FLORIDA JET SERVICE INC

Part 135 operator · designator FJ7A

Data confidence: All records on this page are linked by a shared certificate number or aircraft registration (N-number).

Also recorded as: FLORIDA JET SERVICE INC

Accident & enforcement record

Events that happened, regardless of the operator's own reporting. Each links to its public source.

NTSB accidents & incidents

No NTSB accidents or incidents linked to this operator.

FAA enforcement actions

FAA enforcement records haven't been loaded into GroundCheck yet, so none can be shown — a gap in our data, not evidence of a clean enforcement history.

Maintenance disclosure history

Service Difficulty Reports are self-reported maintenance findings. The NUMBER of reports is not a measure of reliability — diligent operators file more, not fewer. These are shown for transparency, not as a negative signal.

10 reports on file.

J · 2026-04-12 Matched by certificate designator
N171AM · ATA 2740

ON APRIL 12, 2025, WHILE AIRCRAFT N171AM WAS TAXIING FROM THE RAMP AT FORT LAUDERDALE EXECUTIVE AIRPORT (FXE), THE FLIGHT CREW OBSERVED AN EICAS MESSAGE INDICATING “STAB CH 2 INOP.” THE CREW ATTEMPTED TO RESET THE SYSTEM; HOWEVER, THE RESET WAS UNSUCCESSFUL. THE AIRCRAFT SUBSEQUENTLY RETURNED TO THE RAMP FOR MAINTENANCE EVALUATION AND CORRECTIVE ACTION.

Source: SDR FJ7A202605270001 · FAA SDRS
J · 2025-04-08 Matched by certificate designator
N171AM · ATA 2740

CREW REPORTED AFTER DEPARTURE WHEN PILOT TRIED TO TRIM STABILIZER BOTH CHANNELS DISCONNECTED. AFTER ABNORMAL CHECKLIST WAS PERFORMED CREW WAS ABLE TO CONNECT CHANNEL 2. CREW RETURNED TO FIELD AND LANDED WITHOUT INCIDENT. MAINTENANCE TROUBLESHOOT TO FAULT HSTCU BOX.

Source: SDR 2025FA0000274 · FAA SDRS
E J S · 2020-12-30 Matched by certificate designator
N317MM · ATA 3222

DURING A NORMAL CLIMB-OUT AFTER A TAKEOFF ON RUNWAY 25 AT KSBA, "POSITIVE RATE" WAS CALLED BY THE PM (SIC), AND THE PF (PIC) RESPONDED WITH "GEAR UP, YAW DAMPER". UPON GEAR RETRACTION, THE CREW NOTICED THAT THE NOSE RED "UNSAFE" LIGHT REMAINED ILLUMINATED. THIS WAS ALSO ACCOMPANIED BY A SLIGHT INCREASE IN AIRFLOW NOISE COMPARED TO NORMAL GEAR RETRACTION. THE CREW LEVELED OFF AT 2,000 FEET AND BEGAN TO TROUBLE SHOOT. THE GEAR WAS CYCLED TWICE, AND BOTH TIMES THE SAME INDICATION PRESENTED. AFTER THIS, THE CREW DID A FLY-BY WITH TOWER AND THE TOWER COMMENTED THAT THE NOSE GEAR DOORS WERE OPEN AND THE NOSE GEAR APPEARED ONLY PARTIALLY RETRACTED. WHEN THE GEAR WAS LOWERED, THE CREW HAD "3 GREEN, NO RED" INDICATING ALL 3 GEAR WERE DOWN AND LOCKED. AFTER DECIDING THAT THE BEST COURSE OF ACTION WAS TO RETURN TO KSBA AND LAND, THE CREW FLEW AROUND FOR APPROXIMATELY 1.5 HOURS (ON VECTORS WITH SBA APPROACH CONTROL) IN ORDER TO BURN ENOUGH GAS TO COME DOWN BELOW MAXIMUM LANDING WEIGHT. ONCE THE CREW WAS WITHIN MAX LANDING WEIGHT, ONE MORE FLY-BY WAS DONE WITH THE GEAR EXTENDED. THE TOWER COMMENTED THAT ALL 3 GEAR APPEARED TO BE DOWN, LOCKED, AND STRAIGHT. THE CREW BROUGHT THE AIRPLANE AROUND THE PATTERN AND CAME TO A FULL STOP LANDING. EMERGENCY EQUIPMENT/PERSONNEL WERE STANDING BY JUST IN CASE. LANDING WAS UNEVENTFUL. NOSE GEAR HELD UP AND EVEN ALLOWED FOR NOSE STEERING. THE CREW TAXIED THE AIRCRAFT BACK TO PARKING AND SHUT DOWN.

