS SELECTED TO HIGH BUT THE LOSS OF POWER DID NOT IMPROVE. THE ENGINE WAS SHUTDOWN AND THE PROPELLER FEATHERED. THE APPROACH CONTINUED WITH AN UNEVENTFUL LANDING. UPON EXITING THE AIRCRAFT, THE PILOT NOTICED AN EXCESSIVE AMOUNT OF OIL ON THE INBOARD ENGINE COWL AND LEADING EDGE OF THE WING. MAINTENANCE WAS CALLED OUT AND UPON INSPECTION, A LARGE CRACK IN THE ENGINE CASE WAS DISCOVERED COMING FROM THE NUMBER SIX CYLINDER EXHAUST PUSHROD TUBE BOSS RUNNING THE OIL PAN FLANGE.

Source: SDR DUFA20190619001 · FAA SDRS
N · 2018-05-25 Matched by certificate designator
N3108B · ATA 2697

DURING CRUISE, THE NR 2 ENGINE FIRE PANEL LIGHT BEGAN TO FLICKER ON. REDUCED POWER AND CHECKED ALL ENGINE INSTRUMENTS WITH NO ABNORMALITIES NOTED. AFTER A FEW MINUTES, THE ENGINE FIRE LIGHT CAME ON STEADY. THE PILOT SHUT THE ENGINE DOWN AND AFTER A FEW MINUTES, THE LIGHT WENT OUT. THE AIRCRAFT MADE AN UNEVENTFUL LANDING. MAINTENANCE INSPECTION REVEALED A CHAFED WIRE FROM THE ENGINE FIRE DETECTOR PROBE.

Source: SDR DUFA20180529002 · FAA SDRS
X J · 2018-05-16 Matched by certificate designator
N430MA · ATA 7314

WHILE IN CRUISE DURING A PART 91 REPOSITION FLIGHT, THE NR 2 ENGINE FLAMED OUT AND SHUT DOWN. MAINTENANCE CREW WAS DISPATCHED TO THE LOCATION AND THE ENGINE GEARBOX OPENED UP FOR INVESTIGATION. FOUND ACCESSORY GEAR ASSEMBLY HAD FAILED LOSING CONTINUITY TO FUEL PUMP DRIVE GEAR.

Source: SDR DUFA20180529001 · FAA SDRS
A · 2017-12-29 Matched by certificate designator
N3116N · ATA 3240

ON COMPLETION OF THE TAXI AND WHILE HOLDING SHORT OF THE RUNWAY, THE PILOT WAS INFORMED BY ANOTHER AIRCRAFT THAT THE LEFT MAIN GEAR HAD A BRAKE FIRE. SHUTDOWN THE AIRCRAFT. THE LEFT BRAKES HAD A SMALL FIRE AND THE BRAKE DISC WAS GLOWING RED HOT. EXTINGUISHED THE FIRE. MAINTENANACE INSPECTED THE MAIN WHEEL FOR FREEDOM OF MOVEMENT AND FOUND IT FREE. THE BRAKE WAS REMOVED. NO ABNORMALITIES COULD BE FOUND AND THE DISC WAS FREE OF ANY SIGNIFICANT DRAG.

Source: SDR DUFA20170102003 · FAA SDRS
N · 2017-04-12 Matched by certificate designator
N685BA · ATA 7933

WHILE IN CRUISE FLIGHT, THE PILOT NOTICED THE RIGHT ENGINE OIL TEMP CLIMBING TO NEAR RED LINE TEMPERATURE. THE OIL PRESSURE AND ALL OTHER ENGINE PARAMETERS APPEARED NORMAL BUT AS A PRECAUTION, THE PILOT SHUT DOWN THE RIGHT ENGINE. DIVERTED TO THE NEAREST SUITABLE AIRPORT AND MADE AN UNEVENTFUL LANDING. INVESTIGATION FOUND NO OBVIOUS DISCREPANCIES. ENGINE GROUND RUNS WERE PERFORMED AND THE OIL TEMP REMAINED IN THE NORMAL RANGE.

Source: SDR DUFA2017002 · FAA SDRS
K B · 2017-03-28 Matched by certificate designator
N80BS · ATA 2910

DEPARTED, SELECTED GEAR UP AND SHORTLY AFTER BEGAN TO GET A PETROLEUM ODOR IN THE CABIN. IMMEDIATELY AFTER THAT THE LEFT HYD FLOW ANNUNCIATOR LIGHT ILLUMINATED, FOLLOWED BY THE RIGHT. ACTIVATED THE EMERGENCY LANDING GEAR EXTENSION BLOW DOWN SYSTEM AND MADE AN UNEVENTFUL LANDING. DURING INVESTIGATION, IT WAS DISCOVERED THAT ONE OF THE MAIN HYDRAULIC PRESSURE LINES HAD RUPTURED AT A BEND RADIUS.

Source: SDR DUFA20170330001 · FAA SDRS
N · 2016-10-11 Matched by certificate designator
N685BA · ATA 2697

JUST AFTER BEGINNING HIS DESCENT, THE PILOT NOTICED HIS LEFT WING OVERHEAT LIGHT HAD ILLUMINATED STEADY. FOLLOWING PROCEDURES, THE PILOT CLOSED HIS LEFT BLEED AIR VALVE, TURNED OFF THE LEFT GENERATOR AND EXTENDED THE LANDING GEAR. AFTER A COUPLE OF MINUTES HAD PASSED, THE WING OVERHEAT LIGHT REMAINED ON. FOLLOWING THE PROCEDURE FOR THIS, THE PILOT SHUT DOWN THE LEFT ENGINE AS REQUIRED BY THE FLIGHT MANUAL. THE LIGHT STILL REMAINED ILLUMINATED SO, DUE TO THE WEATHER, THE PILOT DIVERTED TO THE NEAREST AIRPORT AND LANDED. INVESTIGATION DISCOVERED THAT THIS HAD BEEN A FALSE INDICATION PROBLEM DUE TO A CHAFED WIRE TO GROUND.

