N98904

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
PRO AIRE CARGO & CONSULTING, INC. (W1XA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

E J · 2019-11-12 Matched by certificate designator
ATA 3220

PILOT PLACED GEAR HANDLE IN THE DOWN POSITION, LOUD BANG, ALL 3 GEAR DOWN LIGHTS ILLUMINATED AND PILOT LANDED WITHOUT ISSUE. AFTER SHUT DOWN NOTICED LINKAGE HANGING FROM NOSE WHEEL WELL. THE NOSE GEAR TORQUE TUBE ADJUST INBD P/N 0842104-3 HAD FAILED AND THE FORK BOLT P/N 5243518-2 WAS SLIGHTLY BENT.

Source: SDR 2020FA0000015 · FAA SDRS
R · 2016-12-08 Matched by certificate designator
ATA 7414

RIGHT ENGINE STARTED RUNNING A BIT ROUGH. VISUALLY INSPECTED MAGNETOS AND REMOVED RIGHT MAGNETO FOR INSPECTION. DISCOVERED WORN DISTRIBUTOR GEAR. REPLACED MAGNETO WITH OVERHAULED UNIT OF SAME TYPE.

Source: SDR 20171212006 · FAA SDRS
O · 1999-09-16 Unresolved
ATA 3230

WHEN PILOT SELECTED GEAR DOWN, HEARD LOUD NOISE IN NOSE, HAD 3 GREEN LIGHTS AND NO HORN, LANDED WITHOUT INCIDENT. FOUND NOSE GEAR INBOARD BELLCRANK BROKEN AND BOLT BENT. GEAR WAS RIGGED TO SPECS 2 MONTHS PRIOR. SUSPECT GEAR MOTOR BRAKE INOPERABLE AND GEAR WENT PAST UPLIMIT SWITCH AND JAMMED IN UP POSITION. UPLOCK HOOK AND BOLT ALSO BENT.

Source: SDR 99ZZZX3915 · FAA SDRS
O · 1998-07-07 Unresolved
ATA 8520

ENGINE REMOVED FROM SERVICE DUE TO METAL CONTAMINATION DUE TO PREMATURE FAILURE OF TAPPET BODIES.

Source: SDR 98ZZZX2647 · FAA SDRS
O · 1998-07-07 Unresolved
ATA 8520

ENGINE REMOVED FROM SERVICE DUE TO METAL CONTAMINATION, DUE TO PREMATURE FAILURE OF TAPPET BODIES.

Source: SDR 99ZZZX625 · FAA SDRS
O · 1998-07-07 Unresolved
ATA 8520

ENGINE REMOVED FROM SERVICE DUE TO METAL CONTAMINATION DUE TO PREMATURE FAILURE OF TAPPET BODIES.

Source: SDR 98ZZZX2648 · FAA SDRS
O · 1998-07-07 Unresolved
ATA 8520

ENGINE REMOVED FROM SERVICE DUE TO METAL CONTAMINATION, DUE TO PREMATURE FAILURE OF TAPPET BODIES.

Source: SDR 99ZZZX626 · FAA SDRS
O · 1998-01-23 Unresolved
ATA 2720

AFTER STARTING ENGINES TO REPOSITION AIRCRAFT, PILOT PUSHED ON LEFT RUDDER PEDAL AND PEDAL BROKE OFF AT BASE WHERE IT IS WELDED TO PEDAL ARM ASSY. AIRCRAFT TOTAL TIME 5,980 HOURS. PART MAY HAVE BEEN ORIGINAL. ANNUAL INSPECTION, 6 MONTHS PRIOR. HAVE HEARD OF SAME PROBLEM WITH SIMILAR AIRCRAFT. SUBMITTER SUGGESTED MORE FREQUENT AND CLOSER INSPECTIONS.

Source: SDR 98ZZZX512 · FAA SDRS