AITHERAS AVIATION GROUP LLC

Part 135 operator · designator K45A

Data confidence: Records are linked by certificate number, aircraft registration, or a name match that a reviewer has confirmed. Each record below shows how it was linked.

Also recorded as: AITHERAS AVIATION GROUP LLC, Aitheras Aviation Group, Aitheras Aviation Group, LLC

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

Acc · 2024-12-11 Operator named in NTSB report
CESSNA 560 (N981AG) None injury Part 91

Operated by Aitheras Aviation group, LLC (per NTSB report)

Source: NTSB case ERA25LA073
Acc · 2008-01-16 Operator named in NTSB report
Hawker Beechcraft Corp. 58 (N3217L) Fatal injury Part 91

Operated by Aitheras Aviation Group (per NTSB report)

Source: NTSB case CHI08FA066

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

16 reports on file.

O · 2012-12-11 Matched by certificate designator
N680EV · ATA 2720

DURING SCHEDULED INSPECTION, THE RUDDER TORQUE TUBE WAS FOUND CRACKED APPROXIMATELY 90% OF DIAMETER. CAUSE IS BELIEVED TO BE WIND DAMAGE DUE TO CONTROL LOCKS NOT ENGAGED WHEN PARKED. RUDDER WAS REMOVED AND SENT TO CESSNA FOR REPAIR.

Source: SDR K45A121412 · FAA SDRS
C · 2012-06-29 Matched by certificate designator
N980AG · ATA 7230

ENGINE WAS INSPECTED TO CHECK OUT BASE MX (FOD INSPECTION). ABRADABLE MATERIAL WAS FOUND MISSNG FROM LOW COMPRESSOR CASE FTO 9 O`CLOCK THROUGH OUT 10:30 O`CLOCK POSITION. BELIEVE THE MATERIAL WAS LOOSENED BY THE BIRD STIKE BUT NOT EASILY DETECTED. THE MATERIAL THEN DEPARTED FROM ENGINE ON RETURN FLIGHT TO BASE. NO ADDITIONAL DAMAGE OR PROBLEMS WERE ENCOUNTERED. THE MATERIAL WAS REPLACED IAW MM.

Source: SDR K45A2012070201 · FAA SDRS
O · 2012-06-29 Matched by certificate designator
N980AG · ATA 5730

ACFT WAS INSPECTED TO CHECK OUT BASE MX (FOD INSPECTION). A 3" BY 5" DENT .125" DEEP WAS DISCOVERED 2 FT INBD OF STALL STRIP UNDER THE DEICE BOOT. DAMAGE WILL BE REPAIRED IAW EA RECOMMENDATIONS.

Source: SDR K45A2012070202 · FAA SDRS
O · 2012-05-15 Matched by certificate designator
N691ES · ATA 3233

RIGHT MAIN LANDING GEAR FAILED TO RETRACT. PILOT'S SELECTED DOWN AND RECEIVED A SAFE INDICATION. AIRCRAFT LANDED WITHOUT INCIDENT. AIRCRAFT WAS PLACED ON JACKS AND TROUBLESHOOTING REVEALED ACTUATOR WAS LEAKING INTERNALLY. ACTUATOR WAS REPLACED IAW C560MM CH32-31-04. RETRACTION TEST SATISFACTORY.

Source: SDR K45A2012051700002 · FAA SDRS
J · 2012-05-03 Matched by certificate designator
N691E · ATA 3230

UPON DEPARTURE CREW REPORTED LANDING GEAR RETRACTED FOLLOWED BY RIGHT MAIN GEAR EXTENDING TO DOWN AND LOCKED POSITION. INDICATION WAS A RED INTRANSIT AND RIGHT GEAR DOWN (GREEN) LIGHTS ILLUMINATED. CREW EXTENDED LANDING GEAR AND RECEIVED THREE GEAR DOWN (GREEN) LIGHTS. CREW RETURNED AND LANDED AT DEPARTURE AIRPORT UNEVENTFULLY. AIRCRAFT WAS PLACED ON JACKS AND RETRACTION TESTED SEVERAL TIMES BUT COULD NOT DUPLICATE PROBLEM. LANDING GEAR UPLOCK HOOK AND ROLLER WAS CLEANED AND LUBRICATED. SEVERAL ADDITIONAL GEAR RETRACTIONS WERE CONDUCTED WITH NO DEFECTS NOTED. AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR K45A20120509001 · FAA SDRS
N · 2012-03-21 Matched by certificate designator
N981AG · ATA 3260