Source: SDR DUFA20161013002 · FAA SDRS
A · 2016-05-27 Matched by certificate designator
N76MD · ATA 8530

PILOT WAS SETTING UP FOR INITIAL APPROACH WHEN THE LT ENG BEGAN TO RUN A LITTLE ROUGH. THE INSTRUCTOR NOTICED THE FUEL FLOW BEGIN TO DROP A LITTLE SO THE AUXILIARY BOOST FUEL PUMP WAS SELECTED TO HIGH. THE ENG BEGAN TO SMOOTH OUT WHEN THEY NOTICED THE TACHOMETER SUDDENLY DROP OFF TO ZERO. AT THAT POINT THE PILOT NOTICED FLAMES STREAMING OUT THE UPPER COWL LOUVERS & RELAYED TO THE INSTRUCTOR THAT THEY HAD AN ENG FIRE. THE ENG WAS IMMEDIATELY SECURED & AN EMER DECLARED TO THE TOWER & MADE AN UNEVENTFUL LANDING. FIRE PERSONNEL FOLLOWED THE ACFT TO PARKING & MONITORED THE ENG FOR ANY RE-IGNITION OR FLARE UP. IT APPEARS THE NR 4 CYLINDER EXPERIENCED BURN THROUGH OF THE CYLINDER HEAD ON THE FWD SIDE OF THE EXHAUST CHAMBER. THIS THEN MELTED THE VLV COVER OF THE NR 6 CYLINDER, SPRAYING OIL AFT WHICH THEN IGNITED. SINCE IT WAS ON THE OTBD SIDE OF THE LT ENG, IT WASN'T SEEN BY THE PILOT UNTIL SIGNIFICANT DAMAGE HAD BEEN DONE.

Source: SDR DUFA20160527001 · FAA SDRS
E · 2015-07-07 Matched by certificate designator
N3813 · ATA 7414

WHILE ON CLIMB OUT, THE PILOT BEGAN TO FEEL A SLIGHT VIBRATION COMING FROM THE LT ENG. ELECTED TO RETURN TO THE AIRPORT WHERE HE MADE AN UNEVENTFUL LANDING. UPON INVESTIGATION, IT WAS NOTED THAT THERE WAS A SUBSTANTIAL RPM DROP DURING THE MAGNETO CHECK OF THE LT ENG`S LT MAG. THE MAG WAS REMOVED & DISASSEMBLED. INSPECTION REVEALED THAT THE BUSHING WITHIN THE DISTRIBUTOR BLOCK WAS EXTREMELY LOOSE. THIS CONDITION ALLOWED THE DISTRIBUTOR GEAR TO BECOME MISALIGNED WITH THE ROTATING MAGNET, JUMPING TEETH & CAUSING AN INTERNAL OUT OF TIME CONDITION. FURTHER INSPECTION REVEALED NO OTHER DISCREPANCIES. THE MAGNETO WAS ASSEMBLED WITH NEW PARTS & OPERATIONS CHECKED OK.

Source: SDR DUFA20150714002 · FAA SDRS
E · 2015-03-30 Matched by certificate designator
N3813 · ATA 7414

WHILE IN CRUISE FLIGHT AT FL7000 THE RT ENG SUDDENLY BEGAN RUNNING VERY ROUGH. THE PILOT SUSPECTED LOW FUEL FLOW SO HE ADJUSTED THE MIXTURE TO FULL RICH & SELECTED THE AUXILIARY PUMP TO LOW & SUBSEQUENTLY TO HIGH WITH NO EFFECT. HE NOTICED THE CYLINDER HEAD TEMPERATURE WAS RISING & NEARING THE TOP OF THE GREEN ARC SO HE ELECTED TO SHUT DOWN THE RT ENG. THE PILOT PERFORMED A SUCCESSFUL SINGLE ENG LANDING. UPON INSPECTION, IT WAS DISCOVERED THAT THE FLANGE ON THE RT MAGNETO HAD CRACKED & THE MAGNETO ROTATED OUT OF TIME WITH THE ENG. THE LT MAGNETO WAS ALSO INSPECTED WHICH REVEALED THE DISTRIBUTOR ROTOR HAD JUMPED OUT OF TIME WITH THE ROTATING MAGNET, DUE TO WORN GEARS, CAUSING THE MAGNETO TO BE OUT OF INTERNAL TIMING. THE RT MAGNETO WAS REMOVED & A SERVICEABLE MAGNETO INSTALLED. THE LT MAGNETO WAS REMOVED, DISASSEMBLED & A NEW DISTRIBUTOR ROTOR INSTALLED. TIMING WAS SET & THE ENG WAS GND RUN & THE MAGNETO'S FUNCTIONALLY CHECKED GOOD.

Source: SDR DUFA20150331001 · FAA SDRS
K J · 2014-05-06 Matched by certificate designator
N103RC · ATA 7920

WHILE IN CRUISE FLIGHT, THE PILOT NOTICED THE LT ENG OIL PRESS DROPPING. ONCE THE OIL PRESS DROPPED BELOW THE GREEN ARC, SHUT DOWN THE LT ENG & CONTACTED CTR. DIVERTED TO ALTERNATE AIRPORT, MADE AN UNEVENTFUL LANDING. THE OIL WAS BEING DUMPED OVERBOARD THROUGH THE AIR & OIL SEPARATOR CAN. WHILE REMOVING THE OIL LINE FITTING AT THE SCAVENGE PUMP INLET, A RATHER LARGE CHUNK OF FOREIGN MATERIAL WAS FOUND BLOCKING THE PASSAGE THROUGH THE FITTING. THIS WAS CLEARED & THE HOSE CHECKED WHICH REVEALED NO FURTHER DEBRIS. A SERVICEABLE SCAVENGE PUMP HOSE WAS INSTALLED AS A PRECAUTION. ENG RUNS WERE PERFORMED & NO ABNORMALITIES WERE REVEALED.

Source: SDR DUFA20140506002 · FAA SDRS
K B · 2014-04-30 Matched by certificate designator
N572GW · ATA 2910

APPROX 200 FT AGL, THE PILOT BEGAN TO SEE & SMELL SMOKE IN THE COCKPIT. CONTACTED ATC & DECLARED AN EMER, MADE A SAFE LANDING. WHILE EXITING THE ACFT, NOTICED THE SMOKE WAS MUCH THICKER IN THE MID CABIN AREA. AN INSPECTION OF THE ENGS REVEALED NO EVIDENCE OF FIRE OR HEAT DAMAGE. INSPECTION PANELS WERE REMOVED & IT WAS DISCOVERED THAT A 1/4 INCH HYD LINE HAD CHAFED AGAINST A BLD AIR TUBE AT THE MIX VLV. HYD FLUID WAS SPRAYED UNDER HIGH PRESS DIRECTLY AT THE MIX VLV & WAS ABLE TO ENTER THE ENVIRONMENTAL SYS THROUGH THE COUPLING AT THE MIX VLV. THE HYD LINE WAS REPLACED & THE BLD AIR TUBES CLEANED OF HYD FLUID. ENG RUN WAS PERFORMED & REVEALED NO ABNORMALITIES.

