AIR 1ST AVIATION COMPANIES OF OKLAHOMA INC

Part 135 operator · designator OXKA

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: AIR 1ST AVIATION COMPANIES OF OKLAHOMA INC

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

4 reports on file.

J · 2010-01-15 Matched by certificate designator
N211BE · ATA 7321

RT ENGINE FUEL CONTROL MALFUNCTION. NO POWER LEVER RESPONSE ON THE RT ENGINE. COULD NOT REDUCE BELOW 900 DEG C. DIVERTED. ON APPROACH , SHUTDOWN ENGINE AND LANDED WITH NO FURTHER PROBLEMS.

Source: SDR OXKA856K · FAA SDRS
O · 2006-12-04 Matched by certificate designator
N777LP · ATA 3210

DURING GEAR EXTENSION FOR LANDING, A LOUD BANG WAS NOTICED BY THE PIVOT AND UNSAFE LIGHT STAYED ON. AIRCRAFT WAS ROUTED TO MAINTENANCE AFTER LANDING. MAINTENANCE FOUND ROD END ART -7E ON SHAFT HAD COME APART ANDALLOWED DOORS TO BECOME DISCONNECTED FROM ACTUATOR. (SW15200706339) (K)

Source: SDR 2007FA0000100 · FAA SDRS
E Y · 2006-04-26 Matched by certificate designator
N777LP · ATA 7210

PILOT REPORTED DURING CRUISE LEVEL FLIGHT FEELING A SUDDEN VIBRATION AND HEARING A SCREAMING NOISE FROM THE LT ENGINE. PILOT THEN NOTICED TORQUE INDICATION ON LT ENGINE INDICATING 120 PERCENT WITH NO YAW INDICATED OR NOTICED BY PILOT. WHILE RETARDING LT POWER LEVER TO REDUCE TORQUE THE LT ENGINE SHUTDOWN UNCOMMANDED. ENGINE NTS SYSTEM FUNCTIONED NORMALLY AND AN UNEVENTFUL SINGLE ENGINE LANDING WAS MADE. UPON ENGINE ASSEMBLY A 2 INCH PIECE OF THE BULL GEAR OUTER RIM WAS LAYING IN THE BOTTOM OF THE ACCESSORY HOUSING. INSPECTION OF THE BULL GEAR REVEALED THE MISSING SECTION AND AN APPROX 4 INCH CRACK IN THE HUB AREA WHICH CAUSED LOSS OF DRIVE TO THE PROPELLER SHAFT.

Source: SDR 2006FA0000476 · FAA SDRS
Y · 2006-02-15 Matched by certificate designator
N640MA · ATA 7712

ENGINE, SN P20186, EXPERIENCED AN UN-COMMANDED INFLIGHT SHUTDOWN, ON SITE INSPECTION REVEALED THAT THE FUEL PUMP DRIVE TRAIN HAD BECOME UNCOUPLED. TEARDOWN INSPECTION REVEALED FAILURE OF SPUR GEARSHAFT PN 8968042, COMPONENT OF TORQUE SENSOR PN 31017262, SN P2648 WITH 3369.8 TSO. THIS ARICRAFT IS IN COMPLIANCE OF ALL APPLICABLE AD. (K)

Source: SDR OXK2006F00000 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N175CAMITSUBISHI MU-2B-601979Valid RegistrationMatched by certificate designator
N741FNMITSUBISHI MU-2B-361975Valid RegistrationMatched by certificate designator
N777LPMITSUBISHI MU-2B-36AValid RegistrationMatched by certificate designator