Aeroflight Academy of Aviation, Inc.

Part 135 operator · designator TVDA

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: Aeroflight Academy of Aviation, Inc.

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

4 reports on file.

O · 2010-03-26 Matched by certificate designator
N167WA · ATA 7421

ON THE 2ND LEG OF A FLIGHT, THE PILOT EXPERIENCED AN OCCASIONAL MISFIRE THAT BECAME MORE REGULAR ADJUSTING MIXTURES AND CHECKING MAGNETOS. FAILE TO ISOLATE PROBLEM SO THE DECISION WAS MADE TO DIVERT WHERE AN UNEVENTFUL LANDING WAS MADE. MX WAS DISPATCHED FOR REPAIRS. THEY CONDUCTED A GROUND RUN AND COULD NOT DUPLICATE MISFIRE. FUEL FLOWS, MANIFOLD PRESSURES AND MAGNETO TIMING AND CYLINDER COMPRESSIONS WERE NORMAL. FURTHER TROUBLESHOOTING REVEALED A COUPLE OF SPARK PLUGS THAT APPEARED WEAK. NEW SPARK PLUGS WERE INSTALLED. GROUND RUNS WERE PERFORMED AND ACFT WAS DETERMINED AIRWORTHY. SUBSUQUENT NON-REVENUE FLIGHT WAS NORMAL. NO FURTHER MX ACTION WAS REQUIRED.

Source: SDR TVD2010F00000 · FAA SDRS
O · 2006-10-30 Matched by certificate designator
N81070 · ATA 2913

LANDING GEAR FAILED TO FULLY RETRACT. FOUND ELECTRIC MOTOR ON HYDRAULIC POWERPACK FAILED. REPLACED POWER PACK AND LANDING GEAR FUNCTIONED PROPERLY. (K)

Source: SDR TVD2006F00001 · FAA SDRS
O · 2006-03-30 Matched by certificate designator
N4549Q · ATA 8530

NR 3 CYLINDER ON THE LT ENGINE CRACKED COMPLETELY AROUND THE HEAD, APPROX 1.25 INCHES ABOVE THE BASE OF THE HEAD. THE CRACK WAS COMPLETELY AROUND THE CIRCUMFERANCE OF THE HEAD AND ALLOWED THE HEAD TO SLIP OFF OF THE BARREL, HALF AN INCH. THE PROP WAS FEATHERED, ENGINE SHUTDOWN AND A SAFE LANDING WAS MADE. NO OTHER DAMAGE TO THE ENGINE OR AIRCRAFT. CYLINDER WAS ON ITS 3RD RUN, HAD BEEN PREVIOUSLY REBARRELED AND BORED .010 OVERSIZED AT THE LAST OVERHAUL. (K)

Source: SDR TVD2006F00000 · FAA SDRS
N · 2005-02-15 Matched by certificate designator
N156SB · ATA 3417

WHILE FLYING AT 170 KIAS, THE PILOT NOTED HE HAD TO REDUCE POWER TO MAINTAIN 170 KIAS. SHORTLY AFTER THAT THE AIRCRAFT`S (STICK SHAKER) ACTIVATED. INSPECTION REVEALED SEVERELY DETERIORATED PLASTIC TUBING FROM FWD PRESSURE BULKHEAD TO AIR DATA COMPUTER. LINES WERE REPLACED. (K)

Source: SDR TVD2005F00000 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N98186CESSNA 172PValid RegistrationMatched by certificate designator