Source: SDR DUFA20140502001 · FAA SDRS
J · 2012-04-26 Matched by certificate designator
N685BA · ATA 7322

THE PILOT WAS ATTEMPTING TO START THE ENGINE WHEN THE EGT TEMP BEGAN TO ACCELERATE TO NEAR THE RED LINE INDICATION. HE ABORTED THE START AND NOTIFIED MX. MX PERSONELL MADE ANOTHER ATTEMPT TO START THE ENGINE BUT AGAIN, THE EGT TEMP BEGAN TO RISE RAPIDLY TO NEAR THE RED LINE SO THE START WAS ABORTED. THE END CAP OF THE P3 CHAMBER ON THE FCU WAS REMOVED AND CORROSION WAS EVIDENT ON THE CAP. UPON FURTHER INVESTIGATION IT WAS NOTED THAT THE TEFLON BACK-UP RING AND THE O-RING ON THE PISTON WERE DETERIORATING AND LEAVING PARTICLES ALONG THE CYLINDER WALL AND INTO THE BOTTOM OF THE CHAMBER. A SERVICEABLE FCU WAS INSTALLED WHICH CORRECTED THE PROBLEM. ENGINEERING WAS CONTACTED AND APPEARED INTERESTED IN INVESTIGATING THE CAUSE HOWEVER NO CONCLUSIONS HAVE BEEN MADE SO FAR.

Source: SDR DUFA201204260001 · FAA SDRS
O · 2011-09-14 Matched by certificate designator
N624CA · ATA 5313

STRINGER 7R CHAFED BY WATER INJECTION LINE BRACKET JUST AFT OF FS 1144.00. REPLACED STRINGER 7R AT FS 1144.00 IAW BOMBARDIER REO 670-53-00-027.

Source: SDR COMA2011091470045 · FAA SDRS
R J · 2011-07-28 Matched by certificate designator
N3108B · ATA 7321

WHILE ON TAKEOFF, THE PILOT BEGAN TO LOSE POWER FROM THE RT ENGINE. HE IMMEDIATELY PULLED THE "STOP & FEATHER" CONTROL AND SECURED THE ENGINE. HE COMPLETED A GO AROUND TO AN UNEVENTFUL LANDING. MX WAS CALLED AND IT WAS DISCOVERED THAT ONE OF THE O-RINGS THAT SEALED THE START PRESSURE REGULATOR TO THE FUEL CONTROL UNIT HAD FAILED. THIS CAUSED A LOSS OF FUEL PRESSURE TO THE FUEL CONTROL. NEW O-RINGS WERE INSTALLED AND THE ENGINE WAS GROUND RUN AND LEAK CHECKED WITH NO DISCREPANCIES NOTED.

Source: SDR DUFA20110002 · FAA SDRS
O · 2011-01-07 Matched by certificate designator
N685BA · ATA 3251

AFTER START UP, THE PILOT WAS STARTING HIS TAXI ROLL WHEN THE ACFT BEGAN TO TURN LT. HE MADE SEVERAL ATTEMPTS TO CORRECT IT BUT THE ACFT CONTINUED LT UNTIL IT WAS HARD OVER. THE ACFT WAS BROUGHT IN AND THE PROBLEM COULD NOT BE DUPLICATED. THE POTS FROM THE ACTUATOR AND RUDDER PEDALS WERE REMOVED AND OHMED OUT. THE WIRING AND CONNECTORS WERE INSPECTED AND CHECKED OK. THE NWS SERVO VALVE WAS REMOVED AND SWAPPED WITH A KNOWN SERVICEABLE UNIT FROM ANOTHER ACFT AND BOTH OPS CHECKED OK. THE FOLLOWING DAY THE SUSPECT VALVE WHICH HAD BEEN INSTALLED ON ANOTHER ACFT FAILED WITH A UNCOMMANDED HARD LT TURN WHILE TAXIING. THERE APPEARS TO BE AN INTERMITTENT PROBLEM WITH THE SERVO VALVE SO A NEW VALVE WAS PURCHASED AND INSTALLED WHICH OPS CHECKED GOOD.

Source: SDR DUFA20110001 · FAA SDRS
O · 2010-10-28 Matched by certificate designator
N685BA · ATA 3250

AFTER LANDING ROLLOUT AND AT APPROX TAXI SPEED, THE PILOT ENGAGED THE NOSE WHEEL STEERING SYS AND IMMEDIATELY ENCOUNTERED AN UNCOMMANDED HARD LT TURN. THE PILOT WAS ABLE TO STOP THE ACFT WITH ONLY THE NOSE WHEEL OFF THE EDGE OF THE RUNWAY. THE ACFT WAS PUSHED BACK ON THE RUNWAY AND TOWED TO MX. THE HYD MULE WAS CONNECTED TO THE ACFT AND THE NOSE WHEEL SYS ACTIVATED WHICH OPERATED NORMALLY. THE WIRING HARNESSES AND CONNECTOR PINS AND SOCKETS WERE INDIVIDUALLY CHECKED WITH NO PROBLEMS NOTED. AFTER SEVERAL ATTEMPTS, THE PROBLEM COULD NOT BE DUPLICATED. MX WAS UNABLE TO DETERMINE THE CAUSE AT THIS TIME.

Source: SDR DUFA20100007 · FAA SDRS
J · 2010-05-03 Matched by certificate designator
N572GW · ATA 7321

WHILE ON APPROACH, THE PILOT WAS INSTRUCTED BY ATC TO REDUCE POWER AND SLOW THE ACFT IN ORDER TO MAINTAIN SEPARATION. IN THIS ATTEMPT, HE WAS UNABLE TO GET THE RT ENGINE TO REDUCE POWER BELOW 54 PERCENT TORQUE INDICATION. HE DECLARED A MISSED APPROACH AND INITIATED A GO AROUND SITUATION. AFTER SOME EVALUATION OF ENGINE CONTROL, THE PILOT DECIDED TO SHUTDOWN THE RT ENGINE AS A PRECAUTIONARY MEASURE. HE CONTINUED ON HIS APPROACH AND MADE AN UNEVENTFUL LANDING. UPON EVALUATION BY MX PERSONNEL, AN ABNORMAL CLICKING NOISE COULD BE HEARD COMING FROM THE FUEL CONTROL UNIT. THE FUEL CONTROL UNIT WAS REMOVED AND A REPLACEMENT ORDERED.

