N816UA

AIRBUS INDUSTRIE A319-131 · 1998 · Valid Registration

Registered owner: UNITED AIRLINES INC, IL (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
United Air LinesOperator2010-01-10 – 2010-01-10Operator named in NTSB report
UNITED AIRLINES INCOperator2010-01-10 – 2010-01-10Operator named in NTSB report

Accident & incident history

Inc · 2010-01-10 Operator named in NTSB report
AIRBUS INDUSTRIE A319-131 Minor injury Part 121United Air Lines
Source: NTSB case DCA10IA021

Maintenance disclosures

O · 2026-01-06 Matched by certificate designator
ATA 2810

FUEL CAP FOUND MISSING ITEM CREATED TO ACCOUNT PDA FUEL CAP CURRENTLY ON CDL REPLACED FUEL CAP IAW AMM 28-25-41-400-007-A.

Source: SDR CALA2026010912835 · FAA SDRS
O · 2025-06-30 Matched by certificate designator
ATA 2810

REFUEL CAP MISSING ON ARRIVAL. REPLACED MISSING REFUEL/DEFUEL CAP IRW AMM 28-25-41-400-005-A.

Source: SDR CALA2025070306196 · FAA SDRS
O · 2025-04-27 Matched by certificate designator
ATA 2810

PDA 2 FUELERS REPORTED FUEL CAP MISSING. NOTIFIED TOMC CONTROLLER JAY NEWMAN APPROVED CDL FOR FUEL CAP MISSING.REF LOG PAGE 4650533. INSTALLED UNDERWING FUEL CAP REF AMM 28-25-41-400-005

Source: SDR CALA2025043004347 · FAA SDRS
A · 2025-02-22 Matched by certificate designator
ATA 2530

OVEN 105 R11 IN FWD GALLEY HAD SMALL FLAME AND POSSIBLE DAMAGE TO INSIDE. REMOVED THE OVEN AT POSITION R11. INSPECTED THE OVEN EXTERNALLY AND ALSO THE COMPARTMENT FOR THE OVEN. VERIFY NO EVIDENCE OF HEAT DAMAGE IS PRESENT. THE FLAME WAS A PIECE OF FOOD INSIDE THE OVEN. FLAME WAS EXTINGUISHED WITH BOTTLED WATER. REF AMM 25-35-19. INOP STICKER INSTALLED. REPLACED R11 OVEN REF AMM 25-35-19 OPS CHECK GOOD.

Source: SDR CALA2025022602471 · FAA SDRS
B · 2025-01-08 Matched by certificate designator
ATA 3520

REF LP3459199 ENCOUNTERED SEVERE TURBULENCE ON DECENT AT AROUND 5-6K WITH AGGRESSIVE VERTICAL SHIFT OF THE AIRCRAFT THAT DEPLOYED ALL THE O2 MASKS. SMOOTH LANDING WITH AN EMERGENCY DECLARED. FA'S NOTICED A HOT SMELL IN THE CABIN THAT THE FIRE DEPARTMENT SUSPECTS IS COMING FROM THE OXYGEN GENERATORS BEING ACTIVATED DUE PRESENCE OF HEAT. INSPECTION OF THE AIRCRAFT AFTER A CREW REPORT OF EXCESSIVE TURBULENCE WITH NO EXTERIOR STRUCTURAL DEFECTS NOTED.FOUND O2 GENERATOR USED AT SEATS 1AB, 1EF, 2EF, 3EF, AND 1L JUMPSEAT. REPORTED BY LOCAL MAINTENANCE, INSPECTED ALL POSTIONS WHERE MASKS DROPPED REF AMM 35-21-00. CONFIRMED O2 GENERATORS USED AT THE LISTED LOCATIONS WITH THE EXCEPTION BEING 2EF. THE PIN REMAINS INTACT AND OK FOR CONTINUED SERVICE. REPLACED O2 GENERATOR AT 1L JUMPSEAT REF AMM 35-21-42. REPLACED O2 GENERATOR AT 1AB AND 3EF REF AMM 35-21-42. VERIFIED REMOVAL OF THE SHIPPING PIN AND PROPER INSTALLATION OF THE OXYGEN GENERATOR REPLACED O2 GENERATOR ASSEMBLY AND CONTAINER AT 1EF AND 2EF REF AMM 35-21-41. OPERATIONAL TEST OF EMERGENCY OXYGEN SYSTEM REF AMM 35-23-00-710-001-A .

Source: SDR CALA2025011001850 · FAA SDRS
L · 2024-12-16 Matched by certificate designator
ATA 3350

CABIN EMERGENCY LIGHTING BATTERY CAPACITY OPERATIONAL CHECK. FOUND FWD BATTERY PACK 10WL, FAILED RED LIGHT. REPLACED EPSU BATTERY PACK, IAW 33-51-38-400-002-A0, OPS TEST GOOD.

Source: SDR CALA2024121601528 · FAA SDRS
O · 2024-11-21 Matched by certificate designator
ATA 2810

PDA 2 FUEL CAP REPORTED MISSING ON ARRIVAL. UPDATED MAA CODE FIX USING VENDOR MAA SCREEN PLEASE CONTACT TOMC BEFORE COMMENCING ANY WORK. MAC METER INITIATED FOR WITH VENDOR ID V123456 MAC RELATED WORK ORDER 000000003122843 AND PRTR VERIFIED NO LEAKS FROM COUPLING. INSTALLED AN INOP STICKER ADJACENT TO THE REGISTRATION NUMBER ON THE FORWARD INSTRUMENT PANEL. CDL 28A APPLIED. COUPLING VERIFIED NOT LEAKING BY ON CALL TECH ROBERT SCOTT V899913. WORK ORDER 3122843. UPDATED SDR INFORMATION. VERIFIED NO LEAKS FROM COUPLING. INSTALLED AN INOP STICKER ADJACENT TO THE REGISTRATION NUMBER ON THE FORWARD INSTRUMENT PANEL. CDL 28A APPLIED. DISPATCH DESK: 16 NAME: JM DATE: 21-NOV-24- DEFERRED DIRECTLY BY TOMC . INSTALLED FUEL CAP IAW AMM 28-25-41 NO LEAKS THIS ACTION CLEARS CLD 28A PLACARD REMOVED PARTS TRANSACTION ADDED ROTABLE PARTS CHANGE WAS INDICATED - TT # 1339668 SN OFF 0643 CAP, COUPLING R OFF 31-2825-9-0001 0643 ON 31-2825-9-0001 0299 CAP, COUPLING R OFF 31-2825-9-0001 0643 ON 0000

Source: SDR CALA2024112101234 · FAA SDRS
K J · 2024-08-22 Matched by certificate designator
ATA 2910

