N855MB

AMERICAN EUROCOPTER CORP AS350B3 · 2013 · Valid Registration

Registered owner: MED-TRANS CORP, TX (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
MED-TRANS CORPORATION (M3XA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2025-06-16 Matched by certificate designator
ATA 2913

PILOT PERFORMED A PRECAUTIONARY LANDING FOR #2 HYDRAULICS FAILED IN FLIGHT. MECHANIC DISCOVERED THE HYDRAULIC PUMP BELT HAD SHEARED. DURING REMOVAL IT WAS DISCOVERED THE HYDRAULIC PUMP BEARING FAILED AND CAUSED THE BELT TO SHEAR. MECHANIC REMOVED AND REPLACED THE HYDRAULIC PUMP PULLEY AND BEARING ASSY AND REPLACED THE HYDRAULIC PUMP BELT. BIS.

Source: SDR M3XA202506165003 · FAA SDRS
W B · 2020-01-18 Matched by certificate designator
ATA 3600

PILOT MADE A PL BACK TO HOSPITAL PAD WITH A PATIENT ON BOARD AND REPORTED AFTER 2 MINUTES INTO THE FLIGHT WITH CABIN HEAT APPLIED, CABIN BAGAN TO FILL WITH SMOKE ON THE CEILING. MECHANIC TROUBLESHOT AND FOUND EXCESS INLET BARRIER FILTER FLUID IN THE ENGINE INTAKE PLENUM FROM RECENT FILTER SERVICEING. CLEANED EXCESS FLUID AND PERFORMED ENGINE RUNUP WITH HEATER APPLIED AND NO FURTHER DEFECTS.

Source: SDR M3XA2020011801 · FAA SDRS
K · 2016-04-08 Matched by certificate designator
ATA 7320

5.7 HOURS AFTER COMPLETING AN ENGINE INSPECTION, WHICH INCLUDED CHANGING THE HMU FILTER AND PACKINGS, THE PILOT UPON HIS POST FLIGHT WALK AROUND NOTICED FUEL ON THE UNDERSIDE OF THE FUSELAGE. TO ASSIST IN TROUBLESHOOTING THE PROBLEM, THE PILOT THEN PROCEEDED TO TURN ON THE AIRFRAME BOOST PUMP. THE FUEL WAS FOUND TO BE LEAKING FROM THE ENGINE OVERBOARD DRAIN. THE MECHANIC WAS ADVISED OF THE PROBLEM. AFTER TROUBLESHOOTING THE SYS IT WAS DISCOVERED THAT THE HMU FUEL FILTER PACKING HAD BEEN CUT DURING THE LAST INSPECTION 5.7 HRS PREVIOUSLY. MECHANIC CHANGED THE PACKINGS AND TEST RAN THE ACFT NUMEROUS TIMES, WITH NO DEFECTS NOTED. PAPERWORK WAS COMPLETED AND THE ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR 7AJA2016FA0000169 · FAA SDRS
K · 2016-04-07 Matched by certificate designator
ATA 7321

FUEL WAS DISCOVERED DRAINING OUT OF THE ENG OVERBOARD DRAIN SYS. FOUND THE FUEL CONTROL, HYDRO MECHANICAL UNIT, PUMP FILTER INTERNAL PACKING CUT.

Source: SDR 7AJA20160415002 · FAA SDRS
K · 2016-04-07 Matched by certificate designator
ATA 7320

AFTER SHUTDOWN, THE PILOT WAS COMPLETING HIS WALK AROUND & NOTICED FUEL DRIPPING FROM THE ENG OVERBOARD DRAIN TUBE. HE ALSO NOTICED THAT THE FUEL LEAKED ONTO THE BELLY & WAS DRIPPING THERE ALSO. AFTER THE MECHANIC ARRIVED, THEY TURNED ON THE ACFT BOOST PUMP & FUEL WOULD START DRIPPING FROM THE OVERBOARD DRAIN. CONTACTING THE TECHNICAL REPRESENTATIVE, WE WERE TASK WITH CHECKING THE HMU FILTER PACKING, AS THIS IS ONE OF THE EASIEST TASKS TO PERFORM. UPON INSPECTING THE FUEL FILTER PACKING IT WAS DETERMINED TO BE CUT & WAS REPLACED. THE ACFT WAS TEST RAN 3 TIMES WITH NO FUEL LEAK PRESENT. THE PAPERWORK WAS COMPLETED & THE ACFT WAS APPROVED FOR RETURN TO SERVICE. THIS PACKING HAD BEEN REPLACED JUST A FEW HOURS EARLIER AS THE ENG WENT THROUGH AN 800 HOUR INSPECTION. THE PACKING MUST HAVE GOT CUT AT THAT TIME.

Source: SDR 7AJA20160407001 · FAA SDRS