Source: SDR DUFA20100006 · FAA SDRS
Y · 2010-01-19 Matched by certificate designator
N3796C · ATA 8520

WHILE IN CRUISE FLIGHT, THE PILOT REPORTED THE LT ENG SUDDENLY LOST FUEL FLOW AND RPM. HE ATTEMPTED TO RESTART THE ENGINE SELECTING OTHER FUEL SOURCES WITHOUT SUCCESS. HE THEN FEATHERED THE PROPELLER AND PROCEEDED TO THE NEAREST SUITABLE AIRPORT WHERE HE MADE AN UNEVENTFUL LANDING. UPON ARRIVAL, MX WAS NOTIFIED AND A MECHANIC DISPATCHED TO INVESTIGATE THE POSSIBLE CAUSE. WHEN THE ENG COWLING WAS REMOVED IT WAS DISCOVERED THAT THE NR 5 CONNECTING ROD HAD FAILED AND PUNCTURED A HOLE IN THE TOP OF THE ENG CASE. THE DIPSTICK WAS PULLED AND FOUND TO STILL HAVE TEN QUARTS OF OIL REMAINING. NO DEFINITE CAUSE OF THE ROD FAILURE IS KNOWN AT THIS TIME.

Source: SDR DUFA20100005 · FAA SDRS
R J · 2009-10-02 Matched by certificate designator
N3116N · ATA 7321

WHILE ON DESCENT DURING APPROACH, PILOT NOTICED AN UNCOMMANDED CHANGE IN PWR ON NR 2 ENG. ATTEMPTED TO ADVANCE PWR LEVER WITH NO INCREASE IN PWR NOTED. CONTINUED HIS DESCENT WHEN HE NOTICED AN UNCOMMANDED PWR INCREASE ON THE NR 2 ENG. THEN MADE DECISION TO SHUTDOWN AND SECURE ENG. CONTINUED APPROACH AND MADE AN UNEVENTFUL LANDING. AFTER SEVERAL ATTEMPTS BY MX, THE DISCREPANCY COULD NOT BE DUPLICATED. TEST FLIGHT WAS PERFORMED AND PROBLEM WAS CONFIRMED. AFTER SEVERAL FUNCTIONAL CHECKS,FCU WAS THE SUSPECTED PROBLEM. UPON REMOVAL OF P2T2 SENSOR AND P3 REFERENCE LINE, CORROSION WAS NOTED AT BELLOPHRAGM CHAMBER INLET. COVER WAS REMOVED AND CORROSION NOTED WITHIN BELLOPHRAGM CHAMBER. FCU WAS REPLACED WITH AN OVERHAULED UNIT. NO SOURCE COULD BE DETERMINED AS TO THE CAUSE OF THE CORROSION BUILD UP.

Source: SDR DUFA20090004 · FAA SDRS
N · 2008-11-26 Matched by certificate designator
N158MC · ATA 2613

WHILE ON CLIMB OUT, THE PILOT NOTICED THAT THE RT WING OVERHEAT LIGHT ILLUMINATED. THE RT GENERATOR WAS SHUT DOWN, BLEED AIR TURNED OFF AND THE LANDING GEAR EXTENDED. AFTER 3 MINUTES THE LIGHT WAS STILL ILLUMINATED AND PROCEDURES CALL OUT FOR ENGINE SHUT DOWN. SHORTLY AFTER ENGINE SHUT DOWN THE LIGHT EXTINGUISHED. THE PILOT INFORMED THE TOWER OF HIS SITUATION AND WAS CLEARED TO RETURN TO THE AIRPORT WHERE HE MADE AN UNEVENTFUL LANDING. UPON INVESTIGATION, NO EVIDENCE OF FIRE OR OVERHEATING COULD BE FOUND IN THE WING AND GEAR WELL AREAS. A NEW DUCT SENSOR WAS INSTALLED AS A PRECAUTION.

Source: SDR DUFA20080003 · FAA SDRS
K · 2008-07-10 Matched by certificate designator
N3108B · ATA 7261

WHILE ENROUTE, THE PILOT NOTICED HIS LT ENGINE OIL PRESSURE GAUGE FLUCTUATING. SHORTLY THERE AFTER THE "LOW OIL PRESSURE" LIGHT ILLUMINATED. SINCE HE WAS VERY CLOSE TO HIS DESTINATION, THE PILOT ELECTED TO SHUTDOWN THE ENGINE AND SECURE IT AS A PRECAUTION. PILOT MADE UNEVENTFUL SINGLE ENGINE LANDING. UPON INVESTIGATION MY MAINT , IT WAS DISCOVERED THAT THE OIL PRESSURE LINE DAMPER FITTING O-RING HAD FAILED AND ALLOWED OIL TO SEEP PAST THE FITTING. THIS DEPLETED THE ENGINE OIL SUPPLY UNTIL, THERE WAS AN INSUFFICIENT AMOUNT TO MAINTAIN THE PROPER PRESSURE. A NEW O-RING WAS INSTALLED AND GROUND RUNS PERFORMED WITH NO LEAK NOTED. (K)

Source: SDR DUF2008F00000 · FAA SDRS
N · 2008-01-03 Matched by certificate designator
N159MC · ATA 2613

WHILE ON CLIMB OUT, THE PILOT NOTICED THAT THE LT WING OVERHEAT LIGHT ILLUMINATED. FOLLOWING PROCEDURE, THE LT GENERATOR WAS SHUTDOWN, BLEED AIR TURNED OFF AND THE LANDING GEAR EXTENDED. AFTER 3 MINUTES THE LIGHT WAS STILL ILLUMINATED AND PROCEDURES CALL OUT FOR ENGINE SHUTDOWN. SHORTLY AFTER ENGINE SHUTDOWN THE LIGHT EXTINGUISHED. THE PILOT INFORMED THE TOWER OF HIS SITUATION AND WAS CLEARED TO RETURN TO WHERE HE MADE AN UNEVENTFUL LANDING. UPON INVESTIGATION, NO EVIDENCE OF FIRE OR OVERHEATING COULD BE FOUND IN THE WING AND GEAR WELL AREAS. IT IS SUSPECTED THAT DUE TO HIGH WINDS DURING THE PILOT’S BACK TAXI TO THE ACTIVE RUNWAY, HE MAY HAVE HAD TO APPLY CONSTANT BRAKE PRESSURE TO KEEP HIS TAXI SPEED LOW. THIS WOULD HAVE CAUSED EXCESSIVE HEATING OF THE BRAKE ASSEMBLY AND ONCE THE GEAR WAS RETRACTED, CAUSED THE WING OVERHEAT LIGHT TO COME ON. IT WAS ALSO REPORTED THAT THE CABIN HEAT WAS SELECTED TO THE FULL HOT POSITION, WHICH MAY HAVE ALSO BEEN A FACTOR.