LEFT MAIN GEAR DOWN LIGHT FAILED TO ILLUMINATE WHEN LANDING GEAR WAS EXTENDED. CREW RECYCLED GEAR WITH SAME RESULT. THEN EXTENDED THE LANDING GEAR USING THE EMERGENCY SYSTEM. THE LANDING WAS UNEVENTFUL. INVESTIGATION REVEALED THE INDICATOR LAMP HAD FAILED. LANDING SYSTEM WAS RESET AND RETRACTION TEST WAS SATISFACTORY. AIRCRAFT RETURNED TO SERVICE.

Source: SDR K45A20120321001 · FAA SDRS
N · 2012-01-05 Matched by certificate designator
N981AG · ATA 3260

ON TAKEOFF, LANDING GEAR WOULD NOT FULLY RETRACT AS INDICATED BY "IN TRANSIT" AND "HYD ON" LIGHT STAYED ON. ACFT ALSO EXPERIENCED BUFFETING. FLIGHT CREW RECYCLED LANDING GEAR WITH SAME RESULT THEN EXTENDED LANDING GEAR NORMALLY. ACFT RETURNED WITH A NORMAL LANDING. ACFT WAS FERRIED TO A REPAIR FACILITY WITH LANDING GEAR EXTENDED. TROUBLESHOOTING REVEALED A STICKY NOSE GEAR UPLOCK AND SWITCH. UNITS WERE CLEANED AND LUBRICATED. OPS TEST OF LANDING GEAR RETRACTION WAS SATISFACTORY. ACFT WAS RETURNED TO SERVICE.

Source: SDR K45A2012F00002 · FAA SDRS
O · 2012-01-03 Matched by certificate designator
N691ES · ATA 5330

ACFT WAS PARKED, POSITIONED WITH STRONG TAILWIND COMPONENT. WHEN CREW OPENED CABIN DOOR PILOT LOST GRIP ON HANDLE AND WIND SLAMMED DOOR OPEN, BREAKING THE HINGE AND DAMAGED THE FUSELAGE SIDE AT FS 171.80. REPAIR IS BEING COMPLETED IAW REPORT S-500-ATA53-07RD.

Source: SDR K452012F00000 · FAA SDRS
O · 2011-04-20 Matched by certificate designator
N503BG · ATA 5610

DURING PHASE 49 INSPECTION, CRACKS AT HOLES NR 5 AND 6 WERE FOUND IN COPILOT'S OUTER SIDE WINDOW. THESE EXCEED ALLOWABLE LIMITS IAW THE MFG. WINDOW WILL BE REPLACED IAW MM.

Source: SDR K45A042011 · FAA SDRS
O · 2011-04-15 Matched by certificate designator
N503BG · ATA 5310

DURING PHASE 49 INSP EDDY CURRENT INP INDICATED A POSSIBLE CRACK. PAINT AND FILLER WERE REMOVED AND AREA INSPECTED BY VISUAL INSP USING MAGNIFICATION WHICH CONFIRMED 3 CRACKS IN BAND AT FS 287.78. IT APPEARS BAND WAS DAMAGED DURING LAST REPAINT OF ACFT, CAUSING STRESS RISERS AND SUBSEQUENT CRACKING.

Source: SDR 2011F00092 · FAA SDRS
O · 2011-03-02 Matched by certificate designator
N82DT · ATA 5755

DURING ROUTINE MX, THE RT LOWER SPEED BRAKE LOWER STIFFENER WAS FOUND CRACKED AT MID SPAN. THE COMPONENT WAS REPLACED IAW THE SRM. CAUSE UNKNOWN.

Source: SDR K452011F00000 · FAA SDRS
O · 2011-03-02 Matched by certificate designator
N82DT · ATA 5755

DURING ROUTINE MX, THE LT LOWER SPEED BRAKE LOWER STIFFENER WAS FOUND CRACKED AT MID SPAN. THE COMPONENT WAS REPLACED IAW THE SRM. CAUSE UNKNOWN.

