N810LF

EUROCOPTER AS 350 B3 · 2010 · Valid Registration

Registered owner: AIR METHODS LLC, CO (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AIR METHODS LLC (QMLA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J S F · 2023-03-11 Matched by certificate designator
ATA 7100

ON A FLIGHT FROM SILVER CITY, NM TO MEMORIAL MEDICAL CENTER IN LAS CRUCES. I GOT A YELLOW AND RED GOV LIGHT. I WAS ABOUT 5 MINS FROM KSVC, SO I TURNED AND LANDED AT GRANT COUNTY AIRPORT. AIRCOM WAS ALERTED, AND THEY GOT NATIVE 30 HEADED OVER TO PICK UP OUR PATIENT. I DID A LOW POWERED APPROACH AND LANDED SAFELY. MANAGEMENT ALL NOTIFIED AND MECHANIC ARRIVED AND DETERMINED THE HELICOPTER NEEDED A NEW DECU

Source: SDR 2023FA0000124 · FAA SDRS
B · 2023-03-09 Matched by certificate designator
ATA 3300

ABOUT 30 MINUTES AFTER TAKEOFF FROM GILA REGIONAL WITH A INTERFACILITY TRANSFER THE COCKPIT STARTED TO SMELL STRONGLY LIKE BURNING PLASTIC/RUBBER. NO SMOKE WAS PRESENT AND INSTRUMENTS AND WARNING LIGHT PANEL WAS NORMAL WITH NO INDICATIONS OF A PROBLEM BESIDES THE SMELL. I OPENED VENTS AND WINDOW TO VENT SMELL BUT IT DIDN'T GO AWAY. WE WERE OVER DESOLATE DESERT WITH NO CITY'S OR ROADS. COCHISE COUNTY P33 AIRPORT WAS THE CLOSEST DIVERSION FOR US SO WE ALL DECIDED TO MAKE THE DIVERSION AND WAS PREPARED TO MAKE AN EMERGENCY LANDING THE WHOLE WAY TO P33. AFTER 23 MINUTES WE MADE IT SAFELY TO P33 AND LANDED. WILCOX BASE CAME AND PICKED UP OUR PATIENT AND FINISHED THE TRANSFER WHILE WE HAD THE MECHANIC INSPECT OUR AIRCRAFT. UPON INSPECTION HE DECIDED IT WAS THE HALOGEN LIGHT ON THE CEILING ABOVE THE MED CREW, THE NVG FILTER AND THE SEALANT THAT HOLDS THE FILTER IN WAS ALL BURNT AND CRACKED AND HE FIGURED THAT WAS THE SOURCE OF THE BURNING SMELL AND RETURNED US TO SERVICE AND WE FLEW BACK TO BASE AND LANDED SAFELY

Source: SDR 2023F00079 · FAA SDRS
O · 2022-01-27 Matched by certificate designator
ATA 5300

CORROSION WAS NOTED ON THE LH AND RH SIDE OF THE CABIN FLOOR EDGE. THE DAMAGE WAS REPAIRED VIA BLENDING AND TRIMMING OUT THE DAMAGED PORTION(S) OF THE EDGE FRAME, ALONG WITH FABRICATING AND INSTALLING SPLICE DOUBLER(S) AT LH STA 75.19 AND RH STA 73.19 TO REINFORCE THE DAMAGED AREAS

Source: SDR 2A6D20220127001 · FAA SDRS
O · 2022-01-20 Matched by certificate designator
ATA 5311

THE TRANSMISSION SUPPORT FRAME (PN 350A21-1041-143) HAS CHAFING DAMAGE ON THE LOWER FLANGE FROM AN UNSECURED CABLE. THE DAMAGE IS UNDER THE TRANSMISSION DECK AT THE AFT RH CORNER OF THE TRANSMISSION CUTOUT. THE CHAFING ON THE TRANSMISSION DECK FRAME WITH A LENGTH OF .42” AND WIDTH OF .19” WITH A MAX DEPTH OF .014”.

Source: SDR 2A6D20220120004 · FAA SDRS
O · 2022-01-20 Matched by certificate designator
ATA 5300

THE L/H LATERAL BAGGAGE COMPARTMENT WE IDENTIFIED THE LANDING GEAR’S L/H VIBRATION DAMPENER FITTING WAS GOUGED. DAMAGE LOCATED AT APROX. STA 2700, WL 2550, BL 600L. THE DAMAGE MEASURES L=0.600”, W=0.300”, D=0.025”.

Source: SDR 2A6D20220120003 · FAA SDRS
O · 2022-01-20 Matched by certificate designator
ATA 5300

AIRCRAFT HAS CHAFE DAMAGE ON THE AFT SIDE OF THE 15 DEGREE BULKHEAD LOCATED IN THE L/H LATERAL BAGGAGE COMPARTMENT IN TWO DIFFERENT LOCATIONS. THE DAMAGE IS LOCATED AT APPROXIMATELY STA 2700, WL 2300, AND BL 500L. THE OB DAMAGE MEASURES.2” LONG AND .11” WIDE WITH A MAX DEPTH OF .009”. THE IB DAMAGE MEASURES .4” LONG AND .39” WIDE WITH A MAX DEPTH OF .015”.

Source: SDR 2A6D20220120001 · FAA SDRS
O · 2022-01-20 Matched by certificate designator
ATA 5300

DAMAGE TO THE 15 DEGREE BULKHEAD LH WEB (PN: 350A21-1032.60 IN THE FORM OF CHAFES. THE FIRST CHAFE DAMAGE AREA WAS FOUND NEAR THE X-FRAME AND WAS MEASURED TO BE APPROXIMATELY 0.40” X 0.39” AND 0.015” DEEP; THE SECOND CHAFE DAMAGE AREA WAS FOUND ON THE STIFFENING FEATURE AND WAS MEASURED TO BE APPROXIMATELY 0.20” X 0.11” AND 0.009” DEEP

Source: SDR 2A6D20220120002 · FAA SDRS
O · 2022-01-20 Matched by certificate designator
ATA 5300

AC 7015 HAS CHAFE DAMAGE TO THE L/H X-FRAME’S AFT LOWER LEG LOCATED AT APPROXIMATELY STA 3650, WL 2305, AND BL 430L. THE DAMAGE MEASURES .21” LONG AND .2” WIDE WITH A MAX DEPTH OF .019”.

Source: SDR 2A6D20220120005 · FAA SDRS
O · 2022-01-14 Matched by certificate designator
ATA 7170

DAMAGE TO THE ENGINE DECK (PN: 350A21-1239.20) IN THE FORM OF CHAFES NEAR THE SCUPPER DRAIN. THE DAMAGE AT THE SCUPPER DRAIN WAS MEASURED TO BE 3.90” X 7.40” AND 0.014” DEEP

Source: SDR 2022FA0000022 · FAA SDRS
O · 2019-12-10 Matched by certificate designator
ATA 5315

GOUGING FOUND ON RIB UNDERNEATH CABIN FLOOR AT THE RIB BEHIND THE CO PILOTS COLLECTIVE. GOUGING WAS THROUGH THE COMPLETE THICKNESS OF THE RIB. THE DAMAGE WAS APPROXIMATELY 13/32" IN LENGTH AND LOCATED AT THE BEND RADIUS OF THE RIB. ** THIS AIRCRAFT REMAINS OOS AT THE TIME OF THIS SUBMISSION. **

Source: SDR QMLA2019121019095 · FAA SDRS