Source: SDR DUFA010308001 · FAA SDRS
N · 2008-01-03 Matched by certificate designator
N159MC · ATA 2613

WHILE ON CLIMB OUT, THE PILOT NOTICED THAT THE LT WING OVERHEAT LIGHT ILLUMINATED. FOLLOWING PROCEDURE, THE LT GENERATOR WAS SHUTDOWN, BLEED AIR TURNED OFF AND THE LANDING GEAR EXTENDED. AFTER 3 MINUTES THE LIGHT WAS STILL ILLUMINATED AND PROCEDURES CALL OUT FOR ENGINE SHUTDOWN. SHORTLY AFTER ENGINE SHUTDOWN THE LIGHT EXTINGUISHED. THE PILOT INFORMED THE TOWER OF HIS SITUATION AND WAS CLEARED TO RETURN TO DEPARTURE WHERE HE MADE AN UNEVENTFUL LANDING. UPON INVESTIGATION, NO EVIDENCE OF FIRE OR OVERHEATING COULD BE FOUND IN THE WING AND GEAR WELL AREAS. IT IS SUSPECTED THAT DUE TO HIGH WINDS DURING THE PILOT’S BACK TAXI TO THE ACTIVE RUNWAY, HE MAY HAVE HAD TO APPLY CONSTANT BRAKE PRESSURE TO KEEP HIS TAXI SPEED LOW. THIS WOULD HAVE CAUSED EXCESSIVE HEATING OF THE BRAKE ASSEMBLY AND ONCE THE GEAR WAS RETRACTED, CAUSED THE WING OVERHEAT LIGHT TO COME ON. IT WAS ALSO REPORTED THAT THE CABIN HEAT WAS SELECTED TO THE FULL HOT POSITION, WHICH MAY HAVE ALSO BEEN A FACTOR.

Source: SDR DUFA20080001 · FAA SDRS
N · 2008-01-03 Matched by certificate designator
N3116N · ATA 2613

WHILE ON CLIMB OUT, THE PILOT NOTICED THAT THE RT WING OVERHEAT LIGHT ILLUMINATED. FOLLOWING PROCEDURE, THE LT GENERATOR WAS SHUTDOWN, BLEED AIR TURNED OFF AND THE LANDING GEAR EXTENDED. AFTER APPROXIMATELY ONE MINUTE THE LIGHT EXTINGUISHED. THE FLIGHT CONTINUED WITHOUT ANY PROBLEMS. UPON INVESTIGATION, NO EVIDENCE OF FIRE OR OVERHEATING COULD FOUND IN THE WING AND GEAR WELL AREAS. IT IS SUSPECTED THAT DUE TO HIGH WINDS DURING THE PILOT’S BACK TAXI TO THE ACTIVE RUNWAY, HE MAY HAVE HAD TO APPLY CONSTANT BRAKE PRESSURE TO KEEP HIS TAXI SPEED LOW. THIS WOULD HAVE CAUSED EXCESSIVE HEATING OF THE BRAKE ASSEMBLY AND ONCE THE GEAR WAS RETRACTED, CAUSED THE WING OVERHEAT LIGHT TO COME ON. IT WAS ALSO REPORTED THAT THE CABIN HEAT WAS SELECTED TO THE FULL HOT POSITION, WHICH MAY HAVE ALSO BEEN A FACTOR.

Source: SDR DUFA20080002 · FAA SDRS
J · 2008-01-03 Matched by certificate designator
N159MC · ATA 2613

WHILE ON CLIMB OUT, THE PILOT NOTICED THAT THE LT WING OVERHEAT LIGHT ILLUMINATED. FOLLOWING PROCEDURE, THE LT GENERATOR WAS SHUTDOWN, BLEED AIR TURNED OFF AND THE LANDING GEAR EXTENDED. AFTER 3 MINUTES THE LIGHT WAS STILL ILLUMINATED AND PROCEDURES CALL OUT FOR ENGINE SHUTDOWN. SHORTLY AFTER ENGINE SHUTDOWN THE LIGHT EXTINGUISHED. THE PILOT INFORMED THE TOWER OF HIS SITUATION AND WAS CLEARED TO RETURN TO DEPARTURE, WHERE HE MADE AN UNEVENTFUL LANDING. UPON INVESTIGATION, NO EVIDENCE OF FIRE OR OVERHEATING COULD BE FOUND IN THE WING AND GEAR WELL AREAS. IT IS SUSPECTED THAT DUE TO HIGH WINDS DURING THE PILOT’S BACK TAXI TO THE ACTIVE RUNWAY, HE MAY HAVE HAD TO APPLY CONSTANT BRAKE PRESSURE TO KEEP HIS TAXI SPEED LOW. THIS WOULD HAVE CAUSED EXCESSIVE HEATING OF THE BRAKE ASSEMBLY AND ONCE THE GEAR WAS RETRACTED, CAUSED THE WING OVERHEAT LIGHT TO COME ON. IT WAS ALSO REPORTED THAT THE CABIN HEAT WAS SELECTED TO THE FULL HOT POSITION, WHICH MAY HAVE ALSO BEEN A FACTOR.

Source: SDR EAC0705 · FAA SDRS
K J · 2007-08-16 Matched by certificate designator
N3796C · ATA 3710

WHILE IN CRUISE FLIGHT, THE PILOT NOTICED OIL STREAMING FROM THE TOP OF THE LT ENGINE COWL. THE OIL PRESSURE WAS STILL IN THE NORMAL OPERATING RANGE AND THE ENGINE APPEARED TO BE OPERATING NORMALLY. AS A PRECAUTION, THE LT ENGINE WAS SHUTDOWN AND SECURED. THE PILOT DEVIATED TO THE NEAREST AIRPORT WHERE HE MADE AN UNEVENTFUL LANDING. UPON INVESTIGATION BY MAINTENANCE, IT WAS DISCOVERED THAT THE WET SYSTEM VACUUM PUMP DRIVE HAD SHEARED AND CAUSED THE GARLOCK SEAL TO DISINTEGRATE, ALLOWING OIL TO SEEP PAST IT.

