N854EC

EUROCOPTER DEUTSCHLAND GMBH MBB-BK 117 C-2 · 2010 · Valid Registration

Registered owner: PITT COUNTY MEMORIAL HOSPITAL INC, NC (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
METRO AVIATION, INC (HDNA)Certificate holderMatched by certificate designator
AIR METHODS LLC (QMLA)Operator2010-12-29 – 2010-12-29Operator named in NTSB report

Accident & incident history

Acc · 2010-12-29 Operator named in NTSB report
EUROCOPTER MBB-BK None injury Part 135AIR METHODS LLC
Source: NTSB case ERA11LA106

Maintenance disclosures

Y · 2022-08-07 Matched by certificate designator
ATA 7600

PILOT'S STATEMENT - WAS AT CRUISE FLIGHT AT 2000 MSL ON LEG BETWEEN ECU NORTH HOSPITAL AND ECU MEDICAL CENTER WHEN OVSP FAIL (#2) CAUTION ILLUMINATED AND THEN EXTINGUISHED ON ITS OWN FOLLOWING ACKNOWLEDGEMENT. AUTOPILOT WAS COUPLED AND THERE WERE NO SECONDARY INDICATIONS. OVER NEXT MINUTE OR SO OVSP FAIL CAUTION RETURNED AND THEN EXTINGUISHED ON ITS OWN SEVERAL MORE TIMES. REFERRED TO CHECKLIST WHICH DIRECTED LAND AS SOON AS PRACTICABLE AND INFORMED CREW WE WOULD BE GOING DIRECTLY TO ECU LOWER PAD FOR MAINTENANCE ACTION. AFTER APPROXIMATELY 3 MINUTES FOLLOWING THE INITIAL CAUTION, THE #2 ENGINE OVSP FAIL ILLUMINATED STEADY ON CAD AND SHUT ITSELF DOWN (THIS STATEMENT WAS BY THE SUBMITTER). I MADE 180 TURN TOWARDS NEAREST AIRPORT (KIXA), SECURED THE AFFECTED ENGINE, AND CONDUCTED A RUN-ON LANDING ON WITHOUT FURTHER INCIDENT. AFTER ACTION FINDINGS BY THE MAINTENANCE STAFF - INSPECTION OF THE #2 ENGINE REVEALED THAT THE #2 ENGINE OVERSPEED SENSOR CONTACTED THE POWER TURBINE PHONIC WHEELS DUE TO INTERNAL SWELLING (BULGING) OF THE SENSOR BODY FROM POTENTIAL OIL INTRUSION. THE CONTACT WITH THE PHONIC WHEELS AND THE OVERSPEED SENSOR RENDERED THE HOMOPOLAR GENERATORS (2 EA) LOCATED IN THE SENSOR INOPERATIVE RESULTING IN THE LOSS OF SIGNAL TO THE TACHOMETER. THIS LOSS OF THESE SIGNALS CAUSED THE AUTOMATIC SHUTDOWN OF THE #2 ENGINE BY THE TACHOMETER BOX THROUGH THE ACTIVATION OF THE OVERSPEED/DRAIN VALVE.

Source: SDR HDNA20220812001 · FAA SDRS
B · 2022-07-25 Matched by certificate designator
ATA 2120

PILOT'S STATEMENT - SHORTLY AFTER DEPARTING FROM A SCENE WITH PATIENT ON BOARD, MEDICAL CREW ANNOUNCED THERE WAS AN ACRID SMELL IN AFT CABIN. COCKPIT INDICATIONS WERE NORMAL (NO ELECTRICAL ISSUES PRESENT AND ALL CIRCUIT BREAKERS IN). AFTER APPROXIMATELY 120 SECONDS ACRID SMELL WAS ALSO NOTICEABLE IN THE COCKPIT AND MED CREW STATED THAT THEY WERE UNCOMFORTABLE CONTINUING THE FLIGHT. I IMMEDIATELY EXECUTED A PRECAUTIONARY LANDING TO THE CLOSEST SUITABLE AREA. LANDING WAS ACCOMPLISHED WITHOUT INCIDENT. CORRECTIVE ACTION TAKEN - MAINTENANCE TECHNICIAN PERFORMED A THOROUGH INSPECTION OF ALL AIRCRAFT AND MEDICAL ELECTRICAL EQUIPMENT, FOLLOWED BY 20 MINUTE GROUND RUN WITH NO SMELL NOTICED, FOLLOWED BY OPERATIONAL CHECK FLIGHT WITH NOT UNUSUAL ODORS NOTED.

Source: SDR HDNA20220725001 · FAA SDRS
O · 2016-03-17 Matched by certificate designator
ATA 5302

FOUND A CRACK ON TAIL BOOM RING FRAME X9227.

Source: SDR HDNA2016F00083 · FAA SDRS
B · 2013-01-10 Matched by certificate designator
ATA 2121

CREW AND PILOT SMELLED ELECTRICAL BURNING ODOR DURING FLIGHT. NORMAL LANDING COMPLETED WITHOUT INCIDENT, AND WITHOUT ANY FURTHER EMERGENCY ACTION TAKEN. MX INSPECTED ACFT, FOUND COCKPIT VENTILATION FAN SHORTING.

Source: SDR QMLA2013011013004 · FAA SDRS
K B · 2011-10-18 Matched by certificate designator
ATA 2810

THE MEDICAL CREW REPORTED TO THE PILOT THAT THEY SMELLED FUEL IN THE CABIN SHORTLY AFTER TAKEOFF. THE PILOT IMMEDIATELY RETURNED TO THE HELIPAD. THE MECHANIC PERFORMED AN INPSECTION OF THE FUEL SYS AND FOUND THAT THE LOWER FITTING OF THE EXPANSION TANK WAS LEAKING. THE ACFT IS CURRENTLY OOS AWAITING THE ARRIVAL OF A REPLACEMENT EXPANSION TANK. THIS PARTICULAR TANK WAS REPLACED IN THIS ACFT JUST AFTER IT INITIALLY ARRIVED FROM THE MFG WITH VERY LITTLE TIME.

Source: SDR QMLA2011101811102 · FAA SDRS
B · 2011-07-21 Matched by certificate designator
ATA 2120

THE PILOT AND CREW REPORTED A ODOR OF FUEL IN THE CABIN ON TAKEOFF. THE PILOT LANDED AT THE NEAREST AIRPORT TO INSPECT THE FUEL CAP AND ACFT FOR ANY NOTICEABLE SIGNS OF FUEL LEAKS, ETC. NO DEFECTS WERE NOTED. THE MECHANIC INSPECTED THE ACFT TO INCLUDE THE ENGINES, ENGINE COMPARTMENTS, CABIN AREA TO INCLUDE CHECKING FOR LEAKS AROUND THE EXPANSION TANK, AND UNDERNEATH THE ACFT FOR POSSIBLE BOOST PUMP OR FUEL SUMP LEAKS. NO DEFECTS NOTED. THE ACFT WAS THEN GROUND RUN WITH NO DEFECTS NOTED. THE ACFT WAS THEN RETURN TO SERVICE.

Source: SDR QMLA2011072111081 · FAA SDRS