N9448B

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
GRANT AVIATION INC (ENHA)Operator2019-07-08 – 2019-07-08Operator named in NTSB report

Accident & incident history

Acc · 2019-07-08 Operator named in NTSB report
Cessna 208 Minor injury Part 135GRANT AVIATION INC
Source: NTSB case ANC19LA031
Accident · 1995-03-02 Unresolved
Cessna 208B Minor injuryoperator not yet resolved
Source: NTSB case FTW95FA129

Maintenance disclosures

J · 2010-04-01 Unresolved
ATA 7260

EN ROUTE FROM OMA TO DSM WHEN THE FORWARD ENGINE CHIP DETECTOR LIGHT CAME ON. LANDED IN DSM NO PROBLEMS. MAINTENANCE FOUND SMALL SLIVER OF METAL ON CHIP DETECTOR. CLEANED DETECTOR, CHECKED OIL FILTER COMPLIED WITH OIL SAMPLE ANALYSIS, RAN ENGINE FOR TEN MINUTES ON GROUND OPS CHECKS GOOD.

Source: SDR BSYA2010021 · FAA SDRS
G B · 2007-12-23 Unresolved
ATA 2460

EN ROUTE FROM SDF TO MDW PILOT HAD TO DIVERT TO DPA BECAUSE OF HIGH WINDS. UPON ARRIVING INTO DPA LOST ALL AVIONICS, THEN STARTED TO SMELL SOMETHING BURNING. AFTER LANDING NEITHER AVIONICS BUSS NR 1 OR BUSS NR 2 WOULD RESET, AND THE ELECTRICAL SMELL WAS COMING FROM P10 PIN (L). REMOVED AND REPLACED CIRCUIT BREAKER AND BURNT PIN IN THE CONNECTOR EVERYTHING OPS CHECKS GOOD.

Source: SDR BSYA200700012 · FAA SDRS
B · 2007-12-23 Unresolved
ATA 2450

EN ROUTE FROM SDF TO MDW AIRCRAFT DIVERTED TO DPA BECAUSE OF HIGH WINDS. UPON ARRIVING AT DPA, LOST ALL AVIONICS. TRIED TO RESET NR 1 & NR 2 CIRCUIT BREAKERS, NO HELP THEN STARTED TO SMELL SMOKE. FOUND NR 1 BUSS CIRCUIT BREAKER BAD AND P10 CONNECTOR HAD A BAD PIN (BURNT). REMOVED AND REPLACED SWITCH AND PIN OPS CHECKS GOOD.

Source: SDR BSYA200700017 · FAA SDRS