HYD Y SYSTEM LO PR ECAM MESSAGE WITH THE ASSOCIATED HYD Y RSVR LO LVL AND ENGINE 2 PUMP LO PR MESSAGES..... UPDATED MAA CODE FIX USING VENDOR MAA SCREEN PLEASE CONTACT TOMC BEFORE COMMENCING ANY WORK. CONTACT TOMC 847-700-9980 UPON A WALKAROUND INSPECTION FOUND HYD FLUID ACCUMULATION AT PANEL 196BB, AND THROUGH FURTHER INVESTIGATION FOUND FLUID SAMPLING VALVE LEAKING. REMOVED AND REPLACED O RING AT FLUID SAMPLING VALVE REFERENCE AMM TASK 29-13-34-400-001-A. OPS CHK GOOD, LEAK CHK GOOD. OK FOR SERVICE.PARTS USED: 00-0585-3-0326,QTY :1

Source: SDR CALA2024082600491 · FAA SDRS
O · 2023-10-08 Matched by certificate designator
ATA 5330

FOR THE REPAIR ACCOMPLISHED AT LH FR35 STR30 HOLES, PLANNING TO CONTACT ENGINEERING AFTER 29FEB2024 BUT BEFORE 15MAR2024, FOR THE EC 5331-03055 PART 3 PERMANENT REPAIR REQUIREMENTS. REF LP 5966875. THE EC 5331-03055 PART 3 PERMANENT REPAIR REQUIREMENTS. REF LP 5966875. FOR THE REPAIR ACCOMPLISHED AT LH FR35 STR30 HOLES, PLANNING TO CONTACT ENGINEERING AFTER 29FEB2024 BUT BEFORE 15MAR2024, FOR FOR THE REPAIR ACCOMPLISHED AT LH FR35 STR30 HOLES, PLANNING TO TOMC-APPROVAL FROM SC1ELBYC COMMENT CONTACT ENGINEERING AFTER 29FEB2024 BUT BEFORE 15MAR2024 PER ECRA 5331-03305 Q/C REVIEWED. Q/C REVIEWED. INSPECTIONS CREATED BY AUTODIP PENDING AIRCRAFT RECORDS AUDIT & UPDATE.

Source: SDR CALA2023100903007 · FAA SDRS
O · 2023-10-08 Matched by certificate designator
ATA 5330

ACCOMPLISH PERMANENT REPAIR AT LH FR35 STR30 HOLE 2 AND HOLES A, B, AND C PER PART 3 OF THE LATEST REVISION OF ECRA 5331-03055 ON OR BEFORE 29MAR2024. OR BEFORE 29MAR2024. ACCOMPLISH PERMANENT REPAIR AT LH FR35 STR30 HOLE 2 AND HOLES A, B, AND C PER PART 3 OF THE LATEST REVISION OF ECRA 5331-03055 ON ACCOMPLISH PERMANENT REPAIR AT LH FR35 STR30 HOLE 2 AND HOLES TOMC-APPROVAL FROM SC1ELBYC COMMENT A, B, AND C PER PART 3 OF THE LATEST REVISION OF ECRA 5331-03055 ON OR BEFORE 29MAR2024. Q/C REVIEWED. Q/C REVIEWED. INSPECTIONS CREATED BY AUTODIP PENDING AIRCRAFT RECORDS AUDIT & UPDATE.

Source: SDR CALA2023100903006 · FAA SDRS
O · 2023-09-29 Matched by certificate designator
ATA 5340

RMLG DOOR ACTUATOR FITTING KEEL BEAM HOLE R16 AN R20 PRODUCED CRACK INDICATIONS IN THE 3 POSITION DURING LFEC INSPECTION FWD LUG . ACCOMPLISH A PERMANENT REPAIR FOR HOLES R1, R2, R12, R16, R18, PART 3B OF THE LATEST REVISION OF ECRA 5330-05721 ON OR BEFORE R20, & S2 ON THE KEEL BEAM AND MLG DOOR SUPPORT STRUCTURE PER 14-SEP-2024. INTERIM REPAIR PERFORMED PER PART 1B STEP 1 OF ECRA 5330-05721 TO RH MLG DOOR AND ACTUATOR FITTING HOLES. PER PART 1B STEP 2

Source: SDR CALA2023100302924 · FAA SDRS
O · 2023-09-20 Matched by certificate designator
ATA 5320

AFT CARGO DRAIN MAST EXHAUST VENT INNER RETAINING PLATE HAS CORROSION BETWEEN RH STRG 38 AND 35 BETWEEN FRM 68 AND 69. RMV AND RPL AFT CARGO DRAIN MAST EXHAUST VEN INNER RETAINING PLATE REINFORCEMENT BETWEEN STRG 38R-STGR 35R AND BETWEEN FR68 AND FR69 IAW A319 SRM 51-72-11-911-001 AND SRM 51-72-11-911-002.

Source: SDR CALA2023092202848 · FAA SDRS
O · 2023-09-11 Matched by certificate designator
ATA 5320

R2 PAX DOOR SILL HAS MULTIPLE SPOTS OF CORROSION, ON HAECO LCQ NR 9290565/40565 REMOVED AND REPLACED R2 DOOR SILL FR 66-68 IAW A319 SRM 51-72-11 P 1&2- INSTALLED ATTACHING PARTS IAW A319 SRM 51-72-11.

Source: SDR CALA2023091402777 · FAA SDRS
O · 2023-09-11 Matched by certificate designator
ATA 5320

R2 PAX DOOR SILL AFT CORNER FITTING CORRODED GEN ON H AECO LCQ NR 9290566/40566 REMOVED AND REPLACED AFT CORNER FITTING ON FR 68 RT IAW A319 SRM 51-72-11.

Source: SDR CALA2023091402778 · FAA SDRS
O · 2023-09-04 Matched by certificate designator
ATA 5310

UPON REMOVAL OF R2 DOOR SILL FR 67 FRAME SEGMENT (STRAP) WAS FOUND TO HAVE CRACK ON UPPER I/B REDIUS. GEN BY V061616 ON HAECO LC Q NR 9290815/40815 REMOVED AND REPLACED FRAME SEGMENT STRAP AT FRAME 67 IAW A319 SR M 51-72-11 P 1&2 ACMP BY V052030 INSP BY V079881

Source: SDR CALA2023090502709 · FAA SDRS
O · 2023-09-03 Matched by certificate designator
ATA 5320

R/H FR68 GUSSET #3, HOLE #3 AND #4 HAS A CRACK INDICATION AT THE 12 O''CLOCK POSITION IN FRAME LAYER (A3NB-53-4-6355) GENERATED BY MECH V061632 GENERATED AT HAECO LCQ PER NR 9290457 (40457) REPAIRED RH FR68 GUSSET HOLE #3 HOLE #4 IAW ECRA 5311-02470 AS D IRECTED BY RFTS 60012 ACMP BY MECH V061616 INSP BY V899260

Source: SDR CALA2023090402698 · FAA SDRS
O · 2023-09-03 Matched by certificate designator
ATA 5320

R/H FR68 GUSSET #3 HOLE #3 HAS A INDICATION AT THE 12 O CLOCK PO SITION IN FRAME LAYER GEN BY V061632 ON NR 9290457/ 40457 REPAIRED RH FR68 GUSSET #3 HOLE #3 IAW ECRA 5311-02470 AS DIRECTED BY RFTS 60012.