Source: SDR DUFA081607001 · FAA SDRS
K J · 2007-08-16 Matched by certificate designator
N3796C · ATA 3700

WHILE IN CRUISE FLIGHT THE PILOT NOTICED OIL STREAMING FROM THE TOP OF THE LT ENGINE COWL. THE OIL PRESSURE WAS STILL IN THE NORMAL OPERATING RANGE AND THE ENGINE APPEARED TO BE OPERATING NORMALLY. AS A PRECAUTION, THE LT ENGINE WAS SHUTDOWN AND SECURED. THE PILOT DEVIATED TO THE NEAREST AIRPORT WHERE HE MADE AN UNEVENTFUL LANDING. UPON INVESTIGATION BY MAINTENANCE, IT WAS DISCOVERED THAT THE WET SYSTEM VACUUM PUMP DRIVE HAD SHEARED AND CAUSED THE GARLOCK SEAL TO DISINTEGRATE, ALLOWING OIL TO SEEP PAST.

Source: SDR DUFA20070004 · FAA SDRS
N · 2007-04-17 Matched by certificate designator
N159MC · ATA 2613

SHORTLY AFTER DEPARTURE, THE LT WING OVERHEAT LIGHT ILLUMINATED. FOLLOWING PROCEDURE, THE PILOT SHUTDOWN THE LT GENERATOR, LT BLEED AIR AND EXTENDED THE LANDING GEAR. THE LIGHT REMAINED ILLUMINATED SO THE LT ENGINE WAS SHUTDOWN AS A PRECAUTIONARY MEASURE AND THE PILOT RETURNED TO FSD AND MADE AN UNEVENTFUL LANDING. AN INVESTIGATION BY MAINTENANCE COULD NOT REVEAL A CAUSE OTHER THAN A POSSIBLE BRAKE HEATING UP DURING TAXI TO THE RUNWAY OR CABIN TEMP CONTROL SET TO MAX HEAT. MAINTENANCE COULD NOT DUPLICATE.

Source: SDR DUFA041707 · FAA SDRS
N · 2007-04-17 Matched by certificate designator
N159MC · ATA 2613

SHORTLY AFTER DEPARTURE, THE LT WING OVERHEAT LIGHT ILLUMINATED. FOLLOWING PROCEDURE, THE PILOT SHUTDOWN THE LT GENERATOR, LT BLEED AIR AND EXTENDED THE LANDING GEAR. THE LIGHT REMAINED ILLUMINATED SO THE LT ENGINE WAS SHUTDOWN AS A PRECAUTIONARY MEASURE AND THE PILOT RETURNED TO FSD AND MADE AN UNEVENTFUL LANDING. AN INVESTIGATION BY MAINTENANCE COULD NOT REVEAL A CAUSE OTHER THAN A POSSIBLE BRAKE HEATING UP DURING TAXI TO THE RUNWAY OR CABIN TEMP CONTROL SET TO MAX HEAT. MAINTENANCE COULD NOT DUPLICATE.

Source: SDR DUFA20070003 · FAA SDRS
E · 2007-04-10 Matched by certificate designator
N80BS · ATA 8530

WHILE ON APPROACH TO AIRPORT, THE PILOT NOTICED MANIFOLD PRESSURE DROPPING AS WELL AS OIL PRESSURE FROM THE RT ENGINE. HE ALSO BEGAN TO FEEL A VIBRATION FROM THE SAME ENGINE. HE ELECTED TO SHUT THE ENGINE DOWN AND MADE AN UNEVENTFUL LANDING. UPON INSPECTION, THE NR 5 CYLINDER HOLD DOWN STUDS HAD SHEARED AND ALLOWED THE CYLINDER TO HAMMER AGAINST THE ENGINE CASE AND COWLING. THIS IN TURN RIPPED THE RT EXHAUST STACK FROM THE NR 1 AND NR 5 CYLINDERS CAUSING HEAT DISTRESS AT THE COWL DOOR.

Source: SDR DUFA041007001 · FAA SDRS
E · 2007-04-10 Matched by certificate designator
N80BS · ATA 8530

WHILE ON APPROACH TO AIRPORT, THE PILOT NOTICED MANIFOLD PRESSURE DROPPING AS WELL AS OIL PRESSURE FROM THE RIGHT ENGINE. HE ALSO BEGAN TO FEEL A VIBRATION FROM THE SAME ENGINE. HE ELECTED TO SHUT THE ENGINE DOWN AND MADE AN UNEVENTFUL LANDING. UPON INSPECTION, THE NR 5 CYLINDER HOLD DOWN STUDS HAD SHEARED AND ALLOWED THE CYLINDER TO HAMMER AGAINST THE ENGINE CASE AND COWLING. THIS IN TURN RIPPED THE RT EXHAUST STACK FROM THE NR 1 AND NR 5 CYLINDERS CAUSING HEAT DISTRESS AT THE COWL DOOR.

Source: SDR DUFA20070002 · FAA SDRS
P · 2006-09-13 Matched by certificate designator
N430MA · ATA 3260

LEFT MAIN DOWN LIGHT FAILED TO ILLUMINATE. FLYOVER SHOWED GEAR DOWN. ANNUNCIATOR CONTACTS WERE CLEANED. GEAR WAS CYCLED AND DISCREPANCY WAS CLEARED.

Source: SDR 2006F00038 · FAA SDRS
N · 2006-09-13 Matched by certificate designator
N430MA · ATA 3260

LEFT LANDING GEAR INDICATION SHOWED GEAR NOT DOWN. CLEANED ANNUNCIATOR CONTACTS. OPS CHECK OK.

