SPECTRUM HEALTH HOSPITALS

Part 135 operator · designator BTEA

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: AERO MED SPECTRUM HEALTH, SPECTRUM HEALTH HOSPITALS, Spectrum Health Hospitals

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

16 reports on file.

N · 2020-04-14 Matched by certificate designator
N176BA · ATA 2612

DURING PILOT TRAINING WHILE ON AN APPROACH TO LAND, THE #1 ENGINE FIRE WARNING SYSTEM INDICATED A FIRE (LIGHTS AND AURAL) FOR 3-4 SECONDS AND THEN THE INDICATIONS WENT AWAY. APPROXIMATELY 5 SECONDS LATER, THE FIRE INDICATIONS CAME BACK ON. THOUGH THERE WEREN'T SECONDARY INDICATIONS OF A FIRE, SINCE THEY WERE ALREADY ON AN APPROACH, THE PILOTS DECIDED TO PULL THE #1 ENGINE OFFLINE AND CONTINUE THEIR APPROACH AND PERFORM A SINGLE ENGINE LANDING. DURING THIS PROCESS, THE FIRE INDICATIONS WENT AWAY AGAIN AND THEN CAME BACK ON FOR THE 3RD TIME. AFTER THE ENGINE WAS PULLED OFFLINE, THE FIRE INDICATIONS WENT AWAY FOR GOOD. UPON LANDING, A VISUAL CONFIRMATION WAS MADE THAT THERE WASN'T A FIRE. MAINTENANCE DID A TEST OF THE TWO FLAME DETECTORS IN THE FIRE WARNING SYSTEM. THE DETECTORS CHECKED OUT AS GOOD. A DECISION WAS MADE TO CHANGE OUT BOTH DETECTORS. AFTER REPLACEMENT OF THE DETECTORS, THE TWO SUSPECT DETECTORS WERE TESTED AGAIN “OFF WING” AND THE DETECTOR THAT WAS IN THE AFT/LOWER POSITION IN THE SYSTEM FAILED. THIS PROBABLY EXPLAINS THE INTERMITTENT NATURE OF THE FIRE SYSTEM INDICATING A FIRE THEN INDICATING THAT THERE WASN’T A FIRE. THE AIRCRAFT HAS FLOWN 3.8 HOURS SINCE THE REPLACEMENT OF THE FLAME DETECTORS WITHOUT FURTHER ISSUES.

Source: SDR BTEA2020041600000 · FAA SDRS
H J · 2013-11-29 Matched by certificate designator
N176AM · ATA 2435

NR 1 STARTER/GENERATOR FAILED. DURING START, THE ENGINE TOOK AN UNUSUALLY LONG TIME TO REACH LIGHT OFF AND IDLE SPEED. AFTER ENGINE START, THE GENERATOR WOULD NOT COME ON LINE. AFTER THE ACFT RETURNED TO THE MAINTENANCE FACILITY, THE STARTER WAS EXAMINED AND THE INTERNAL DAMAGE WAS FOUND TO THE BRUSHES, BRUSH HOLDER CLIPS, ETC. THE STARTER/GENERATOR WAS REPLACED. ALL SYSTEMS CHECKED GOOD.

Source: SDR BTEA2014F00047 · FAA SDRS
H J · 2013-06-25 Matched by certificate designator
N176AM · ATA 2435

NR 2 DC GENERATOR FAILED IN FLIGHT. AFTER THE ACFT RETURNED TO THE MX FACILITY, THE STARTER GENERATOR WAS REMOVED FOR INSPECTION. THE BRUSHES WERE FOUND WORN EXCESSIVELY AND BROKEN. REPLACED WITH AN O/H UNIT, ALL SYS CHECKED GOOD.

Source: SDR BTEA201306250001 · FAA SDRS
J · 2013-05-11 Matched by certificate designator
N176BA · ATA 3410

PILOT SIDE EFIS DISPLAY WENT BLACK WITH A RED X ACROSS BOTH DISPLAYS. FAULT FOUND WAS THE MOUNTING RACK LOCKING SCREWS WERE OUT OF ADJUSTMENT, ALLOWING THE SYMBOL GENERATOR TO BE LOOSE IN THE RACK AND THE PINS TO GET COATED WITH A DUST, THUS LOOSING CONTACT. CLEANED BOTH THE PINS IN THE SYMBOL GENERATOR AND THE RACK. READJUSTED THE LOCING SYSTEM. REMOUNTED THE SYMBOL GENERATOR. ALL SYSTEMS TESTED GOOD.

Source: SDR BTEA201306020001 · FAA SDRS
K · 2012-12-20 Matched by certificate designator
N176BA · ATA 2810

LEFT FUEL TANK WAS SEEPING FUEL, IT WAS NOTICED WHILE SETTING IN THE HANGAR. DEFUELED AIRCRAFT, RESEALED FASTENER AT AFT SEAM OF TANK, STA 215.