Source: SDR CALA2023090402699 · FAA SDRS
O · 2023-09-02 Matched by certificate designator
ATA 5300

AFT WET AREA AFT RH SHEAR PLATE CRACKED (A3NB-53-3-6357) PER HAE CO LCQ NON ROUTINE 9290567/40567 GENERATED BY V937268 REMOVED AND REPLACED RH SHEAR PLATE IAW A319 SRM 51-42-11 PAGE 6 AND 7. ACMP BY MECH V944156 INSP BY V061771

Source: SDR CALA2023090402692 · FAA SDRS
O · 2023-09-02 Matched by certificate designator
ATA 5220

RH OVERWING EMERGENCY HATCH HAS SUSPECTED CRACK AT AFT VERTICAL SUPPORT @ RIVET POINTS (A3NB-05-3-6170) PER HAECO LCQ NON ROUTIN E 9290527/40527 GENERATED BY V899260 REMOVED FOR CRACK 2EA ANGLE SEGMENT FWD FR38 & AFT FR39 FROM R/H EMERGENCY DOOR & INSTALLED 2EA NEW ANGLE SEGMENT FWD FR38 & AFT FR39 IAW A319 SRM 51-42-11 PER MECH V913400 INSP V061771

Source: SDR CALA2023090402690 · FAA SDRS
O · 2023-09-02 Matched by certificate designator
ATA 5220

LH OVERWING EMERGENCY EXIT HAS SUSPECTED CRACKS AT FWD AND AFT VERTICAL SUPPORTS @ RIVET POINTS (A3NB-05-3-6171) PER HAECO LCQ NON ROUTINE 9290526/40526 GENERATED BY V899260 REMOVED CRACKED 2EA ANGLE SEGMENT AND INSTALLED NEW 2EA ANGLES SEGMENT FROM LH EMERGENCY DOOR FR38 FWD AND FR39 AFT IAW A319 SRM 51-42-11 ACMP BY MECH V052050 INSP BY V913126

Source: SDR CALA2023090402689 · FAA SDRS
O · 2023-09-02 Matched by certificate designator
ATA 5300

AFT WET AREA AFT L/H SHEAR PLATE MULTIPLE HOLES ARE ELONGATED AND GOUGE (A3NB-53-3-6357) PER HAECO LCQ NON ROUTINE 9290574/40574 GENERATED BY V937268. REMOVED AND REPLACED LH SHEAR PLATE IAW A319 SRM 51-42-11 PAGE 6 ACMP BY MECH V944156 INSP BY V061771

Source: SDR CALA2023090402693 · FAA SDRS
O · 2022-05-11 Matched by certificate designator
ATA 2800

PDA 3 FUEL CAP MISSING REPLACED MISSING FUEL CAP PART CHANGE UPDATE ROTABLE PARTS CHANGE WAS INDICATED - TT # 1613986 SN OFF 2830 CAP, COUPLING R OFF 31-2825-9-0001 2830 ON 31-2825-9-0001 0457

Source: SDR CALA2022051101210 · FAA SDRS
O · 2022-02-24 Matched by certificate designator
ATA 3810

REFERENCE 8020643, NEED TO ACCOMPLISH ECRA 2011-01000 DUE TO POTABLE WATER LEAK. NEED DEEP CLEANING FROM STA 19761FR47 TO STA 26695 FR64 DID INITIAL CLEAN UP ,NEED FURTHER CLEAN FROM STA19761FR47 TO STA26895FR64 WATER LEAK WAS CONFINED TO BELOW THE FLOOR FROM WATER SERVICE TOMC-APPROVAL FROM SC1ELBYC COMMENT PANEL FWD TO FRAME 47 APPROXIMATELY STRINGER 42R TO 42L. APPROVED DIP FOR IN DEPTH CLEANUP TO BE ACCOMPLISHED WITHIN 7 DAYS, PER EC/RA 2011-01000 CARGO COMPARTMENT SPILL, SECTION 2.B. DIP 38-DIP PLEASE INDICATE THAT THE INITIAL CLEANUP HAS BEEN ACCOMPLISHED PER ECRA 2011-01000. ACCOMPLISHED INITIAL CLEANUP NEED DEPH CLEAN UP FROM TOMC APPROVED

Source: SDR CALA2022022400491 · FAA SDRS
O · 2021-07-20 Matched by certificate designator
ATA 3246

#1 MLG TIRE TIE BOLT BROKEN.. FOUND SHEAR TIE BOLT BROKEN AND MISSING FROM FAIRLY NEW TIRE UPDATING SDR REPLACED NUMBER 1 MAIN GEAR TIRE REF AMM32-41-11 WHEEL ASSYMBLY SERIAL NUMBER REMOVED 9336P INSTALLED SERIAL NUMBER 7106P. TIRE REMOVED WAS JUST INSTALLED YESTERDAY AND SHEAR TIE BOLT SHEARED AND FELL OUT, CHECKED BRAKE FOR DAMAGE NONE NOTED

Source: SDR CALA2021072101151 · FAA SDRS
O · 2020-11-04 Matched by certificate designator
ATA 5320

R1 DOOR FRAME 16 STOP FITTING NR 7 LOWER INBOARD HOLE IS CRACKED IN THE WEB AT 1 O'CLOCK AND IN THE INTERCOASTAL AT 7 O'CLOCK REPAIR BEFORE NEXT FLIGHT CONTACT ENGINEERING FOR APPROVED REPAIR INSTRUCTIONS ON HAECO LCQ, REF 9298093 GEN BY V061633. REMOVED AND REPLACED R1 DOOR FRAME 16 STEP FITTING NR 7 INTEROSTAL, IAW A319 SRM 51-42-11-801 AND 51-72-11-911-001. PERFORMED BY MECH V079529 INSP BY N078625 AT HAECO LCQ.

Source: SDR CALA2020110601246 · FAA SDRS
L · 2020-07-26 Matched by certificate designator
ATA 3350

EMERGENCY BATTERY 13WL FAILS TEST.

Source: SDR CALA2020072701078 · FAA SDRS
J · 2020-02-03 Matched by certificate designator
ATA 2913

ECAM AFTER TAKEOFFHYD B LO PRESS REMOVED AND REPLACED THE BLUE HYDRAULIC SYSTEM ELECTRIC POMP PER

Source: SDR CALA2020020300324 · FAA SDRS
O · 2019-04-29 Matched by certificate designator
ATA 7200

PDA 2 ENGINE 2 INBOARD FLEX SEAL SEGMENT IS BENT, BROKEN, CRACKED, WITH PIECE MISSING.

Source: SDR CALA2019042900672 · FAA SDRS
O · 2018-08-24 Matched by certificate designator
ATA 5743

LEFT MLG SIDE STAY UPPER INBD CARDAN BUSHING WAS DAMAGED IN THE INBD FACE. REMOVED TWO INBD SIDE STAY BUSHINGS AND OVERSIZED INBD LUG BORE TO 3.2515 FINAL SIZE. INSTALLED NEW BUSHINGS & HONED TO FINAL DIMENTIONS. SEALED BUSHING FLANGES. INSTALLED NEW GREASE NIPPLES. ALL WORK ACCOMPLISHED IAW SRM 57-26-13-300-023.

