N984ME

EUROCOPTER DEUTSCHLAND GMBH MBB-BK 117 C-2 · Valid Registration

Registered owner: AIR METHODS LLC, CO (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AIR METHODS LLC (QMLA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2026-01-27 Matched by certificate designator
ATA 7714

NUMBER 2 ENGINE OVSP FAIL DID NOT EXTINGUISH.

Source: SDR QMLA2026012720006 · FAA SDRS
E · 2025-03-27 Matched by certificate designator
ATA 6200

MRB VIBE ABSORBERS LEAKING.

Source: SDR QMLA2025032820043 · FAA SDRS
O · 2021-04-15 Matched by certificate designator
ATA 5330

DAMAGE TO THE LH STA5025 FRAME INNER SKIN PANEL (PN: B533K5606-211) IN THE FORM OF 2EA CRACKS ON THE UPPER END OF THE PART AND A CHAFE ON THE LOWER END OF THE PART. THE CRACKS WERE MEASURED TO BE APPROXIMATELY 0.19” AND 0.20” IN LENGTH EMANATING FROM A FASTENER HOLE. THE CHAFE WAS MEASURED TO BE APPROXIMATELY 0.66” X 0.55” AND 0.010” DEEP. THIS DAMAGE HAS BEEN REPAIRED AND DOCUMENTED ON FAA FORM 337 DATED 06/05/2021.

Source: SDR QMLA2021041520032 · FAA SDRS
O · 2021-04-15 Matched by certificate designator
ATA 5320

DAMAGE WAS REPORTED ON THE RWL1505 INTERCOSTAL (PN: B533K5396-204) IN THE FORM OF CHAFES. THE CHAFES WERE MEASURED TO BE APPROXIMATELY 0.007” AND 0.010” DEEP. THIS DAMAGE HAS BEEN REPAIRED AND DOCUMENTED ON FAA FORM 337 DATED 06/05/2021.

Source: SDR QMLA2021041520031 · FAA SDRS
O · 2021-04-15 Matched by certificate designator
ATA 5313

S/N 9080 BK117 C-2/EC145 WAS FOUND TO HAVE CHAFE DAMAGE IN THE TAIL CONE OMEGA STRINGER AT STA6541. THIS DAMAGE HAS BEEN REPAIRED AND DOCUMENTED ON FAA FORM 337 DATED 06/05/2021.

Source: SDR QMLA2021062320033 · FAA SDRS
O · 2021-04-15 Matched by certificate designator
ATA 5311

DAMAGE WAS REPORTED ON THE STA5375 CANT FRAME UPPER DOUBLER (PN: B533K3517-201) IN THE FORM OF A CHAFE MEASURING APPROXIMATELY 0.50” X 0.10” AND 0.050” DEEP. THIS DAMAGE HAS SINCE BEEN REPAIRED AND DOCUMENTED ON FAA FORM 337 DATED 06/05/2021.

Source: SDR QMLA2021041520030 · FAA SDRS
O · 2021-04-15 Matched by certificate designator
ATA 5312

BK117-C2 S/N 9080 WAS FOUND TO HAVE CHAFE DAMAGE TO THE UPPER BULKHEAD ANGLE P/N L533K3138-201 AT STA 4963, RBL 40, WL 2625. THE DAMAGE MEASURES 0.01” DEEP, AND 0.25” X 0.25” IN AREA.

Source: SDR QMLA2021041520029 · FAA SDRS
B H · 2018-09-18 Matched by certificate designator
ATA 3310

MEDCREW REPORTED SMOKE IN THE CABIN AREA, PILOT NOTICED CIRCUIT BREAKER WAS POPPED, DESCENDED AND MADE AN UNSCHEDUALED LANDING. CALLED MECHANIC.

Source: SDR QMLA2018091918103 · FAA SDRS
E · 2008-04-23 Matched by certificate designator
ATA 2150

AIR CONDITIONING DRIVE PULLEY BOLTS SHEARED AND THE PULLEY DETACHED FROM THE DRIVE. IT LOOKS LIKE THE BOLTS LOST TORQUE SLIGHTLY, BOLT HEADS WERE SAFETIED, THE THE PULLEY WORKED THE THE BOLTS UNTIL THEY SHEARED. I HAVE OPERATED 8500 HOURS ON 5 DIFFERENT EC-145S WITH THIS PULLY SYSTEM WITHOUT ANY PROBLEMS. I HAVE CHECKED MY OTHER 5 EC-145 HELICOPTERS FOR AIR-CONDITIONG PULLY ATTACHMENT AND THEY ARE ALL PERFECT. THIS SEEMS TO BE AN ISOLATED INCIDENT. --- AFTER FURTHER INVESTIGATION OF THE ATTACHING BOLTS, THE BOLT SHANKS THAT WERE STILL IN THE PULLEY WERE TIGHT HOWEVER FRETTING WAS FOUND ON THE PULLEY ATTACHING SURFACE. IT IS QUITE POSSIBLE THAT THE INSTALLER OF THIS STC (HELI-DYNE)INSTALLED THE WRONG LENGTH BOLTS.

Source: SDR N984ME9080 · FAA SDRS
B · 2007-08-27 Matched by certificate designator
ATA 2110

THE AIR-CONDITIONING COMPRESSOR SEIZED, THE DRIVE BELT CONTINUED TURNING, SMOKING UNTIL IT BROKE.

Source: SDR 984ME · FAA SDRS