RELIANT AIR CHARTER, INC.

Part 135 operator · designator QREA

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: RELIANT AIR CHARTER, INC., Reliant Air Charter, Inc.

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

7 reports on file.

J · 2021-09-23 Matched by certificate designator
N525EZ · ATA 2421

LEFT AC ALTERNATOR BEARING FAIL-CAS MESSAGE SAID PRIMARY BEARING FAIL THIS ITEM WAS RECEIVED FROM OVERHAUL WITH OVERHEATING EVIDENCE STILL APPARENT VIA THE BROWN TINT ON THE PAINT ON THE CASE DIRECTLY FROM CESSNA. SOMEONE NEEDS TO CONTACT PACIFIC SCIENTIFIC AS THIS BEARING FAILURE IS ONGOING. TOO MANY FAILURES

Source: SDR 2021F00216 · FAA SDRS
X P · 2021-03-30 Matched by certificate designator
N379R · ATA 7320

WHILE JUST BEGINNING A DECENT FROM FL450 THE THROTTLE WAS REDUCED SLOWLY AND TOGETHER ON BOTH ENGINES, THE RIGHT ENGINE ROLLED BACK TO FLAME-OUT. ENGINE WAS RE-STARTED SUCCESSFULLY AT FL220 AND REMAINED RUNNING AND OPERATING NORMALLY THE REST OF THE FLIGHT TO LANDING AT KHPN WHITE PLAINS, NY. FADEC DATA WAS DOWNLOADED AND SENT TO WILLIAMS BY WAYNE TOHER OF RELIANT AIR. WILLIAMS CONCLUDED THE FUEL DELIVERY UNIT FAILED. FDU WAS REPLACED BY TEXTRON/CESSNA IN WHITE PLAINS AND WELL AS THE OTHER ENGINE (LH) FDU BY DEMAND FROM RELIANT.

Source: SDR QREA202104140001 · FAA SDRS
O · 2018-05-24 Matched by certificate designator
N904MC · ATA 2910

PILOT SELECTED GEAR DOWN WITH THE GEAR HANDLE, BUT THE GEAR DID NOT COME DOWN, AND AFTER 15 SECONDS OR SO, THE 2 AMP GEAR CONTROL BREAKER TRIPPED. A SUCCESSFUL GEAR EXTENSION WAS PERFORMED USING THE MANUAL HAND PUMP SYSTEM. JACKED AIRCRAFT AND SUCCESSFULLY RETRACTED THE GEAR, BUT GEAR WOULD NOT EXTEND WHEN SELECTED, BUT THE HYDRAULIC POWER-PACK WOULD RUN, BUT WOULD NOT BUILD PRESSURE TO EXTEND THE GEAR. PROBLEM WAS TROUBLESHOT TO BE A FAULTY GEAR CONTROL SOLENOID, WHICH IS ATTACHED TO THE SIDE OF THE POWER-PACK. ECONOMICS DICTATED REPLACING THE ENTIRE HYDRAULIC POWER-PACK. SUCCESSFUL GEAR OPERATION WAS OBSERVED AFTER REPLACEMENT.

Source: SDR 2018FA0000172 · FAA SDRS
J · 2013-11-07 Matched by certificate designator
N717HA · ATA 3231

HYDRAULIC ON AND GEAR UNLOCK LIGHT CAME ON DURING DECENT, FOLLOWED BY A THUMPING NOISE FROM THE LT GEAR. GEAR EXTENDED NORMALLY WITH 3 GREEN. LANDED AND CALL DOM. DOM ASKED THE PILOT TO LOOK AT THE UPLOCK HOOK ON THE LT GEAR. SHOWED UPLOCK HOOK CRACKED. FERRY PERMIT REQUESTED AFTER AN INSPECTION WAS CONDUCTED. LANDING GEAR CONTROL CB COLLARED AND ACFT FERRIED TO SERVICE CENTER. HOOK AND POSITION SWITCH WERE REPLACED AND ACFT RETURNED TO SERVICE. RT UPLOCK HOOK WAS INSPECTED, NO DEFECTS FOUND.

Source: SDR QREA2013111200001 · FAA SDRS
B · 2012-06-04 Matched by certificate designator
N8111M · ATA 2140

AFTER TAKEOFF THE PILOT TURNED ON HEATER AND CABIN STARTED TO FILL WITH SMOKE. SHUT HEATER OFF AND SMOKE CLEARED. BACK AT MX BASE, TURNED ON ONLY CABIN BLOWER AND NOTED NO ODOR OR SMOKE. ON LIGHTING HEATER, STARTED TO SMELL HEAVY ELECTRICAL ODOR AND COMBUSTION BLOWER SOUNDED MUCH NOISIER THAN NORMAL. REMOVED COMBUSTION BLOWER AND DISASSEMBLED. FOUND THE END HOUSING (FAN END) THAT SECURES BEARING WAS SEVERELY ELONGATED WHICH ALLOWED ROTOR TO MOVE & CONTACT PERMANENT MAGNETS.

Source: SDR QREA2012F00109 · FAA SDRS
O · 2008-07-10 Matched by certificate designator
N425WD · ATA 7603

THE PILOT MENTIONED UPON LENDING THE LT ENGINE NG DID NOT GO ALL THE WAY BACK TO IDLE SPEED, BUT STAYED AT 80 PERCENT. UPON EXAMINATION OF THE FUEL CONTROL LINKAGE, IT WAS NOTED THAT THE FUEL CONTROL ARM WAS NOT RESTING ON THE IDLE STOP, BUT WAS UP ABOUT 1 INCH. USING LIGHT HAND PRESSURE THE LINKAGE WAS PUSHED TO THE STOP. THE FUEL CONTROL ARM AFT ROD END WAS FOUND TO BE BOUND AND CAUSING THE PROBLEM. INSPECTION OF THE ROD END DISCLOSED NO OBVIOUS DEFECTS. REPLACED ROD END WITH A NEW UNIT AND OPS SHOW NORMAL. (K)

Source: SDR QRE2008F00000 · FAA SDRS
O · 2003-12-19 Matched by certificate designator
N904MC · ATA 5730

LEFT IB LEADING EDGE WING PANEL WAS REMOVED TO REPLACE THE DE-ICE BOOT AND IT WAS DISCOVERED THAT SUBSTANTIAL DEBONDING OF THE LOWER HALF OF THIS PANEL HAD OCCURRED. THERE WAS NO APPARENT DAMAGE TO THE OUTSIDE SKIN THAT WOULD EXPLAIN THIS AND ITS UNLIKELY THAT THE LINE PERSONNEL FUELING THE AUX TANK CAUSED THIS DUE TO THE DEBONDING ISOLATED TO THE LOWER SKIN. TECH SUPPORT REQUIRES REPLACING THIS SKIN WITH A NEW UNIT.

Source: SDR 2004F00054 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N379RCESSNA 525A2008Valid RegistrationMatched by certificate designator
N525EZCESSNA 525C2012Valid RegistrationMatched by certificate designator
N525RECESSNA AIRCRAFT CO 525B2011Valid RegistrationMatched by certificate designator
N904MCBEECH B3001991Valid RegistrationMatched by certificate designator
N969LDMatched by certificate designator
N971TBCESSNA 525B2010Valid RegistrationMatched by certificate designator