Source: SDR CALA2018082701851 · FAA SDRS
O · 2018-08-24 Matched by certificate designator
ATA 5743

LEFT MLG SIDESTAY UPPER CARDAN OTBD BUSHING ROTATING. REMOVED THE BUSHING. THE BORE AND SPOTFACED INBD & OTBD FACES TO REMOVE ALL CORROSION. ACCOMPLISHED ISSURANCE CUTS TO ALL REWORKED AREAS AND RESTORED CHAMFERS. INSTALLED A NEW BUSHING. HONED TO FINAL DIM. INSTALLED NEW TAB WASHER, SPECIAL NUT, SEALED NEW FLANGES & INSTALLED NEW GREASE NIPPLES. ALL WORK ACCOMPLISHED IAW SRM 57-26-13-300-023.

Source: SDR CALA2018082701852 · FAA SDRS
K J · 2018-01-12 Matched by certificate designator
ATA 2910

RESERVOIR LOW DISPLAYED ON UPPER ECAM SCREEN. EMERGENCY DECLARED. FOUND SAFETY VALVE 49GA LEAKING AT SWITCH ASSY. REPLACED LANDING GEAR SAFETY VALVE IAW AMM 32-31-17-000-001, LEAK CHECKED GOOD. COMPLETED MM 32-31-17, TESTED SAFETY VALVE IAW MM 32 -31-00. CHECKED GOOD.

Source: SDR CALA2018011200108 · FAA SDRS
J · 2018-01-01 Matched by certificate designator
ATA 3234

GEAR WOULD NOT EXTEND NORMALLY AFTER CYCLING HANDLE 2 TIMES. HAD TO PERFORM MANUAL EXTENSION. EMERGENCY DECLARED. REMOVED AND REPLACED LDG SELECTOR VALVE REF AMM 32-31-12, EXTENSION & RETRACTION TESTS CHECK NORMAL. REMOVED AND REPLACED LDG SAFETY VALVE REF AMM 32-31-17, REQUIRES OPS CK TASK 32-31-00-710-005-A01. EXTENSION AND RETRACTION OF LANDING GEAR TEST. E AND L/G SAFETY VALVE PER AMM 32-31-12 AND 32-31-17. VERIFIED VERIFIED P/NS WITH IPC, VERIFIED INSTALLATION OF L/G SELECT VALVE REF ECRA 3231-01172 FOR LDG GEAR SELECTOR VALVE INSTALL. PERFORMED TASK 32-31-00-710-005-A01 , ALL OPS CKS NORMAL. ALL OPS CKS FOR NORMAL GEAR RETRACTION & EXTENSION NORMAL REF AMM TASK 32-31-00-720-002-A FUNCTIONAL TEST OF THE NORMAL EXTENSION AND RETRACTION VERIFIED GEAR EXTENSION AND RETRACTION, ALL OPS AND FUNCTIONAL C CHECKS PER AMM 32-31-00-710-005-A01 ALL OPS CKS FOR NORMAL GEAR RETRACTION & EXTENSION NORMAL.

Source: SDR CALA2018010100002 · FAA SDRS
J · 2017-03-29 Matched by certificate designator
ATA 2131

CREW REPORTED AT 6000 FT, CABIN PRESSURE LIGHT ON ECAM. AT 8000 FT, CREW RECEIVED A MASTER CABIN PRESSURE LIGHT. UNABL E TO CONTROL THE PRESSURIZATION AS CABIN CLIMBED. NEVER ASSENDED ABOVE 10000 FEET. TROUBLESHOT IAW TSM 21-31-00-810-831-A, AND FOUND A CPC1 FAULTING. REPLACED CPC1 IAW AMM 21-31-34-400-001-A. OPS TESTED IAW AMM 21-31-00-710-002 -A, BOTH SYSTEMS 1 AND 2 CHECKED OK. SYSTEM OK FOR SERVICE.

Source: SDR CALA2017033100768 · FAA SDRS
O · 2016-08-19 Matched by certificate designator
ATA 2740

HORIZONTAL STAB THSA NO BACK YOKE AFT INNER YOKE FLANGE IS CONTACTING THE BASE OF ROD SPHERE WITH DAMAGE TO FLANGE AND ROD SPHERE (AT THE PRIMER COLORED RINGS ON THE ROD SPHERE). THSA REQUIRES REPLACEMENT IAW EA 2744-01056 REV C OP 002 STEP 5.3. REF AMM27-44-51-400-001-A . REMOVED AND REPLACED THS ACTUATOR

Source: SDR CALA2016082395663 · FAA SDRS
O · 2016-06-08 Matched by certificate designator
ATA 5314

DURING EG 1384, KEELBEAM, INSP 8 HOLES WERE FOUND TO BE DISCREPANT. ALL HOLES REPAIRED IAW ECRA 5330-05721.

Source: SDR CALA2016061395444 · FAA SDRS
M J · 2014-10-02 Matched by certificate designator
ATA 7500

NR 1 ENGINE EGT OVERLIMIT DURING TAKEOFF. FAULTED 2.5 BLEED ACTUATOR. EXCEEDANCE RECORDED WAS 640 FOR 8 SECONDS. REPLACED 2.5 BLEED ACTUATOR IAW AMM 75-31-42-400-010-B13

Source: SDR CALA2014092992321 · FAA SDRS
J · 2014-03-30 Matched by certificate designator
ATA 3130

DFDR FAULT DISPLAYED ON UPPER ECAM. SYS FAULT ECAM AT PARKING INTERMITTENT. NO PREVIOUS HISTORY LAST LEG & PLR NO FAULTS. OPERATIONS CHECKED GOOD IAW AMM 31-33-00-710-007.

Source: SDR CALA2014033190719 · FAA SDRS
J · 2014-02-12 Matched by certificate designator
ATA 7261

ENG 2 OIL QTY GAUGE SHOWING AMBER XX. LATER OIL QTY INDICATOR BECAME NORMAL, SHOWING 26Q TS. REMOVED 2.5 QTS OF OIL IAW AMM 12-13-79, 5 MIN IDLE RUN QTY WITHIN ACCEPTABLE LIMITS & PRESENT IN ECAM AFTER ENG RUN, NO FURTHER SERVICE NEEDED.

Source: SDR CALA2014021290360 · FAA SDRS
K · 2013-12-03 Matched by certificate designator
ATA 2822

FLUID SEEP ON WALK AROUND. FOUND PUMP 37-QA LEAKING. REMOVED PUMP IAW AMM 28-21-51-000-002-A & INSTALLED PUMP IAW AMM 28-21-51-400-002-1 THRU STEP B 8. INSTALL PROC COMPLETED SEE SEQ 9562004.