Source: SDR FJ7A20210105002 · FAA SDRS
O · 2019-11-14 Matched by certificate designator
N178AM · ATA 3244

DURING A NORMAL TAKEOFF ROLL ON 19L AT KLAS ONE OF THE LEFT MAIN TIRES BLEW DUE TO A SUSPECTED ENCOUNTER WITH FOD AT APPROXIMATELY 105 KNOTS WITH A V1 TAKEOFF DECISION SPEED OF 136; THIS WAS ASSOCIATED WITH AN AUDIBLE "BANG". SHORTLY THEREAFTER THE AIRCRAFT BEGAN TO LOSE DIRECTIONAL CONTROL AND THE CAPTAIN ELECTED TO ABORT THE TAKEOFF. THIS SERIES OF EVENTS CAUSED THE REMAINING LEFT TIRE TO BLOW AND CAUSED THE LEFT WHEEL ASSEMBLIES AND BRAKES TO DRAG ON THE RUNWAY DURING THE ABORT DECELERATION AND STOP. THE AIRCRAFT REMAINED ON THE RUNWAY THE ENTIRE TIME. AFTER THE AIRCRAFT CAME TO A STOP ON RUNWAY 19L THE CREW PERFORMED A PRECAUTIONARY EVACUATION AND SHUTDOWN OF THE AIRCRAFT.

Source: SDR 2020F00047 · FAA SDRS
J · 2017-09-20 Matched by certificate designator
N178AM · ATA 2130

ON DEPARTING KCXY "CABIN ALT" LIGHT ILLUMINATED PASSING THROUGH 10,000 FEET. CAPTAIN ELECTED TO LAND AT KMDT INSTEAD OF THE FILED DESTINATION (FXE).

Source: SDR 2017F00178 · FAA SDRS
O · 2007-08-09 Matched by certificate designator
N174AM · ATA 3411

INDICATION OF NO PITOT HEAT ON ANNUNCIATOR PANEL.

Source: SDR FJ7A116867 · FAA SDRS
O · 2007-05-29 Matched by certificate designator
N174AM · ATA 2432

BATTERY, CONTINUALLY WEAK ON STARTS.

Source: SDR FJ7A115661 · FAA SDRS
O · 2007-05-25 Matched by certificate designator
N174AM · ATA 7261

CLAMP WELDED TO TUBE CRACKED, LEAVING TUBE UNSUPPORTED.

Source: SDR FJ7A115622 · FAA SDRS
O · 2007-05-24 Matched by certificate designator
N174AM · ATA 7261

CLAMP WELDED TO TUBE, CRACKED, LEAVING TUBE UNSUPPORTED.

Source: SDR FJ7A115621 · FAA SDRS
K · 2007-05-17 Matched by certificate designator
N174AM · ATA 6320

FIBERGLASS GASKET INSTALLED ON BOTH SIDES OF RING GEAR CRACKED AND PUSHED OUT CAUSING AN OIL LEAK.

Source: SDR FJ7A115620 · FAA SDRS

Linked aircraft

N-numberMake / modelYearStatusLink basis
N171AMBOMBARDIER INC CL-600-2B162010Valid RegistrationMatched by certificate designator
N178AMGATES LEARJET CORP 55CValid RegistrationMatched by certificate designator
N317MMLEARJET INC 602001Valid RegistrationMatched by certificate designator
N62LJGATES LEARJET CORP 551982Valid RegistrationMatched by certificate designator
N717AMGATES LEARJET CORP 551984Valid RegistrationMatched by certificate designator