Source: SDR 2006F00039 · FAA SDRS
R · 2006-08-02 Matched by certificate designator
N80BS · ATA 7310

PILOT REPORTED THAT WHILE IN CRUISE FLIGHT THE LEFT ENGINE FUEL FLOW SUDDENLY DROPPED OFF AND THE ENGINE BEGAN TO RUN ROUGH AND LOSE POWER. THE BOOST PUMP WAS SELECTED TO HIGH AND THE MIXTURE INCREASED TO FULL RICH WHICH HAD LITTLE EFFECT. THE PILOT CONTACTED DISPATCH AND MAINTENANCE AND AFTER A SHORT DISCUSSION, MAINTENANCE RECOMMENDED THE ENGINE BE SHUT DOWN AND SECURED TO PREVENT THE POSSIBILITY OF FIRE. THE PILOT SHUT DOWN THE ENGINE AND MADE AN UNEVENTFUL LANDING. THE ENGINE WAS UNCOWLED AND IT WAS DISCOVERED THAT THE UPPER DECK PRESSURE LINE HAD PULLED OUT OF THE FITTING AT THE LEFT AND RIGHT JUNCTION TEE. THE LINE WAS REPAIRED AND GROUND RUNS REVEALED NO OTHER ABNORMALITIES.

Source: SDR BAC001 · FAA SDRS
R · 2006-08-02 Matched by certificate designator
N80BS · ATA 2844

PILOT REPORTED THAT WHILE IN CRUISE FLIGHT THE LT ENGINE FUEL FLOW SUDDENLY DROPPED OFF AND THE ENGINE BEGAN TO RUN ROUGH AND LOSE POWER. THE BOOST PUMP WAS SELECTED TO HIGH AND MIXTURE INCREASED TO FULL RICH WHICH HAD LITTLE EFFECT. THE PILOT CONTACTED DISPATCH AND MAINTENANCE AND AFTER A SHORT DISCUSSION, MAINTENANCE RECOMMENDED THE ENGINE BE SHUTDOWN AND SECURED TO PREVENT THE POSSIBILITY OF FIRE. THE PILOT SHUT THE ENGINE DOWN AND MADE AN UNEVENTFUL LANDING. THE ENGINE WAS UNCOWLED AND IT WAS DISCOVERED THE UPPER DECK PRESSURE LINE HAD PULLED OUT OF IT'S FITTING AT THE LT AND RT JUNCTION TEE. THE LINE WAS REPAIRED AND GROUND RUNS REVEALED NO OTHER ABNORMALITIES.

Source: SDR BAC005 · FAA SDRS
B · 2005-03-28 Matched by certificate designator
N159MC · ATA 2910

JUST BEFORE LANDING, HYDRAULIC VAPOR/SMOKE NOTED IN CABIN AND COCKPIT. AIRCRAFT LANDED WITHOUT INCIDENT, ENGINES SHUTDOWN AND PAX DEPLANED. MAINTENANCE FOUND FAILED HYDRAULIC LINE IN WING ROOT THAT SPRAYED FLUID INTO AIR CYCLE MACHINE INTAKE WHICH TRANSFERRED VAPOR TO CABIN.

Source: SDR MR0510 · FAA SDRS
K J · 2005-03-23 Matched by certificate designator
N371PH · ATA 2910

WHILE EN ROUTE FROM SIOUX FALLS, SD TO RAPID CITY, SD THE PILOT NOTICED THE HYDRAULIC PRESSURE WAS FLUCTUATING ON THE LEFT HAND ENGINE. SHORTLY THEREAFTER THE RIGHT HAND PRESSURE BEGAN TO FLUCTUATE. THE PILOT REQUESTED CLEARANCE TO RETURN TO SIOUX FALLS WHICH WAS GRANTED. EMERGENCY VEHICLES WERE DISPATCHED AS A PRECAUTION AND AN UNEVENTFUL LANDING WAS PERFORMED. INVESTIGATION REVEALED THAT A HYDRAULIC PRESSURE LINE HAD RUPTURED.

Source: SDR 2005F00062 · FAA SDRS
F · 2005-03-03 Matched by certificate designator
N3796C · ATA 6122

WHILE IN CRUISE FLIGHT, THE RT ENGINE BEGAN TO LOSE RPM. THE PILOT PUSHED THE PROPELLER CONTROL LEVER ALL THE WAY FORWARD TO MAX RPM WITH NO CHANGE. THE PILOT DESCENDED AND MADE AN UNEVENTFUL LANDING. THE RT ENGINE QUIT ON ROLL OUT AND THE RT PROPELLER WENT INTO FEATHER. THE PROPELLER GOVERNOR WAS REMOVED AND APPEARED TO HAVE AN INTERNAL FAILURE. A SERVICEABLE GOVERNOR WAS INSTALLED AND OPS CHECKED OK.

Source: SDR 2005F00040 · FAA SDRS
R · 2005-03-03 Matched by certificate designator
N3796C · ATA 6122

WHILE IN CRUISE FLIGHT, THE RT ENGINE BEGAN TO LOSE RPM. THE PILOT PUSHED THE PROPELLER CONTROL LEVER ALL THE WAY FORWARD TO MAX RPM WITH NO CHANGE. THE PILOT DESCENDED AND MADE AN UNEVENTFUL LANDING. THE RT ENGINE QUIT ON ROLL OUT AND THE RT PROPELLER WENT INTO FEATHER. THE PROPELLER GOVERNOR WAS REMOVED AND APPEARED TO HAVE AN INTERNAL FAILURE. A SERVICABLE GOVERNOR WAS INSTALLED AND OPS CHECKED OK.

Source: SDR 2005F00041 · FAA SDRS
D · 2005-01-05 Matched by certificate designator
N3108B · ATA 5610

WHILE ON CLIMB OUT, THE PILOTS WINDSHIELD BLEW OUT AND CAUSED A RAPID DE-COMPRESSION OF THE AIRCRAFT. THE PILOT TOOK EMERGENCY ACTION AND PERFORMED A RAPID DECENT TO A SUITABLE ALTITUDE. NO COMMUNICATION COULD BE ESTABLISHED WITH ANYONE DUE TO THE DAMAGE DONE TO THE PILOTS HEADSET SO 7700 WAS SQUAWKED ON THE AIRCRAFT TRANSPONDER. THE PILOT MOVED INTO THE RIGHT SEAT AND RETURNED TO THE AIRPORT, WHERE HE MADE AN UNEVENTFUL LANDING. AFTER QUESTIONING THE PILOT ABOUT THE INCIDENT, IT CAN ONLY BE SPECULATED THAT BECAUSE OF THE SEVERE COLD AIR (-40) AND WITH THE WINDSHIELD HEAT SELECTED ON, A FRACTURED DEVELOPED IN THE OUTER WINDOWPANE ALLOWING IT TO FAIL.