Source: SDR CALA2013120593485 · FAA SDRS
K · 2013-11-25 Matched by certificate designator
ATA 2820

NR 1 CTR FUEL PUMP LEAKING. REMOVED NR 1 CTR FUEL PUMP REPLACE O-RING SEALS & PUMP, LEAK CHECKED GOOD IAW MM.

Source: SDR CALA2013112693277 · FAA SDRS
O · 2013-09-19 Matched by certificate designator
ATA 3520

O2 MASKS FELL IN ROW 8 DEF. REPACKED & ACCOMPLISHED TEST MT35-00.

Source: SDR CALA2013092391379 · FAA SDRS
O · 2013-09-04 Matched by certificate designator
ATA 2520

SEAT BACK LOOSE & ROCKING AT 11E. SWAPPED A NUT FROM SEAT 32F, SEAT 11E WORKS NORMALLY. DEFER 32F IAW MEL, LOCKED UPRIGHT. INSTALLED LOCK NUT ON 32F SEAT STILL LOCKED UPRIGHT.

Source: SDR CALA2013090591035 · FAA SDRS
O · 2013-08-05 Matched by certificate designator
ATA 2697

NR 1 ENGINE PYLON FWD FIRE EXT BOTTLE WIRES, SEVERED 8 INCHES FROM CONNECTOR 5WE1-A. REPLACED WIRE 2621-19-DL20 2621-20-CF20 AND CONDUIT IAW AWM 26-21-01.

Source: SDR CALA2013080890237 · FAA SDRS
E · 2013-06-16 Unresolved
ATA 2700

AIRFRAME VIBRATION FROM T/O THROUGH 17K FT. SUSPECT LOWER F/O NOSE AREA. ENGINE PARAMETERS NORMAL, FOUND SEAL AT PANEL 191BT AND 191DT SPLIT AND PROTRUDING OUT OF THE GAP. TAPED OVER DAMAGED AREA IAW AMM MT 53-004. COMPLETED VIBRATION SHEET AND TROUBLESHOOTING IAW MT 53-005. DL1493 CREATED TO MONITOR . SEAL WITH AERODYNAMIC SEALANT. SEAL INTACT AND SECURE.

Source: SDR UALA2013061804207 · FAA SDRS
J · 2013-06-13 Unresolved
ATA 3350

CABIN EMERGENCY LIGHTING MESSAGE "EPSU BATTERY AFT LIGHT". REPLACED POWER SUPPLY IAW AMM EST PASSED,

Source: SDR UALA2013061404136 · FAA SDRS
O · 2013-05-21 Unresolved
ATA 5744

LEFT INBD FLAP TRUNNION WORN AT AREA D. BLENDED OUT DAMAGED AREA.

Source: SDR UALA2013052203548 · FAA SDRS
K · 2013-04-13 Unresolved
ATA 2910

ON WALK AROUND, FOUND SMALL HYDRAULIC LEAK FROM GREEN SYSTEM. VERIFIED LOW QTY ON COCKPIT GAUGES. FOUND BRAKE RETURN LINE UNION O-RING BAD. REPLACED O-RING, LEAK CHECKS GOOD.

Source: SDR UALA2013041502565 · FAA SDRS
L · 2013-03-27 Unresolved
ATA 2350

CAPTAIN'S OXYGEN MASK FAILED TEST, NO TRANSMIT OF MICROPHONE. REPLACED OXYGEN MASK. CHECKED GOOD.

Source: SDR UALA2013032801993 · FAA SDRS
O · 2013-03-27 Unresolved
ATA 2520

FORWARD CABIN F/A INBRD JUMP SEAT BROKEN BY 1L. UNTANGLED SEAT-BELTS.

Source: SDR UALA2013032902053 · FAA SDRS
N · 2013-02-23 Unresolved
ATA 3140

MULTIPLE WARNINGS, FLT DIVERTED. REPLACED BOTH FLIGHT WARNING COMPUTERS. PRECAUTIONARY WITH TOMC SUPPORT.

Source: SDR UALA2013022401103 · FAA SDRS
O · 2013-01-18 Unresolved
ATA 4997

ECAM MESSAGE APU AUTO SHUTDOWN DISPLAYED ON UPPER ECAM SCREEN - APU. APU AUTO SHUTDOWN DURING START ON TAXI IN. :"RE-SET" "OPS CHECK OK" HAS MADE THIS ITEM-C. APU ASD W.O. BITE MSG REF: TSM 490000-810-992-A (POSSIBLE WATER INGRESS IN PANEL 121AL). REMOVED IGNITER PLUGS AND FOUND FOULED. REPLACED PLUGS IAW AMM 49-41-41, OPS CHECK GOOD AT THIS TIME.

Source: SDR UALA2013012100325 · FAA SDRS
J · 2013-01-02 Unresolved
ATA 2611

SMOKE DETECTOR FAULT DISPLAYED ON UPPER ECAM. REPLACED AFT PIT SMOKE DETECTOR 6WH. NO HELP, BOTH CHANNELS FAILING DIFFERENT SMOKE DETECTORS EACH TIME TESTED. SLAVED IN KNOWN GOOD DETECTOR NO HELP. TRIED NEW SDCU NO HELP. RE-INSTALLED ORIGINAL SDCU. REF TSM 26-16-0 0-810-819-A AND 26-17-00-810-803-A SDCU DOUBLE CHANNEL FAULT.

Source: SDR UALA2013010300019 · FAA SDRS
O · 2012-12-06 Unresolved
ATA 2520

ROW 11ABC THE SEATS ARE LOOSE. REPLACED LOCK RINGS & SECURED SEATS PER AMM. ACCOMPLISHED IDT INSPECTION PER GMM- 09-10-05 AND MM25-21-41.

Source: SDR UALA2012121007121 · FAA SDRS
J · 2012-11-28 Unresolved
ATA 2611

SMOKE DETECTOR MESSAGE ECAM. REPLACED SDCU PER MM, NO HELP. RESET, CHECK OK PER TASK 26-17-00-810-803A. MSG CLEARED.

Source: SDR UALA2012112906863 · FAA SDRS
O · 2012-09-10 Unresolved
ATA 7830

NR 1 ENGINE INBOARD REVERSER AT THE 0100 POS (LOOKING AFT) HAS A 4X6 PIECE OF PREVIOUS REPAIR DEGRADING AND STICKING UP INTO THE AIRSTREAM. REPLACED INBOARD REVERSER PER MM. OPS CHECK PER MM AND OPS CHECK OKAY.

Source: SDR UALA2012091305178 · FAA SDRS
O · 2012-09-03 Unresolved
ATA 5320

OVERHEAD PANEL ABOVE SEAT 2F IS LOOSE. AFT END OF PANEL IS SECURE WITH TAPE. PSU AND VIDEO MONITOR ARE NOT OBSTRUCTED, OK FOR SERVICE. REPLACED PANEL COVE LIGHT ASSEMBLY AT 2EF.

