N818LX

RAYTHEON AIRCRAFT COMPANY HAWKER 800XP · 2001 · Valid Registration

Registered owner: N818LX LLC, DE (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
M & N EQUIPMENT, LLC (MY5A)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2023-12-27 Matched by certificate designator
ATA 2131

ON CLIMB OUT FROM DENVER, CENTENNIAL, (KAPA), THE AIRPLANE WOULD NOT PRESSURIZE. THE CREW ELECTED TO RETURN TO THE POINT OF DEPARTURE. MAINTENANCE WAS SUMMONED. IT WAS DETERMINED THAT THE PRESSURIZATION CONTROLLER HAD FAILED. AN OVERHAULED PRESSURIZATION CONTROLLER WAS INSTALLED AND WAS OPERATIONALLY TESTED ON THE GROUND. AN EVALUATION FLIGHT WAS DONE, AND THE PRESSURIZATION SYSTEM WAS FOUND TO OPERATE SATISFACTORY. AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 2024F00000 · FAA SDRS
J · 2022-06-10 Matched by certificate designator
ATA 2913

#2 (RIGHT) HYDRAULIC PUMP FAILURE.

Source: SDR 2022F00254 · FAA SDRS
J · 2019-04-07 Matched by certificate designator
ATA 2160

CREW WAS AT CRUISE FLIGHT AND HEARD AS THUMPING SOUND IN THE BACK OF THE AIRCRAFT AND THE CABIN BEGAN TO CLIMB UNCONTROLLED. THEY DECLARED AN EMERGENCY AND DESCENDED AND DIVERTED. CREW ALSO REPORTED THAT THE AUTOTEMP SYSTEM WAS NOT WORKING AND THE DUCT TEMP WAS CLOSE TO ZERO AND THE AIRCRAFT WAS COLD. AFTER DESCENT TO LOWER ALTITUDE AND WARMER AIR THE PRESSURIZATION SYSTEM BEGAN TO WORK. THE TEMP CONTROL VALVE WAS DETERMINED TO BE STUCK IN THE FULL COLD POSITION CAUSING THE WATER SEPARATOR TO FREEZE CAUSING THE LOSS OF PRESSURIZATION AIR.

Source: SDR MFGA2019041058444 · FAA SDRS
B · 2009-01-25 Matched by certificate designator
ATA 2120

ON DESCENT, CREW NOTED A HOT ELECTRICAL BURNING ODOR IN THE COCKPIT. NO SMOKE WAS SEEN AND ACFT LANDED SAFELY. MX PERFORMED A THOROUGH INSP OF THE ACFT SYS BUT WAS UNABLE TO DUPLICATE THE DISCREPANCY.

Source: SDR DJFA2009005 · FAA SDRS