Source: SDR 2005F00000 · FAA SDRS
B · 2004-12-31 Matched by certificate designator
N430MA · ATA 2150

ON TOUCHDOWN, THE CREW NOTICED AN ACRID SMELL IN THE COCKPIT. THE CREW LANDED AND TAXIED IN WITH NO FURTHER INCIDENT. TROUBLESHOOTING FOUND THE SOURCE TO THE RT ACM. INITALLY DEFERRED ACM IAW MEL, LATER CHANGED THE ACM, MEL WAS CLEARED. (NM05200403534) (K)

Source: SDR 2005FA0000041 · FAA SDRS
N · 2004-12-18 Matched by certificate designator
N158MC · ATA 2612

RT ENGINE FIRE WARNING LIGHT FLICKERED ON AND OFF DURING CLIMB. CREW RETURNED TO STATION. FAILED FIRE DETECTOR PROBE (CENTER CERAMIC INSULATOR LOOSE). REPLACED FIRE DETECTOR LOCATED BELOW THE OIL COOLER MOUNTED ON THE FIREWALL. (NM05200400110) (K)

Source: SDR 2005FA0000040 · FAA SDRS
J · 2004-12-06 Matched by certificate designator
N430MA · ATA 7261

MRR-M04-23, NR 2 ENGINE OIL PRESSURE LIGHT CAME ON AS FLIGHT LEVELED OUT IN CRUISE, OIL PRESSURE GAUGE WAS CHECKED AND FOUND PRESSURE DROPPING. CREW DID A PRECAUTIONARY INFLIGHT SHUTDOWN, AND RETURNED TO STATION. LOSS OF OIL PRESSURE DUE TO LOSS OF OIL FRM REAR SCAVANGE PUMP AREA. REMOVED ENGINE, REPLACED SCAVANGE PUMP AND REINSTALLED ENGINE. MFG HAS CHANGED PUMP DESIGN TO DECREASE REAR SCAVANGE PUMP FAILURES. (K)

Source: SDR 2005FA0000064 · FAA SDRS
B · 2004-11-29 Matched by certificate designator
N80BS · ATA 2434

WHILE IN CRUISE FLIGHT, THE PILOT NOTICED SPARKS COMING FROM THE LEFT ENGINE FORWARD COWL AREA. AS A PRECAUTION, THE ENGINE WAS SHUTDOWN AND SECURED. THE AIRCRAFT THEN MADE AN UNEVENTFUL LANDING. UPON INVESTIGATION, IT WAS DISCOVERED THAT THE ALTERNATOR OUT SENSOR SHORTED INTERNALLY AND HAD BURNED A HOLE THROUGH THE END OF IT'S CASE. THE SENSOR WAS REPLACED AND AN OPS CHECK PROVED SATISFACTORY.

Source: SDR 2004F00429 · FAA SDRS
K J · 2004-06-02 Matched by certificate designator
N159MC · ATA 7310

MRR-M04-11, ENGINE RPM ONLY WENT TO 97 PERCENT DURING TAKEOFF ROLL AND TORQUE WAS ALSO LOW, ALSO, THERE WAS LITTLE RESPONSE TO POWER LEVER MOVEMENT. CREW ABORTED TAKEOFF AND RETURNED TO THE GATE. INITIALLY SUSPECTED FCU FAILURE, BUT UPON INSPECTION FOUND FCU INPUT ARM ROD END DISCONNECTED. RECONNECTED ROD END AND SAFETIED. A FUEL LEAK WAS NOTED WHEN COWLING WAS OPENED, AND WAS FOUND TO BE COMING FROM THE SECONDARY FUEL MANIFOLD LOCATED AT THE 8:00 O’CLOCK POSITION. THE FUEL MANIFOLD LINE WAS REPLACED. MR`S WERE ISSUED TO INSPECT ALL OTHER AIRCRAFT FUEL MANIFOLD LINES, FUEL NOZZLE TASK CARD WAS ISSUED TO INCLUDE INSPECTION OF THE MANIFOLD LINES AT EACH INSPECTION.

Source: SDR 2005FA0000053 · FAA SDRS
J · 2004-05-03 Matched by certificate designator
N159MC · ATA 5230

THE CARGO DOOR WARNING LIGHT CAME ON DURING CLIMBOUT, CREW RETURNED TO STATION. ONE OF THE FOLLOWING: DOOR CLOSING PROCEDURES, DOOR HARD TO CLOSE, DOOR CLICKCLACK RIGGING/ LUBRICATION, OR SWITCH RIGGING. MAINTENANCE FOUND HANDLE NOT FULLY ROTATED TO CLOSED POSITION, CHECKED DOOR AND CLICKCLACKS, RECLOSED THE DOOR AND STOWED THE HANDLE, NO FURTHER PORBLEMS NOTED. CREW CONTINUED FLIGHT WITH NO FURTHER INCIDENTS. (NM05200404459) (K)

Source: SDR 2005FA0000048 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N103RCCESSNA 4041977Valid RegistrationMatched by certificate designator
N158MCFAIRCHILD SA227-AC1988Valid RegistrationMatched by certificate designator
N159MCFAIRCHILD SA227-ACValid RegistrationMatched by certificate designator
N3108BSWEARINGEN SA227-ACValid RegistrationOperator named in NTSB report
N3108BSWEARINGEN SA227-ACValid RegistrationMatched by certificate designator
N366AEFAIRCHILD SA227-AC1987Valid RegistrationMatched by certificate designator
N371PHFAIRCHILD SA227-ACValid RegistrationMatched by certificate designator
N3796CCESSNA 402B1974Valid RegistrationMatched by certificate designator
N3813Matched by certificate designator
N387PHSWEARINGEN SA227-AC1982Valid RegistrationMatched by certificate designator
N402BPOperator named in NTSB report
N430MAFAIRCHILD SA227-ACValid RegistrationMatched by certificate designator
N572GWFAIRCHILD SA227-ACValid RegistrationMatched by certificate designator
N624CACESSNA 402B1975Valid RegistrationMatched by certificate designator
N660EAFAIRCHILD SA227-AC1986Valid RegistrationMatched by certificate designator
N685BAFAIRCHILD SA227-AC1987Valid RegistrationMatched by certificate designator
N690WWFAIRCHILD SA227-AC1987Valid RegistrationMatched by certificate designator
N76MDCESSNA 402B1977Non-citizenMatched by certificate designator
N80BSCESSNA 4041977Valid RegistrationMatched by certificate designator