Source: SDR UALA2012090404973 · FAA SDRS
W · 2012-07-10 Unresolved
ATA 2560

DOOR 2R WILL NOT ARM. LUBED GIRT BAR FITTINGS AND ROLLERS ON DOOR FRAME. ARM DISARM FUNCTIONS OKAY.

Source: SDR UALA2012071203767 · FAA SDRS
O · 2012-06-30 Unresolved
ATA 2561

FIRST OBSERVER LIFE PRESERVER MISSING FROM FLT DECK. REPLACED LIFE VEST.

Source: SDR UALA2012070203531 · FAA SDRS
O · 2012-03-20 Unresolved
ATA 2510

CAPT SEAT SHOULDER HARNESS LOCK-UNLOCK LEVER MISSING. SAMC TEXT: REF IPC 25-11-51-01M: REPLACE SEAT ASSY. PCN 021-9017. REPLACED CAPTAIN'S SEAT PER MM, OPS CHECKS GOOD.

Source: SDR UALA2012032301855 · FAA SDRS
O · 2012-01-06 Unresolved
ATA 5610

RT SLIDING WINDOW REPLACEMENT. REPLACEMENT OF THE RT SLIDING WINDOW WAS ACCOMPLISHED PER TASK CARD 4S5686108.

Source: SDR UALA2012010900216 · FAA SDRS
J · 2011-11-26 Unresolved
ATA 2913

GREEN HYDRAULIC SYS OVERHEAT ILLUMINATED, FLIGHT DIVERTED. REPLACED OVERHEAT SWITCH 1381 GR, CHECKED CASE DRAIN FILTER NO DEFECTS. ACCOMPLISHED INTERNAL LEAK CHECK. NO DEFECTS. ACCOMPLISHED TSM 29-11- 00-810-802, ALL CHECKED GOOD. RAN ENGINE FOR 20 MINUTES NO OVERHEAT MESSAGE. REPLACED THE NR 1 ENGINE GREEN HYD PUMP 1030GK.

Source: SDR UALA2011112706457 · FAA SDRS
O · 2011-05-05 Unresolved
ATA 5210

DOOR 1R ASSIST BOTTLE PRESSURE LOW. SERVICED ASSIST BOTTLE.

Source: SDR UALA2011050502210 · FAA SDRS
O · 2010-09-12 Unresolved
ATA 3397

BACKSHELL FOR CONNECTOR ON EPSU 13WL, IS MISSING. ALSO STRAIN RELIEF IS CRACKED. REPLACED BACKSHELL-STRAIN RELIEF ON CONNECTOR 13WLA. EMERGENCY LIGHTS TEST PASSES.

Source: SDR UALA2010091303403 · FAA SDRS
L · 2010-09-12 Unresolved
ATA 3350

ON 3SV FAILED EMERGENCY LIGHT TEST BTSU INT LOAD AFT LT. REPLACED BATTERY FOR EPSU 13WL. EMER LIGHT TEST OK.

Source: SDR UALA2010091303404 · FAA SDRS
E · 2010-05-27 Unresolved
ATA 2910

ON FLT CONTROL CHECK L-R AILERON HAVE HYD NOISE-VIBRATION HEARD AND FELT IN COCKPIT. ISOLATED RT AILERON HYD SYSTEMS, RT AILERON FLUTTERS WITH ONLY GREEN HYD SYSTEM ON. ATTEMPTED ELAC 1 AND 2 RESET, NO HELP. SUSPECT RT GREEN AILERON SERVO ISSUE. THERE WERE NO AILERON FLUTTER ISSUES WTH BLUE HYD SYS SELECTED, ONLY GREEN SYS. REPLACED RT GREEN AILERON SERVO CONTROL UNIT, OPS CHECKED NORMAL.

Source: SDR UALA2010052801840 · FAA SDRS
O · 2010-01-26 Unresolved
ATA 5322

FRAME 73 STRINGER 31L & 32L SHEAR TIE DAMAGED. MAJOR REPAIR ACCOMPLISHED: REPLACED DAMAGED TIE.

Source: SDR UALA2010012700329 · FAA SDRS
O · 2010-01-26 Unresolved
ATA 5322

FRAME 74 STRINGER 32L & 33L CHECKED AND DAMAGED. FRAME 74, STRINGER 32L AND 33L SHEAR TIE IS CRACKED AND DAMAGED. MAJOR REPAIR ACCOMPLISHED: REPLACED DAMAGED TIE.

Source: SDR UALA2010012700327 · FAA SDRS
O · 2010-01-26 Unresolved
ATA 5322

FRAME 74 STRINGER 31L & 32L CRACKED AND DAMAGED. FRAME 74 STRINGER 31 LEFT AND 32 LEFT, SHEAR TIE CRACKED AND DAMAGED. MAJOR REPAIR ACCOMPLISHED: REPLACED DAMAGED TIE.

Source: SDR UALA2010012700328 · FAA SDRS
O · 2010-01-15 Unresolved
ATA 2565

DOOR 1R SLIDE FAILED TO DEPLOY. SLIDE STILL IN PLACE ON ACFT WITH DOOR CLOSED AND UNARMED. UNABLE TO RECORD MR NR AND DASH DUE TO POSITION OF SLIDE. REPLACED SLIDE PACK.

Source: SDR UALA2010011800204 · FAA SDRS
J · 2010-01-11 Unresolved
ATA 3233

RT MLG FAILED TO EXTEND. RAT DEPLOYED. VALVE FOUND FAULTY. REPLACED CUTOUT VALVE L-G FREE FALL 2515GM. OPS NORMAL.

Source: SDR UALA2010011100146 · FAA SDRS
O · 2008-09-11 Unresolved
ATA 5315

FLOORBEAM - Y765 HAS CORROSION FWD OF FR68. MAJOR REPAIR ACCOMPLISHED. BEAMS REMOVED AND BRACKETS TRANSFERRED (BEAM 95 AND 150) BEAMS NEED TO BE SPLICED TOGETHER AND INSTALLED. SPLICE INSTALLED AND BEAMS 95 AND 150 INSTALLED.

Source: SDR 2008UALA05668 · FAA SDRS
O · 2008-09-10 Unresolved
ATA 5711

STIFFENER IN NOSE WHEEL WELL LEFT SIDE IS CRACKED ON THE RISER. REPAIRED STIFFENER PER SRM 57-11-16.

Source: SDR 2008UALA05667 · FAA SDRS
O · 2008-09-09 Unresolved
ATA 5315

FLOORBEAM 145 HAS LOOSE RIVET(MARKED). MAJOR REPAIR ACCOMPLISHED. BEAM OUT AND ON BENCH WORKING. FOUND CORRODED BEAM REPLACED. ACP INSP OF BEAM 145.

Source: SDR 2008UALA05665 · FAA SDRS
O · 2008-09-09 Unresolved
ATA 5315

FLOORBEAM Y254 HAS CORROSION BETWEEN FR65 AND FR66 (MARKED). REPLACED BEAM 160. REPLACED FLOORBEAM 160.