Source: SDR BTEA20121220001 · FAA SDRS
M · 2012-11-29 Matched by certificate designator
N176AM · ATA 7321

THE FUEL CONTROL FAILED ON START CAUSING THE ENGINE TO EXCEED TEMPERATURE LIMITS. THE HMU WAS FOUND TO BE AT FAULT. (SUSPECT THE CONSTANT DELTA "P" VALVE FAILED). THE ENGINE ASSEMBLY AND HMU WERE REPLACED. THIS FAILURE COULD HAVE OCCURRED IN FLIGHT CAUSING AN IN FLIGHT SHUT DOWN OF THE ENGINE.

Source: SDR BTEA20121130001 · FAA SDRS
J · 2012-08-10 Matched by certificate designator
N176BA · ATA 2435

WHEN THE AIR CONDITIONER WAS TURNED ON, THERE WAS A "POPPING" SOUND IN THE INTERCOMM SYSTEM IN CREW HELMETS. THIS WAS ACCOMPANIED BY AN "AUX BATTERY" LIGHT. INSPECTION OF NR 2 STARTER GEN SHOWED SIGNIFCANT WEAR OF BRUSHES AND AN UNUSUAL WEAR PATTERN ON THE COMMUTATOR. STARTER GEN WAS REPLACED. NOISE WENT AWAY. THERE WAS A SECONDARY DEFECT WITH THE CURRENT LIMITER FOR THE SYSTEM. THAT UNIT WAS REPLACED AND ALL FUNCTIONS RETURNED TO NORMAL.

Source: SDR BTEA2012FA0000554 · FAA SDRS
E J · 2012-08-08 Matched by certificate designator
N176AM · ATA 7200

INTEGRATED INFORMATION DISPLAY SYSTEM, (IIDS), DISPLAYED A "MINOR" ENGINE FAULT "TQ TRIM LVL L" FOR THE NR 1 ENGINE FROM THE DIGITAL ENGINE CONTROL UNIT (DECU). PILOTS CHECK FOR FAULTS FROM THE DECU AND THE IIDS. A MINOR FAULT WAS NOTED ON THE NR 1 ENG; "TQ. TRIM, LVL 1". FAULT OCCURRED ON THREE SEPARATE FLIGHTS IN AN INTERMITTENT FASHION. ON ALL THREE OCCURRENCES, ACFT DIVERTED AND RETURNED TO MX FACILITY. FIRST OCCURRENCE, TROUBLESHOOTING TOOK PLACE USING BOTH ENGINE AND ACFT MM. THE FAULT CLEARED ITSELF AND NO DEFINITIVE ACTION WAS TAKEN. SECOND OCCURRENCE, TROUBLESHOOTING AGAIN SHOWED NO DEFINED DEFECTS. TORQUE CONFIRMATION BOX WAS REPLACED. THIRD OCCURRENCE, "MINOR" FAULT ADDITIONAL TROUBLESHOOTING DETECTED EXCESSIVE VIBRATION OF THE NR 1 ENGINE. THE ENGINE WAS R & R WITH A 0.0 TSO, ENGINE ASSEMBLY.

Source: SDR BTEA2012F00158 · FAA SDRS
O · 2008-05-07 Matched by certificate designator
N176BA · ATA 5320

DURING INSP, TECH FOUND CRACKED TEE ANGLE P/N 76201-23014-138 AFT SECTION. REMOVED TEE ANGLE FOUND THE ENTIRE ANGLE CRACKED AND THE FWD BATHTUB FITTING P/N 76209-03002-119 CRACKED AT THE MOUNT BOLT HOLE. THE FOLLOWING PARTS WERE REPLACED IAW SRM SA 4047-76-12: TEE FITTING P/N 76201-23014-138 LT FWD BATHTUB FITTING P/N 76209-03002-119 LT AFT BATHTUB FITTING P/N 76209-03002-125.

Source: SDR EGRR119590 · FAA SDRS
O · 2008-04-14 Matched by certificate designator
N176BA · ATA 5330

DURING PRELIMINARY INSP FOUND 6.5 INCH CRACK ON LT SIDE SKIN PANEL AT AC STA 254, WATERLINE 107. THE LT SIDE SKIN PANEL WILL BE REPLACED WITH SERVICEABLE ONE.