Source: SDR K452011F00001 · FAA SDRS
O · 2010-08-31 Matched by certificate designator
N727EF · ATA 3240

ON LANDING, PILOT REPORTED BRAKING ACTION WAS NORMAL. UPON SECOND APPLICATION OF BRAKES TO ENTER A TAXIWAY, LOST ALL BRAKING ACTION. ACFT WAS STOPPED WITHOUT INCIDENT, USING EMERGENCY PNUEMATIC SYS. MX BLED BRAKES AND TROUBLESHOT SYS TO A LOOSE FITTING DRIVE CLIP IN RT HUBCAP. CLIP WAS ADJUSTED AND OPS TEST WAS STATISFACTORY. ACFT TAXI TEST WAS SATISFACTORY.

Source: SDR K452010F00000 · FAA SDRS
K · 2009-02-05 Matched by certificate designator
N103BG · ATA 7310

MECHANIC EXPERIENCED A SLOW/COLD START ON LT ENGINE. ENGINE IDLED SLOWER THAN NORMAL. ALL OTHER PARAMETERS WERE NORMAL. UPON SHUTDOWN, FLUID (FUEL) WAS PUDDLED IN BYPASS DUCT AND DRIPPING FROM AFT ENGINE CORE. INVESTIGATION REVEALED PRIMARY AND SECONDARY CROSS MANIFOLD AREA WAS LEAKING. FUEL MANIFOLD WAS REMOVED FOR FURTHER INSPECTION. (K)

Source: SDR K452009F00000 · FAA SDRS
O · 2007-10-26 Matched by certificate designator
N103BG · ATA 7830

DURING ROUTINE INSPECTION, THE LT OB THRUST REVERSER STANG FOUND DISPLACED .2500 INCH OB FROM NORMAL POSITION. REMOVAL OF STANG REVEALED THE LOWER FWD SUPPORT WAS MISSING THE UPPER FWD SUPPORT SHEARED OFF. THE ATTACHING RIVETS HAD FAILED. FURTHER INSPECTION REVEALED THE UPPER AFT MOUNTING LUG OF OB (BIRDCAGE) WAS CRACKED DUE TO STRESSES IMPOSED DUE TO MISSING FWD SUPPORT. THRUST REVERSER WAS REMOVED AND SENT TO MFG FOR REPAIR. AS PREVENTIVE MEASURE, THE RT OB THRUST REVERSER STANG WAS REMOVED AND THE LOWER FWD SUPPORT WAS FOUND LOOSE WITH ONE SHEARED ATTACHING RIVET. THE UNIT WAS REMOVED FOR REPAIR. CAUSE MAY HAVE BEEN ACCUMULATED AGE AND VIBRATION. (K)

Source: SDR K452007F00001 · FAA SDRS
O · 2007-06-01 Matched by certificate designator
N103BG · ATA 2750

FLAPS WOULD NOT EXTEND DURING APPROACH. AN UNEVENTFUL (NO FLAP)LANDING WAS ACCOMPLISHED. INSPECTION REVEALED THE FLAP FOLLOWUP CABLE (AFT) HAD BROKEN WHERE IT PASSES OVER 1 PULLEY FORMING AN (S) ROUTING. THIS IS A HIGH WEAR AREA AND COMMON PROBLEM ON THIS MODEL AC. THE CABLE WAS REPLACED. (K)

Source: SDR K452007F00000 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N164RACESSNA 5602007Valid RegistrationMatched by certificate designator
N3217LOperator named in NTSB report
N35BGMIKOYAN GUREVICH MIG 15UTI1954Valid RegistrationMatched by certificate designator
N525GJDJI AGRAS T100Valid RegistrationMatched by certificate designator
N600TBCESSNA 550Valid RegistrationMatched by certificate designator
N680AGCESSNA 6802007Valid RegistrationMatched by certificate designator
N690ESCESSNA 5601995Valid RegistrationMatched by certificate designator
N691ESCESSNA 5601997Valid RegistrationMatched by certificate designator
N981AGCESSNA 5601998Valid RegistrationOperator named in NTSB report
N981AGCESSNA 5601998Valid RegistrationMatched by certificate designator
N985AGCESSNA 560XL2001Valid RegistrationMatched by certificate designator