Source: SDR 2008UALA05664 · FAA SDRS
O · 2008-09-09 Unresolved
ATA 5315

FLOORBEAM -Y1292 HAS CORROSION JUST AFT OF FR66. MAJOR REPAIR ACCOMPLISHED. REPLACED BEAM & SECURED WITH FASTENERS. ACP BEAM INSTALLATION FOR Y1292 FWD OF BEAM 140.

Source: SDR 2008UALA05663 · FAA SDRS
O · 2008-09-08 Unresolved
ATA 5320

THE 2R DOOR SILL CORRODED AT FWD SPLICE OUTBOARD SIDE, AT NUT CLIP HOLE. MAJOR REPAIR ACCOMPLISHED. STARTED TO REMOVE FASTENERS, INBOARD AND OUTBOARD ANGLES, NEW ANGLES FOR REPAIR IN WORK AREA. ACCOMPLISHED REPAIR PER MT 53-025. INSPECTED REPAIR.

Source: SDR 2008UALA05656 · FAA SDRS
O · 2008-09-08 Unresolved
ATA 5315

FLOORBEAM 190 HAS CORROSION AFT OF FR68 (MARKED). MAJOR REPAIR ACCOMPLISHED. STARTED REMOVING FASTENERS. BEAM REMOVED. STARTED INSTALLATION OF BEAMS 190 AND 195. SECURED NUT PLATES FOR FLOORBOARD. INSTALLATION IS COMPLETE.

Source: SDR 2008UALA05661 · FAA SDRS
O · 2008-09-08 Unresolved
ATA 5315

FLOORBEAM 195 HAS CORROSION ALONG LENGTH (MARKED). MAJOR REPAIR ACCOMPLISHED. STARTED REMOVING FASTENERS. REMOVED SEVERAL FASTENERS FROM BEAM 190 TO REMOVE BEAM 195. BEAM REMOVED. INSTALLED 8 NUT PLATES ON BEAM 195 FOR PNL 261FF. SECURED NUT PLATES FOR FLOORBOARD HOLES. INSTALLATION IS COMPLETE.

Source: SDR 2008UALA05659 · FAA SDRS
O · 2008-09-08 Unresolved
ATA 5322

AFT RT SHEAR TIE CORRODED BETWEEN FRAME 69 & 70. MAJOR REPAIR ACCOMPLISHED. FABRICATED NEW SHEAR TIE. INSTALLED SHEAR PLATE.

Source: SDR 2008UALA05662 · FAA SDRS
O · 2008-09-08 Unresolved
ATA 5315

FLOORBEAM 185 HAS CORROSION AT FR68 (MARKED). MAJOR REPAIR ACCOMPLISHED. REMOVED FLOORBEAM. BEAM OUT AND ON BENCH WORKING. STARTED INSTALLATION OF BRACKETS. RIVETING OF STANDOFF BRACKETS IS WHAT IS LEFT. DRILLED AND INSTALLED NEW BEAM 185. ALL BRACKETS RE-INSTALLED.

Source: SDR 2008UALA05658 · FAA SDRS
O · 2008-09-07 Unresolved
ATA 5315

FLOORBEAM 175 HAS CORROSION ALONG LENGTH BETWEEN FR68 AND FR70. MAJOR REPAIR ACCOMPLISHED. REMOVED FLOORBEAM. INSTALLED LAV AND GALLEY MOUNT FITTINGS TO NEW FLOORBEAM. DRILLED AND INSTALLED BEAM.

Source: SDR 2008UALA05657 · FAA SDRS
O · 2008-09-06 Unresolved
ATA 5315

FLOORBEAM 140 HAS CORROSION ON ENTIRE LENGTH. MAJOR REPAIR ACCOMPLISHED. BEAM OUT AND ON BENCH WORKING. FAB'D SPLICES FOR BEAMS FORE AND AFT PRIMED, SEALED & INSTALLED AFT END TO BEAM 145, FWD READY TO INSTALL. INSTALLED SPLICE TO BEAM 80. REPLACED BEAM AND COMPLETED WITH FASTENERS.

Source: SDR 2008UALA05660 · FAA SDRS
L · 2008-07-31 Unresolved
ATA 3350

CABIN EMERGENCY LIGHTS WILL NOT TEST.

Source: SDR 2008UALA04065 · FAA SDRS
W · 2008-06-17 Unresolved
ATA 3350

ON EMERGENCY LIGHT TEST, FAULT KEEPS COMING UP EPSU BATT AFT L.

Source: SDR 2008UALA03417 · FAA SDRS
W · 2008-06-03 Unresolved
ATA 2730

ELAC 2 FAULT INDICATIONS. SERVO 34CE1 FAILING CAUSING ELAC 2 TO FAULT CHRONICALLY. REPLACED LT INBOARD ELEVATOR SERVO CONTROL UNIT 34CE1, ADJUSTED AND OPS TESTED OK.

Source: SDR 2008UALA03191 · FAA SDRS
O · 2008-04-27 Unresolved
ATA 2565

DOOR 1L SIDE FELL OUT OF PACK. REPLACED SLIDE WITH SERVICEABLE UNIT.

Source: SDR 2008UALA02507 · FAA SDRS
O · 2008-04-26 Unresolved
ATA 2565

FOUND DOOR 1 LEFT DOOR BOTTLE LOW AND SHEAR PIN, SHEARED IN REF TO SLIDE PACK ON JET WAY. REPLACED DIAPHRAGM AND SHEAR PIN AND SERVICED BOTTLE PER MM. ALSO REPLACED WITH SERVICABLE SLIDE.

Source: SDR 2008UALA02457 · FAA SDRS
L · 2008-04-22 Unresolved
ATA 3350

EMERGENCY LIGHTS TEST FAILED. FOUND EPSU FAILED. REPLACED EPSU 13WL, TEST PASSES.

Source: SDR 2008UALA02375 · FAA SDRS
L · 2007-12-30 Unresolved
ATA 3350

EMERGENCY LIGHT SYSTEM FAIL TO TEST. EPSU FAILURE. REPLACED EPSU 13WL. OPS CHECKED NORMALLY.

Source: SDR 2007UALA05343 · FAA SDRS
L · 2007-09-22 Unresolved
ATA 3350

FWD EMERGENCY LIGHT POWER SUPPLY FAIL TEST PER 3 SVC.

Source: SDR 2007UALA03821 · FAA SDRS
O · 2007-09-15 Unresolved
ATA 5210

DOOR 2R EMERGENCY CYLINDER ACCUMULATOR PRESSURE LOW.

Source: SDR 2007UALA03715 · FAA SDRS
F · 2007-08-29 Unresolved
ATA 2730

ELAC 2 FAULT DISPLAYED ON UPPER ECAM SCREEN, - F-CTL. AIRCRAFT STARTED UNCOMMANDED FLIGHT MOVEMENT IN A DOWN PITCH BEFORE ECAM AND AFTER FAULT NO FURTHER UNCOMMANDED MOVEMENT. RESET ELAC2 AND PERFORMED GROUND SCAN- NO PROBLEMS NOTED, NO REPEATS SINCE ORIGINAL

Source: SDR 2007UALA03461 · FAA SDRS
K B · 2007-07-05 Unresolved
ATA 4990

CREW REPORT, 280 MILES FROM DESTINATION GOT BURNED AIR COND DUCT OR OVERHEAT ODOR FROM ROW 10 TO COCKPIT. APU OIL LEAKING INTO BLEED AIR SYSTEM. APU REMOVED AND REPLACED.