Source: SDR EGRR119440 · FAA SDRS
N · 2006-05-08 Matched by certificate designator
N176BA · ATA 2612

ENROUTE, WHEN NR 1 ENG FIRE WARNING SYS WAS ACTIVATED. PILOT REPORTED WARNING LIGHTS, HORN AND T-HANDLES ILLUMINATED WITH FIRE WARNING INDICATION. WARNING STAYED ON FOR 30 SECONDS, WENT OUT. AFTER SHORT PERIORD OF TIME, WARNING CAME BACK. PILOT DECLARED EMERGENCY WITH GRR CONTROLLERS. WARNING WENT OUT AND CAME BACK ON 2 ADDITIONAL TIMES. ENG PWR WAS REDUCED TO IDLE,THEN WAS SECURED USING FIRE T-HANDLE. WHEN AC WAS IN SIGHT, IT WAS REPORTED, NO VISIBLE SMOKE TRAILING AC. PILOT CONTINUED, MADE EMERGENCY LANDING W/O INCIDENT. ENG WAS OPENED AND INSPECTED FOR ANY VISIBLE SIGNS OF DAMAGE. NO FIRE INDICATIONS. TROUBLESHOOTING RESULTED FROM DEFECTIVE FIRE WARNING SENSOR, REPLACED. AC RETURNED TO SERVICE.

Source: SDR 2006FA0000540 · FAA SDRS
B J · 2006-05-07 Matched by certificate designator
N176BA · ATA 8300

ENROUTE TO A PICK UP A PATIENT. WITHIN 4 MINUTES OF TAKEOFF, MEDICAL CREW REPORTED, SMELLED SMOKE IN CABIN, BECOMING VISIBLE ALSO. PILOT NOTICED IT ABOUT SAME TIME. PILOT RETURNED WITHOUT DELAY, APPROX 30 SECONDS BEFORE TOUCHDOWN, BAGGAGE COMPARTMENT SMOKE DETECTOR WENT OFF. AC LANDED WITHOUT INCIDENT. INVESTIGATION SHOWED NR 2 ENG ACCY GEARBOX VENT TUBE HAD BROKEN FREE OF ENG DECK FITTING. THIS OVERBOARD BREATHER TUBE MADE OF A VINYL MATERIAL, HAD DETERIORATED TO POINT OF BREAKING OFF OF FITTING ON BOTTOM OF ENG DECK. TUBE RUNS THROUGH AFT CORNER OF BAGGAGE COMPT, WHEN TUBE BROKE, FILLED COMPT WITH OIL MIST/VAPOR THAT ILLUMINATED SMOKE DETECTOR. VINYL TUBE WAS REPLACED, AC RETURNED TO SERVICE. (K)

Source: SDR 2006FA0000539 · FAA SDRS
O · 2002-12-26 Matched by certificate designator
N176BA · ATA 5600

PILOTS WINDSHIELD CRACKED IN FLIGHT WITH THE WINDSHIELD HEAT "ON". WHEN THE CRACK OCCURED, THERE WERE SPARKS COMING FROM THAT AREA. ALSO, THERE WERE TWO AREAS APPROXIMATELY 3 INCH IN LENGTH THAT HAD MELTED PLASTIC EXTRUDED OUT OF THE CRACK. THE INNER LAYER OF GLASS SHOWED NO SIGNS OF DAMAGE.

Source: SDR 12262002 · FAA SDRS
K J · 2000-09-08 Matched by certificate designator
N176BA · ATA 2910

NR 2 HYDRAULIC PRESSURE LINE FROM HYDRAULIC PUMP TO BULKHEAD FITTING FAILED ON AIRCRAFT START-UP. LINE BURST FROM INSIDE WITHOUT WARNING, (NO LEAKS NOTED ON PREFLIGHTS). LINE WAS REPLACED, SYSTEM SERVICED AND AIRCRAFT RETURNED TO SERVICE. (X)

Source: SDR BTEAS76B001 · FAA SDRS
O · 1995-05-14 Matched by certificate designator
N176RA · ATA 7933

REMOVED GAUGE FOR NEEDLE RAPID FLUCTUATION - 20-50 DEGREES, SPIKING WILDLY OCCASIONALLY.

Source: SDR 96ZZZX1413 · FAA SDRS
L · 1995-01-17 Matched by certificate designator
N801BA · ATA 7321

FCU FAILED MAXIMUM NG CHECK BY MINIMUM OF .8 PERCENT. MINIMUM CHECK OF 101.8 PERCENT MINUS NG EQUALS 101.0 PERCENT. REMOVED FCU FOR REPAIR.

Source: SDR 96ZZZX562 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N176AMSIKORSKY S-76C2007Valid RegistrationMatched by certificate designator
N176BASIKORSKY S-76B1985Valid RegistrationMatched by certificate designator
N610TARAYTHEON AIRCRAFT COMPANY B2001998Valid RegistrationMatched by certificate designator
N764AMKEYSTONE HELICOPTER CORP S-76C2009Valid RegistrationMatched by certificate designator