Source: SDR 2007UALA02418 · FAA SDRS
L · 2007-06-07 Unresolved
ATA 3350

CABIN EMERGENCY LIGHT TEST FAILED. EPSU 115 VAC EMER L.

Source: SDR 2007UALA01889 · FAA SDRS
J · 2007-04-21 Unresolved
ATA 3250

NW STEERING FAULT DISPLAYED ON UPPER ECAM SCREEN WHILE ENROUTE. NEEDED TOW TO GATE. ON SUBSEQUENT FLIGHT HAD LOW LEVEL GREEN HYD INDICATION. TOW TO GATE ALSO NEEDED. [06-22-07] FAULT TRACING FOUND A WANDERING SIGNAL VOLTAGE FROM 4GC NOSE WHEEL STEERING FEEDBACK SENSOR. REPLACED FAULTY FEEDBACK SENSOR AND REPLACED 6GC NOSE WHEEL STEERING SERVO AS A PRECAUTION.

Source: SDR 2007UALA01244 · FAA SDRS
L · 2006-07-06 Unresolved
ATA 3350

FOUND EMERGENCY LIGHTS FAILED. REPLACED BATTERY AT LEFT OVERWING EXIT TEST OK PER 33-51-00.

Source: SDR 2006UALA01349 · FAA SDRS
B · 2006-06-09 Unresolved
ATA 2497

DIVERTED FLIGHT DUE TO ELECTRICAL ODOR IN CABIN. FOUND SEAT ELECTRONICS BOX (SEB) AT SEAT 13 DEF BURNED UP ALONG WITH SEAT TO SEAT CABLE 13DEF TO 14 DEF.REPLACED CABLE AND SEB.ALSO FOUND SEB'S BAD AT 15DEF,16DEF,16ABC. PULLED 3 CB'S ON 2000VU PANEL FOR PES CENTER, RIGHT, & LEFT. COLLARED. PA WORKS FOR SAFETY VIDEO. IN REF TO LOG 1 FOUND SEB AT SEAT 13DEF BURNED UP. REPLACED SEB AT 13 DEF AND SEAT TO SEAT CABLE 13DEF TO 14DEF ALSO REPLACED WALL DISCONNECT BOX. OP CHKS OK.

Source: SDR 2006UALA01128 · FAA SDRS
N · 2006-05-04 Unresolved
ATA 5270

AFT CARGO DOOR LIGHT DISPLAYED ON CLIMB-OUT. CHECKED THAT NO BAGGAGE LOOSE IN COMPARTMNT. LGCIU STANDARD 4D INSTALLED. CHECKED AFT CARGO DOOR CLOSED AND ALL LOCKS ENGAGED. FOUND AFT CARGO DOOR CONNECTOR LOOSE, SECURED AND OPTS NORMAL.

Source: SDR 2006UALA00884 · FAA SDRS
L · 2006-03-12 Unresolved
ATA 3350

AFTER REPLACING BATTERY IN REAR EPSU, PTP TEST DISPLAYS *EPSU AFT L*. REPLACED POWER SUPPLY. TESTED THROUGH PTP AND GOT GREEN OK LIGHT AND TEST OK MESSAGE.

Source: SDR 2006UALA00475 · FAA SDRS
L · 2005-11-28 Unresolved
ATA 3350

EMERGENCY LIGHT TEST FAULTS LEFT FWD BATTERY. REPLACED BATTERY.

Source: SDR 2005UALA01376 · FAA SDRS
O · 2003-09-09 Unresolved
ATA 5311

AFT PIT FRAME 54L DAMAGED AT STR 38L. MAJOR REPAIR ACCOMPLISHED. INSTALLED DOUBLER REPAIR.

Source: SDR 2003UALA00675 · FAA SDRS
O · 2002-06-11 Unresolved
ATA 5210

DOOR 2R DOOR ASSIST BOTTLE PRESSURE OVER LIMIT AT 2100 PSI. FOUND SCHRADER SERVICE VALVE BAD. REPLACED VALVE AND SEAL. SERVICED AND CHECKED OK.

Source: SDR 2002UALA00986 · FAA SDRS
J · 2001-09-03 Unresolved
ATA 2910

LANDED UNDER AMBER ALERT DUE TO LOSS OF YELLOW HYDRAULIC SYSTEM.

Source: SDR 2001UALA01934 · FAA SDRS
O · 2001-06-29 Unresolved
ATA 3350

OVERHEAD EMERGENCY LIGHTS REMAIN ON. REPLACED RT OVERWING POWER SUPPLY.

Source: SDR 2001UALA01255 · FAA SDRS
O · 1999-08-05 Unresolved
ATA 5610

CRACKED RIGHT WINDSHIELD. *S/D* CAUSE OF CRACKED RIGHT WINDSHIELD WAS FOD AS THERE WAS NUMEROUS HITS ALONG LOWER EDGE.

Source: SDR 99UAL900412 · FAA SDRS
J · 1999-02-26 Unresolved
ATA 2211

AUTOPILOT DISENGAGED ON APPROACH ALONG WITH THE MAP NOT AVAIL FLAG ON THE CAPTAIN SIDE NAV DISPLAY. PFR SHOWS FAILURE MESSAGES FMGC2 AND FAC2. *S/D* THE POSTFLIGHT REPORT IDENTIFIED THE FLIGHT MANAGEMENT AND GUIDANCE COMPUTER (FMGC) NR 2 AND FLIGHT AUGMENTATION COMPUTER (FAC) NR 2 AS THE POSSIBLE FAULTS. THE FMGC 1 AND 2 WERE RERACKED AND SWAPPED BETWEEN POSITIONS. NO FURTHER FAILURES HAVE OCCURED. THIS MAY BE RELATED TO THE SOFTWARE ANOMALIES IDENTIFIED BY SEXTANT, AIRBUS AND AD 97-21-10. AIRBUS HAS BEEN NOTIFIED OF THIS EVENT. ADDITIONALLY COA 403350/1 HAS BEEN GENERATED TO TERMINATE AD 97-21-10.

Source: SDR 99UAL900131 · FAA SDRS
W · 1999-01-08 Unresolved
ATA 5220

OVERWING EMERGENCY EXIT DOOR AIR LEAK. SEATS 9BC AND 10ABC NOT TO BE OCCUPIED DURING FLIGHT UNTIL REPAIRS ARE COMPLETE. FOUND DOOR INSTALLED INCORRECTLY WITH SEAL STUCK IN THE GAP BETWEEN THE DOOR AND FUSELAGE. DOOR WAS REINSTALLED CORRECTLY.

Source: SDR 99UAL900020 · FAA SDRS